The Marshall County Coal Company et al v. Oliver et al
Filing
14
MEMORANDUM in Opposition to Plaintiff's 21 Motion for a Temporary Restraining Order by Home Box Office, Inc., Partially Important Productions, LLC, Time Warner, Inc. . (Attachments: # 1 Exhibit A, # 2 Exhibit B, # 3 Exhibit C, # 4 Exhibit D, # 5 Exhibit E, # 6 Exhibit E (con'd), # 7 Exhibit F, # 8 Exhibit G)(Fitzsimmons, Robert) Modified on 7/28/2017 to link to Motion (kac).
Exhibit E
CAI-2007-15-17, 19-24
UNITED STATES
DEPARTMENT OF LABOR
MINE SAFETY AND HEALTH ADMINISTRATION
COAL MINE SAFETY AND HEALTH
REPORT OF INVESTIGATION
Underground Coal Mine
Fatal Underground Coal Burst Accidents
August 6 and 16, 2007
Crandall Canyon Mine
Genwal Resources Inc
Huntington, Emery County, Utah
ID No. 42-01715
Accident Investigators
Richard A. Gates
District Manager, District 11, Birmingham, AL
Michael Gauna
Mining Engineer, Roof Control Division, Technical Support, Triadelphia, WV
Thomas A. Morley
Mining Engineer, Ventilation Division, Technical Support, Triadelphia, WV
Joseph R. O’Donnell Jr.
Supervisory Coal Mine Inspector, District 11, Bessemer, AL
Gary E. Smith
Supervisory Coal Mine Inspector, District 2, New Stanton, PA
Timothy R. Watkins
Assistant District Manager, District 6, Pikeville, KY
Chris A. Weaver
Supervisory Coal Mine Inspector, District 3, Bridgeport, WV
Joseph C. Zelanko
Supervisory Mining Engineer, Roof Control Division, Technical Support, Pittsburgh, PA
Originating Office
Mine Safety and Health Administration
Office of the Administrator, Coal Mine Safety and Health
1100 Wilson Boulevard, Arlington, Virginia, 22209
Kevin G. Stricklin, Administrator
PREFACE
This investigation was conducted by the Mine Safety and Health Administration (MSHA) under the
authority of The Federal Mine Safety and Health Act of 1977 (Mine Act). The Mine Act requires
that authorized representatives of the Secretary of Labor make investigations in coal and other mines
for the purpose of obtaining, utilizing, and disseminating information relating to the causes of
accidents. The objective of MSHA’s accident investigations is to determine the root cause(s) of the
accident and to utilize and share this information with the mining community and others for the
purpose of preventing similar occurrences. MSHA’s accident investigations include determinations
of whether violations of the Mine Act or implementing regulations contributed to the accident. In
addition to providing critical, potentially life-saving information, the findings of these investigations
provide a basis for formulating and evaluating MSHA health and safety standards and policies.
In addition to the traditional accident investigation, the Secretary of Labor also appointed an
independent review team. The independent review will consist of a thorough examination of written
mine plans (including the mine’s approved roof control plan), inspection records, and other
documents relevant to the Crandall Canyon Mine and interviews of MSHA employees with personal
knowledge of MSHA’s inspection responsibilities and enforcement procedures at the mine. This
review will provide a comparison of MSHA’s actions at the Crandall Canyon Mine with the
requirements of the Mine Act (as amended by the Mine Improvement and New Emergency Response
Act of 2006), its standards and regulations, and MSHA policies and procedures. The findings of the
independent review will result in the development of recommendations to improve MSHA’s
enforcement program and the agency’s oversight of rescue and recovery programs in the aftermath
of mine accidents. Copies of this review will be made available to the families of the miners
involved in the Crandall Canyon Mine accident, Congress, and the public.
The tragic accidents at the Crandall Canyon Mine in August 2007 occurred when overstressed coal
pillars suddenly failed, violently expelling coal from the pillars into the mine openings. Locally
referred to in Utah as a “bounce,” terminology for this type of event differs regionally, and is also
known as an outburst, bump, or burst. Bounces and bumps are broader terms that can include any
dull, hollow, or thumping sound produced by movement or fracturing of strata as a result of mining
operations. In many cases, vibrations in the strata resulting from such movement can be felt by
miners and detected by seismographic instruments. Bounces resulting from intentional caving,
where strata in active workings remain intact, are common in deep coal mines and do not pose a
threat to miners. However, coal or rock bursts, also known as outbursts 1*, are those bounces
specifically characterized by the sudden and violent failure of overstressed rock or coal resulting in
the instantaneous release of large amounts of accumulated energy with the ejection of material.
When such events occur in active workings, they pose a serious hazard to miners. Federal mine
safety standards, therefore, require that the roof, face, and ribs be controlled to protect persons from
hazards related to bursts through proper ground support and pillar dimensions. Also, coal or rock
outbursts that cause withdrawal of miners or which disrupt regular mining activity for more than one
hour are defined as accidents (even if no miners are injured) and must be immediately reported to
MSHA, as required by relevant portions of 30 CFR 50. Definitions for these and other terms are
provided in Appendix Y. Any references to product manufacturers, distributors, or service providers
are intended for factual documentation and do not imply endorsement by MSHA.
*
References identified by superscript numbers are listed in Appendix Z.
i
TABLE OF CONTENTS
EXECUTIVE SUMMARY..................................................................................................... 1
GENERAL INFORMATION ................................................................................................ 5
DESCRIPTION OF THE ACCIDENT................................................................................. 8
August 6 Accident Description....................................................................................... 8
Underground Rescue Efforts ....................................................................................... 14
Attempts to Explore South Barrier Section and Main West Sealed Area ........... 14
Rescue Efforts in South Barrier Section Nos. 3 and 4 Entries.............................. 16
Rescue Efforts in South Barrier Section No. 1 Entry ............................................ 18
Preparation for Rescue Effort in No. 1 Entry....................................................... 18
Material Clean-Up from the No. 1 Entry .............................................................. 21
August 16 Accident Description................................................................................... 26
Surface Rescue Efforts.................................................................................................. 33
Attempt to Locate Miners - Boreholes .................................................................... 33
Description of Boreholes........................................................................................ 37
Attempt to Locate Miners - MSHA’s Seismic System ........................................... 41
Suspension of Rescue Efforts ....................................................................................... 41
Mine Closure .......................................................................................................... 42
INVESTIGATION OF THE ACCIDENT.......................................................................... 43
DISCUSSION ........................................................................................................................ 44
August 6 Accident Discussion ...................................................................................... 44
Background for Ground Control Analysis ............................................................. 47
General Mine Geology ........................................................................................... 47
Mining Horizon and Mining Width ...................................................................... 48
Primary and Supplemental Roof Support ............................................................. 49
Accidents Related to Ground Control Failures..................................................... 50
Room and Pillar Retreat Coal Mining Overview .................................................. 51
Nature and Extent of Failure ................................................................................... 51
Underground Observations.................................................................................... 52
Borehole Observations ........................................................................................... 54
Surface Subsidence Determined from GPS Surveys ............................................ 54
Surface Subsidence Determined from InSAR Analyses....................................... 55
Seismology .............................................................................................................. 57
Time of the Accident .............................................................................................. 59
Summary - Nature and Extent of Failure ............................................................. 60
Main West Ground Control History ....................................................................... 61
Main West Development ........................................................................................ 61
Longwall Panel Extraction .................................................................................... 62
North Barrier Section Development ...................................................................... 66
North Barrier Section Pillar Recovery .................................................................. 67
March 10, 2007, Coal Outburst ............................................................................. 69
South Barrier Section Development ...................................................................... 71
South Barrier Section Pillar Recovery .................................................................. 72
Summary – Main West Ground Control History .................................................. 74
Analysis of Collapse .................................................................................................. 74
Safety/Stability Factors .......................................................................................... 75
Analysis of Retreat Mining Pillar Stability (ARMPS) .......................................... 76
Finite Element Analysis......................................................................................... 86
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Boundary Element Analysis .................................................................................. 91
Boundary Element Analyses of GRI Mining ........................................................ 96
Summary - Analyses of Collapse ......................................................................... 107
Critique of Mine Design ......................................................................................... 108
Previous Ground Control Studies at Crandall Canyon Mine ............................ 108
Barrier Pillar Design............................................................................................ 109
Agapito Associates, Inc. Analyses ....................................................................... 113
Roof Control Plan ................................................................................................ 130
Summary – Critique of Mine Design................................................................... 136
Mine Ventilation...................................................................................................... 136
Mine Ventilation System ...................................................................................... 136
Post-Accident Mine Ventilation........................................................................... 138
Ventilation in Area of Entrapment...................................................................... 140
Air Quality in South Barrier Section Pillar Recovery Area ............................... 140
Attempt to Locate Miners with Boreholes ............................................................ 145
Boreholes Drilled Prior to August 16 .................................................................. 145
Boreholes Drilled After August 16 ...................................................................... 146
MSHA’s Seismic Location Systems ....................................................................... 148
Emergency Response Plan...................................................................................... 149
Notification........................................................................................................... 149
Self-Rescuers ........................................................................................................ 150
Post-Accident Logistics ........................................................................................ 150
Lifelines ................................................................................................................ 151
Post-Accident Communication ............................................................................ 151
Post-Accident Tracking........................................................................................ 152
Local Coordination .............................................................................................. 152
Training ................................................................................................................ 152
Post-Accident Breathable Air .............................................................................. 152
Additional Provisions ........................................................................................... 153
Family Liaisons ....................................................................................................... 153
Mine Emergency Evacuation and Firefighting Program of Instruction............ 153
Procedures for Evacuation .................................................................................. 154
Atmospheric Monitoring System (AMS) Fire Detection .................................... 154
Training Plan........................................................................................................... 155
August 16 Accident Discussion .................................................................................. 155
Ground Control during Rescue Efforts ................................................................ 157
Selection of Entry for Rescue Work .................................................................... 157
Work Procedures under Operator’s Recovery Plan ........................................... 158
Pillar Burst Support System................................................................................. 159
Seismic Activity Recorded by UUSS during Rescue Efforts............................... 162
Pillar Bounce and Burst Activity during Rescue in No. 1 Entry ........................ 164
Ground Condition Monitoring .............................................................................. 165
Ventilation on August 16 ........................................................................................ 167
Post-Accident Tracking .......................................................................................... 168
Local Coordination ................................................................................................. 168
ROOT CAUSE ANALYSIS ............................................................................................... 169
CONCLUSION.................................................................................................................... 171
ENFORCEMENT ACTIONS ............................................................................................ 174
Appendix A - Persons Participating in the Investigation ................................................ A-1
Appendix B - Victim Data Sheets ...................................................................................... B-1
iii
Appendix C - Safety Zone Map ......................................................................................... C-1
Appendix D - Mine Development History Map................................................................ D-1
Appendix E - AAI May 5, 2000, Report .............................................................................E-1
Appendix F - AAI July 20, 2006, Draft Report .................................................................F-1
Appendix G - AAI August 9, 2006, Report ....................................................................... G-1
Appendix H - AAI December 8, 2006, Report .................................................................. H-1
Appendix I - AAI April 18, 2007, Report............................................................................I-1
Appendix J - Roof Control Plan for Recovering South Barrier Section......................... J-1
Appendix K - Massive Pillar Collapse............................................................................... K-1
Appendix L - Subsidence Data............................................................................................L-1
Appendix M - Neva Ridge Technologies Report ............................................................. M-1
Appendix N - Seismic Analysis .......................................................................................... N-1
Appendix O - Images of March 10, 2007, Coal Outburst Accident................................ O-1
Appendix P - ARMPS Method Using Barrier Width Modified Based on
Bearing Capacity..........................................................................................P-1
Appendix Q - Finite Element Analysis of Barrier Pillar Mining
at Crandall Canyon Mine........................................................................... Q-1
Appendix R - Description of BEM Numerical Models .................................................... R-1
Appendix S - Back-Analysis of the Crandall Canyon Mine Using the
LaModel Program........................................................................................S-1
Appendix T - Abutment Load Transfer.............................................................................T-1
Appendix U - Coal Properties Input ................................................................................. U-1
Appendix V - Rock Mass Properties ................................................................................. V-1
Appendix W - MSHA Main West 2006 ARMPS............................................................. W-1
Appendix X - Mine Ventilation Plan ................................................................................. X-1
Appendix Y - Glossary of Mining Terms as used in this Report .................................... Y-1
Appendix Z - References ....................................................................................................Z-1
TABLES
Table 1 - Accident Incidence Rates....................................................................................... 8
Table 2 - Summary of Borehole Size, Depth, Drill Rate, Location, Voids, and O2
Concentration ............................................................................................... 36
Table 3 - Analysis Results of Air Samples Taken at Boreholes ....................................... 38
Table 4 - NIOSH Pillar Design Considerations................................................................. 78
Table 5 - Pillar Stability Factors for Continuous Haulage Panel Back-Analysis........... 80
Table 6 - Pillar Stability Factors for South Mains Back-Analysis for Areas
with Side and Active Gobs........................................................................... 82
Table 7 - Pillar Stability Factors for North Barrier Section ............................................ 83
Table 8 - Pillar Stability Factors for South Barrier Section ............................................ 84
Table 9 - Barrier Pillar Design Formulas ........................................................................ 110
Table 10 - Coal Properties Calculated by AAI................................................................ 114
Table 11 - Effect Thresholds for Exposure to Reduced Oxygen.................................... 141
Table 12 - Results of Air Sample Analysis ....................................................................... 143
Table 13 - Handheld Gas Detector Concentrations ........................................................ 144
Table 14 - Crandall Canyon Longwall Subsidence Parameters,
Values, and Comparisons .......................................................................... L-8
Table 15 - LaModel Confined Coal Strength ..................................................................U-1
iv
FIGURES
Figure 1 - Map of Accident Sites........................................................................................viii
Figure 2 - Location of Miners during August 6 Accident................................................. 10
Figure 3 - South Barrier Section Rescue Area .................................................................. 15
Figure 4 - View of No. 3 Entry after August 7 Burst ........................................................17
Figure 5 - Hardwood Posts Installed with Jackpots in No. 1 Entry ................................ 20
Figure 6 - RocProps, Cables, and Chain-link Fencing Installed in the No. 1 Entry ...... 20
Figure 7- Damaged Roof Bolts and Torn Mesh after August 6 Accident ....................... 22
Figure 8 - Damaged Roof Bolts in No. 1 Entry after August 6 Accident ........................ 22
Figure 9 - Steel Channels Installed in No. 1 Entry to Support Deteriorated Roof ........ 23
Figure 10 - No. 1 Entry Packed with Coal Rubble Inby Crosscut 124............................ 24
Figure 11 - Continuous Mining Machine in Loading Area Inby Crosscut 124.............. 24
Figure 12 – Damage to Outby Portion of Pillar on Right Side of No. 1 Entry
(Outby August 16 Accident Site) ................................................................ 27
Figure 13 - 20-foot Deep Void over Pillar on Right Side of No. 1 Entry
following August 16 Accident...................................................................... 28
Figure 14 - August 16, 2007, Coal Burst Effects and Location of Injured Miners ........ 28
Figure 15 – Clean-up Area Following the Fatal August 16, 2007, Accident................... 32
Figure 16 - Mountainous Terrain where Roads and Drill Pads were Constructed ....... 33
Figure 17 - Heliportable Drill Rig ...................................................................................... 34
Figure 18 - Drill Rig at Borehole No. 4............................................................................... 35
Figure 19 - Borehole Locations Intersecting Underground Workings ........................... 35
Figure 20 - Surface Location of Boreholes......................................................................... 36
Figure 21 - Arrangement for Lowering Robot into Mine Through a Borehole ............. 40
Figure 22 - Robot Being Lowered Into Borehole .............................................................. 40
Figure 23 - General Stratigraphic Column for Crandall Canyon Mine ......................... 48
Figure 24 - Hour Glass Shape of Stressed Pillars ............................................................. 49
Figure 25 - Example of a Pillar Recovery Cut Sequence.................................................. 51
Figure 26 - Extent of Pillar Rib Damage Outby Crosscut 119......................................... 52
Figure 27 - Normal Main West Pillar Rib Conditions...................................................... 53
Figure 28 - Main West Pillar Rib Condition showing Recent Sloughage
from Abutment Stress.................................................................................. 53
Figure 29 - Borehole Locations and Conditions Observed .............................................. 54
Figure 30 - Subsidence Profiles over Panels 13 to 15........................................................55
Figure 31 - Surface Deformation from Neva Ridge InSAR Analyses
(June to Sept. 2007) ...................................................................................... 56
Figure 32 – Double Difference Locations of Seismic Events, August 6-27, 2007 ........... 58
Figure 33 - Combined Data and Likely Extent of Collapse ............................................. 61
Figure 34 – Initial Main West Barrier Pillars after Panel 13 Mining
showing Overburden.................................................................................... 62
Figure 35 - Abutment Stress due to Cantilevered Strata from Mining .......................... 63
Figure 36 – South Mains “Rooming Out” Pillar Recovery Sequence ............................. 65
Figure 37 - North Barrier Section Mining showing Overburden .................................... 66
Figure 38 – Stopping Damaged during March 2007 Coal Outburst Accident on
North Barrier Section .................................................................................. 70
Figure 39 –Damage in No. 4 Entry after the March 2007 Coal Outburst
Accident on North Barrier Section............................................................. 70
Figure 40 - South Barrier Section Mining showing Overburden .................................... 71
Figure 41 - South Barrier Section Pillar Recovery Cut Sequence................................... 72
v
Figure 42 - Illustration of ARMPS Input Related to Panel Geometry............................ 77
Figure 43 - ARMPS Case History Data Base (Chase et al.7)............................................ 78
Figure 44 - 1st North Mains Left Panel ARMPS Calculation Areas............................... 80
Figure 45 - ARMPS Stability Factors at Crandall Canyon Mine.................................... 81
Figure 46 - South Mains ARMPS Calculation Areas .......................................................82
Figure 47 - Methods of Incorporating a Bleeder Pillar in ARMPS Analyses ................ 84
Figure 48 - ARMPS Layout for Simplified Main West Analysis..................................... 85
Figure 49 - Element Safety Factors about a Barrier Pillar after Longwall Mining ...... 88
Figure 50 - Element Safety Factor Distribution after North Barrier Section
Development ................................................................................................. 89
Figure 51 - Element Safety Factor Distribution after South Barrier Section
Development ................................................................................................. 90
Figure 52 - Illustration of Boundary Element Model Components................................. 91
Figure 53 - LaModel Grid Boundaries and Overburden Stress ...................................... 94
Figure 54 - Optimum Model Before and After South Barrier Section Mining.............. 95
Figure 55 - Optimum Model after August 6 Failure......................................................... 95
Figure 56 - Distribution of Vertical Stress in the South Barrier Section........................ 97
Figure 57 - Vertical Stress Increases due to Barrier Mining ........................................... 98
Figure 58 - Effect of Barrier Mining on Average Pillar Stress ........................................ 98
Figure 59 - Pillar Safety Factors for Pillar Recovery Outby Crosscut 139 .................... 99
Figure 60 - Cross-Section through South Barrier Section during Pillar Recovery ..... 100
Figure 61 - Effect of Bottom Mining on Pillar Geometry............................................... 101
Figure 62 - Model Representation of Bottom Mining in the Remnant Barrier ........... 102
Figure 63 - Distribution of Vertical Stress in the South Barrier Section...................... 102
Figure 64 - Differences in Vertical Stress due to Bottom Mining.................................. 103
Figure 65 - Element Safety Factors .................................................................................. 104
Figure 66 – Pillar Safety Factors Modeled with a 120-foot Southern Barrier ............. 105
Figure 67 – Pillar Safety Factors Modeled with a 140-foot Southern Barrier
for Development Mining............................................................................ 106
Figure 68 - Barrier Pillar Sizes from Empirical Methods.............................................. 111
Figure 69 – Plan View of Pillars showing Coal Property Elements .............................. 114
Figure 70 - Simulation Process Flow Chart..................................................................... 117
Figure 71 - Modeled Yield Condition - Partial Retreat in 9th Left Panel .................... 118
Figure 72 - Modeled Vertical Stress – Retreat Completed in 9th Left Panel ............... 119
Figure 73 - Notes Made by AAI on March 16, 2007 .......................................................120
Figure 74 - AAI Model Results of Vertical Stress in March 2007 Burst Area ............. 121
Figure 75 - Element Safety Factors with Coal Properties Distributed
as Indicated in AAI Report ....................................................................... 122
Figure 76 - Element Safety Factors using Modified Coal Strength Property
Distribution, Gob Properties, and Lamination Thickness ..................... 123
Figure 77 - AAI Notation on Plot of Model Results ........................................................ 124
Figure 78 – AAI Modeled Vertical Stress Results Comparing Effects of
Crosscut Spacing ........................................................................................ 125
Figure 79 - ARMPS Analysis Geometries used by AAI ................................................. 126
Figure 80 - Pillar Stability Factors from NIOSH ARMPS Database
for Depths Over 1,500’............................................................................... 127
Figure 81 – Crandall Canyon Mine ARMPS Stability Factors showing AAI South
Barrier Calculations .................................................................................. 129
Figure 82 - Comparison of South Barrier Roof Control and Ventilation Plans .......... 134
Figure 83 - Mark Up Map Provided to Mine Management on July 31, 2007 .............. 135
vi
Figure 84 - Ventilation System before August 6 Accident ............................................. 137
Figure 85 - Fan Pressure at the Time of the August 6 Accident .................................... 138
Figure 86 - Ventilation Controls after Accidents ............................................................ 139
Figure 87 – Approx. Time of Useful Consciousness vs. Oxygen Concentration .......... 141
Figure 88 – Steel Cables Connected to RocProps ........................................................... 160
Figure 89 - New Roof Bolts and New Wire Mesh Installed in the No. 1 Entry ............ 161
Figure 90 - Sheet of Lexan Suspended from Mine Roof................................................. 161
Figure 91 - Initial Location of Seismic Events August 6-16, 2007 ................................. 163
Figure 92 - Double Difference Locations of Seismic Events, August 6-16, 2007 .......... 163
Figure 93 – Bounce or Burst Activity Recorded in Command Center Log Book........ 164
Figure 94 - No. 1 Entry Rescue Clean-up Progress Plotted by Day .............................. 165
Figure 95 - Convergence Measurements.......................................................................... 167
Figure 96 - How Satellites and Radar Interferometry Detect Surface Movement ...... L-1
Figure 97 – Example of Interferogram Color Banding from
USGS Fact Sheet 2005-3025 ...................................................................... L-2
Figure 98 - USGS InSAR Image of Subsidence above the Accident Site...................... L-3
Figure 99 - Surface Deformation from USGS InSAR..................................................... L-4
Figure 100 - InSAR Vertical Subsidence Contours (cm) from Neva Ridge.................. L-4
Figure 101 - Comparison of Vertical Subsidence from Interpreted USGS and
Neva Ridge InSAR Results........................................................................ L-5
Figure 102 - InSAR Vertical Subsidence Contours & GPS Subsidence Line Data ..... L-6
Figure 103 - Longwall Panels 13 to 15 GPS Surveyed Subsidence Profiles.................. L-7
Figure 104 - Mining-Induced Seismicity in Utah ............................................................N-1
Figure 105 - Locations of UUSS Seismographs in the Wasatch Plateau.......................N-2
Figure 106 – Locations of Selected Events showing Progressive Refinements
Using Three Methods.................................................................................N-4
Figure 107 - Observed and Calculated Locations for Events ........................................N-5
Figure 108 - Calculated Double Difference Locations and the Location of Mining Color
Coded by Month.........................................................................................N-6
Figure 109 – Seismic Location of the August 6 Accident and Following Events..........N-7
Figure 110 - P-Wave First Motion Analysis Examples...................................................N-8
Figure 111 - Vertical Component Waveform Data for August 6, 2007 Event..............N-9
Figure 112 - Source Type Plot from Ford et al. (2008). ................................................N-10
Figure 113 – Depth Analysis of August 6, 2007 event from Ford et al 2008...............N-11
Figure 114 - General Strain-Softening Element Characteristics...................................U-2
Figure 115 - Traditional Strain-Softening Element Distribution ..................................U-3
Figure 116 - Strain-Softening Element Distribution to Account for
Corner Effects (as Deployed by AAI).......................................................U-4
Figure 117 - North Barrier MSHA 2006 ARMPS Model..............................................W-2
Figure 118 - South Barrier MSHA 2006 ARMPS Model ..............................................W-3
vii
Figure 1 - Map of Accident Sites
EXECUTIVE SUMMARY
The August 6 and 16 Accidents
The Crandall Canyon Mine, in Emery County, Utah, was operated by Genwal Resources Inc
(GRI), whose parent company was acquired by a subsidiary of Murray Energy Corporation in
August 2006. On August 6, 2007, at 2:48 a.m., a catastrophic coal outburst accident occurred
during pillar recovery in the South Barrier section, while the section crew was mining the barrier
near crosscut 139. The outburst initiated near the section pillar line (the general area where the
miners were working) and propagated toward the mine portal.
Within seconds, overstressed pillars failed throughout the South Barrier section over a distance of
approximately ½ mile. Coal was expelled into the mine openings on the section, likely causing
fatal injuries to Kerry Allred, Don Erickson, Jose Luis Hernandez, Juan Carlos Payan, Brandon
Phillips, and Manuel Sanchez. The barrier pillars to the north and south of the South Barrier
section also failed, inundating the section with lethally oxygen-deficient air from the adjacent
sealed area(s), which may have contributed to the death of the miners. The resulting magnitude
3.9 seismic event shook the mine office three miles away and destroyed telephone communication
to the section.
Federal and local authorities responded to the accident. MSHA issued an order pursuant to section
103(k) of the Mine Act that required GRI to obtain MSHA approval for all plans to recover or
restore operations to the affected area. Mine rescue teams were organized, a command center was
established, and a rescue effort was initiated. After unsuccessful attempts to reach the miners by
crawling over the debris, GRI developed a rescue plan, approved by MSHA, to access the
entrapped miners by loading burst debris from the South Barrier section No. 1 entry using a
continuous mining machine. These efforts began on August 8 at crosscut 120.
On August 16, 2007, at 6:38 p.m., a coal outburst occurred from the pillar between the No. 1 and
No. 2 entries, adjacent to rescue workers as they were completing the installation of ground
support behind the continuous mining machine. Coal ejected from the pillar dislodged standing
roof supports, steel cables, chain-link fence, and a steel roof support channel, which struck the
rescue workers and filled the entry with approximately four feet of debris. Ventilation controls
were damaged and heavy dust filled the clean-up area, reducing visibility and impairing breathing.
Also, air from inby the clean-up area containing approximately 16% oxygen migrated over the
injured rescue workers. Nearby rescue workers immediately started digging out the injured miners
and repairing ventilation controls. Two mine employees, Dale Black and Brandon Kimber, and
one MSHA inspector, Gary Jensen, received fatal injuries. Six additional rescue workers,
including an MSHA inspector, were also injured.
Underground rescue efforts were suspended while a group of independent ground control experts
reevaluated conditions and rescue methods, although surface drilling continued. In total, seven
boreholes were drilled from the surface to the mine workings. Each successive borehole provided
information as to conditions in the affected area and helped to determine the location of the next
hole. None of the boreholes identified the location of the entrapped miners. Ultimately, it was
learned that the area where the miners were believed to have last been working sustained extensive
pillar damage and had levels of oxygen that would not have sustained life.
Explanation of the August 6 Collapse
The August 6 collapse was not a “natural” earthquake, but rather was caused by a flawed mine
design. Ultimately, it is most likely the stress level exceeded the strength of a pillar or group of
1
pillars near the pillar line and that local failure initiated a rapid and widespread collapse that
propagated outby through the large area of similar sized pillars.
Three separate methods of analysis employed as part of MSHA’s investigation confirmed that the
mining plan was destined to fail. Results of the first method, Analysis of Retreat Mining Pillar
Stability (ARMPS), were well below NIOSH recommendations. The second method, a finite
element analysis of the mining plan, indicated a decidedly unsafe, unstable situation in the making
even without pillar recovery. Similarly, the third method, boundary element analysis,
demonstrated that the area was primed for a massive pillar collapse. Seismic analyses and
subsidence information employed in the investigation provided clarification that the collapse was
most likely initiated by the mining activity. Information provided by the University of Utah
Seismograph Stations (UUSS) and from satellite radar images also helped in defining the nature
and extent of the collapse.
The extensive pillar failure and subsequent inundation of the section by oxygen-deficient air
occurred because of inadequacies in the mine design, faulty pillar recovery methods, and failure to
adequately revise mining plans following coal burst accidents.
GRI’s mine design was inadequate and incorporated flawed design recommendations from
contractor Agapito Associates, Inc. (AAI). Although AAI had many years of experience at this
mine and was familiar with the mine conditions, they conducted engineering analyses that were
flawed. These design issues and faulty pillar recovery methods resulted in pillar dimensions that
were not compatible with effective ground control to prevent coal bursts under the deep
overburden and high abutment loading that existed in the South Barrier section.
AAI’s analysis using the engineering model known as “ARMPS” was inappropriately applied.
They used an area for back-analysis that experienced poor ground conditions and did not consider
the barrier pillar stability factors in any of their analyses. The mine-specific ARMPS design
threshold proved to be invalid, as evidenced by March 7 and 10, 2007, coal outburst accidents and
other pillar failures. Despite these failures, AAI recommended a pillar design for the South
Barrier section that had a lower calculated pillar stability factor than recommended by the National
Institute for Occupational Safety and Health (NIOSH) criteria, lower than established by their
mine specific criteria, and lower than the failed pillars in the North Barrier section. AAI
performed the ARMPS analysis for the South Barrier section, but did not include these results in
their reports that were presented to MSHA in support of GRI’s plan submittal.
AAI’s analysis using the engineering model known as “Lamodel” was flawed. They used an area
for back-analysis that was inaccessible and could not be verified for known ground conditions,
which resulted in an unreliable calibration and the selection of inappropriate model parameters.
These model parameters overestimated pillar strength and underestimated load. AAI modeled
pillars with cores that would never fail regardless of the applied load, which was not consistent
with realistic mining conditions. They did not consider the indestructible nature of the modeled
pillars in their interpretation of the results. Modeled abutment stresses from the adjacent longwall
panels were underestimated and inconsistent with observed ground behavior and previous studies
at this and nearby mines.
AAI managers did not review input and output files for accuracy and completeness. They also did
not review vertical stress and total displacement output at full scale, which would have shown
unrealistic results and indicated that corrections were needed to the model. Following the
March 10 coal outburst accident, AAI modified the model, but failed to correct the significant
2
model flaws. They did not make further corrections to the model when this analysis result still did
not accurately depict known failures that AAI and GRI observed in the North Barrier section.
The mine designs recommended by AAI and implemented by GRI did not provide adequate
ground stability to maintain the ventilation system. The designs did not consider the effects of
barrier pillar and remnant barrier pillar instability on separation of the working section from the
adjacent sealed areas. Failure of the barrier pillars or remnant barrier pillars resulted in inundation
of the section by lethally oxygen-deficient air. AAI and GRI also did not consider the effects of
ground stability on ventilation controls in the bleeder system. GRI allowed frequent destruction of
ventilation controls by ground movement and by air blasts from caving. GRI mined cuts from the
barrier pillar in the South Barrier section between crosscuts 139 and 142 intended to be left
unmined to protect the bleeder system.
GRI’s mining practices, including bottom mining and additional barrier slabbing between
crosscuts 139 and 142, reduced the strength of the barrier and increased stress levels in the vicinity
of the miners. As pillars were recovered in the South Barrier section, bottom coal (a layer of coal
left in the mine floor after initial mining) was mined from cuts made into the production pillars
and barrier. The effect of this activity was to reduce the strength of the remnant barrier behind the
retreating pillar line. Bottom mining was not addressed in AAI’s model to evaluate the mine
design or in GRI’s approved roof control plan. Similarly, barrier mining was conducted in
violation of the approved roof control plan. A portion of the barrier immediately inby the last
known location of the miners was mined even though it was required by the roof control plan to be
left unmined. Barriers are solid blocks of coal left between two mines or sections of a mine to
provide protection. Although neither of these actions is a fundamental cause of the August 6
collapse, they increased the amount of load transferred to pillars at the working face and reduced
the strength of the barrier adjacent to it.
The mine operator did not report three coal outbursts that occurred prior to August 6 to MSHA or
properly revise its mining plan following these coal bursts. Between late 2006 and February 2007,
the 448-foot wide barrier north of Main West was developed by driving four entries parallel to the
existing Main West entries. Smaller barriers remained on either side of the new section entries (53
feet wide on the south side and 135 feet wide on the north side). The 135-foot wide barrier that
separated the North Barrier section from the adjacent longwall panel gob was insufficient to
isolate the workings from substantial abutment loading. Despite the high stress levels associated
with deep cover (up to 2,240 feet of overburden) and longwall abutment stress, the section
remained stable during development. However, as pillar recovery operations retreated under a
steadily increasing depth of overburden, conditions worsened. On March 7, 2007, a non-injury
coal outburst accident occurred that knocked miners down, damaged a ventilation control, and
caused a delay in mining. These worsening conditions culminated in a March 10, 2007, outburst
accident of sufficient magnitude to cause the mining section to be abandoned.
Between March and July 2007, four entries were developed in the barrier south of Main West.
Once again, the section was developed without incident but conditions worsened during pillar
recovery. On August 3, 2007, another non-injury coal outburst accident occurred as the night shift
crew was mining. Coal was thrown into the entries dislodging timbers and burying the continuous
mining machine cable. The continuous mining machine operator was struck by coal.
GRI did not notify MSHA of these three coal outburst accidents within 15 minutes as required by
30 CFR 50.10. GRI’s failure denied MSHA the opportunity to investigate these accidents and
ensure that corrective actions were taken before mining resumed in the affected area. GRI did not
3
submit written reports of these accidents to MSHA or plot coal bursts on a mine map available for
inspection by MSHA and miners as required.
These reporting failures were particularly critical because they deprived MSHA of the information
it needed to properly assess and approve GRI’s mining plans. Under Federal regulations, a mine
operator is required to develop and submit to MSHA a “roof control plan” suitable to the
prevailing geological conditions and the mining system to be used at the mine. MSHA has an
opportunity to review and approve or disapprove the plan. MSHA had specifically separated the
operator’s proposed mining plans into four separate plans, addressing different stages of the
mining process, and had asked the mine operator to communicate any problems encountered so
that MSHA could evaluate the safety of the plans as mining progressed. MSHA was only to
approve the “retreat mining” phases of the project if favorable conditions were observed during
development of the sections. However, the operator failed to make MSHA aware of the extent of
the violent conditions encountered during mining and did not make MSHA aware of the severity
of the March 10 coal outburst. MSHA approved the operator’s plans to conduct retreat mining in
the South Barrier, where the fatal accident ultimately occurred, without the benefit of this critical
information.
Additionally, GRI continued pillar recovery without adequately revising their mining methods
when conditions and accident history indicated that their roof control plan was not suitable for
controlling coal bursts. GRI investigations of non-injury coal burst accidents did not result in
adequate changes of pillar recovery methods to prevent similar occurrences before continued
mining. GRI did not consult with AAI or propose revisions to their roof control plan following
the August 3, 2007, coal outburst accident in the South Barrier section, even though pillar
conditions were similar to the failed area in the North Barrier section.
Explanation of the August 16 Accident
The August 16 accident occurred because rescue of the entrapped miners required removal of
compacted coal debris from an entry affected by the August 6 accident. Entry clean-up reduced
confining pressure on the failed pillars and increased the potential for additional bursts. Methods
for installing ground control systems required rescue workers to travel near areas with high burst
potential. Methods were not available to determine the maximum coal burst intensity that the
ground support system would be subjected to. On August 16, the coal burst intensity exceeded the
capacity of the support system. No alternatives to these methods were available to rescue the
entrapped miners. As a result, only suspension of underground rescue efforts could have
prevented this accident.
Prior to the August 16 accident, underground rescue efforts were only likely to have been
suspended had definitive information been available to indicate that the entrapped miners could
not have survived the accident. Information was not sufficient to fully evaluate conditions on the
section prior to this accident. Sufficient resources, including drilling resources, should have been
deployed. The rescue attempt imposed greater risks on rescue workers than would be accepted for
normal mining. However, the prospect of saving the entrapped miners’ lives warranted the heroic
efforts of the rescue workers. The greater risks imposed on the rescue workers underscore the
high degree of care that must be taken by mine operators to prevent catastrophic pillar failures.
4
GENERAL INFORMATION
The Crandall Canyon Mine, located near Huntington in Emery County, Utah, was opened into
the Hiawatha bituminous coal seam through five drift openings. At the time of the accident, the
mine operated with one working section (South Barrier section) and one spare section (3rd North
section). The miners, including 63 underground and 4 surface employees, were not represented
by a labor organization. Coal was loaded from a continuous mining machine onto shuttle cars
and transported to the section loading point, where it was dumped onto a belt and conveyed to
the surface. Personnel and materials were transported via diesel-powered, rubber-tired, mobile
equipment. An atmospheric monitoring system (AMS) was used for fire detection and
monitoring other mine systems, including: electrical power, conveyor belt status, tonnage mined,
air quality, and fan operation. An AMS operator was stationed on the surface to monitor and
respond to AMS signals and alarms. Two-way voice communication was provided by pager
phones installed throughout the underground mine and hardwired to various locations on the
surface. A Personal Emergency Device (PED) system was used at the mine to send one-way text
messages from the surface to selected miners who wore PED receiver units integrated with their
cap lamp battery. To comply with the post-accident tracking requirements of the MINER Act,
GRI established five zones from the portal to the South Barrier section for tracking the location
of underground personnel (see Appendix C). As miners passed from one zone to another, they
reported their location over the pager phone system to the AMS operator who tracked their
movements.
Coal was mined seven days per week during two 12-hour shifts. Day shift production crews
worked from 7:00 a.m. to 7:00 p.m. and night shift production crews worked from 6:00 p.m. to
6:00 a.m. Maintenance personnel worked 5:00 a.m. to 5:00 p.m. during day shift and 5:00 p.m.
to 5:00 a.m. during night shift. One set of day and night shift crews worked Monday through
Thursday and another set worked Friday through Monday. Everyone worked on Monday, which
was referred to as a “double-up day.” Preshift examinations were conducted on established
8-hour intervals beginning at 3:00 a.m., 11:00 a.m., and 7:00 p.m.
The coal resources within the Crandall Canyon Mine mining permit boundary are owned by
either the Federal Government or the State of Utah and are leased for mining to GRI. The U.S.
Department of the Interior through the Bureau of Land Management (BLM) manages the Federal
coal and the Utah School and Institutional Trust Lands Administration manages the State coal.
Mining plans for the Federal leases must be approved by BLM and must comply with a Resource
Recovery Protection Plan (R2P2) to ensure diligent extraction of all minable coal. The R2P2 is
approved by BLM, within the mining capabilities of the operator, to achieve maximum economic
recovery of the Federal coal. BLM inspectors monitor compliance with the approved R2P2
through underground inspections. Since the mine is entirely within the Manti-LaSal National
Forest, the R2P2 also addresses the impacts of mining on surface lands and water resources that
are managed by the United States Forest Service.
The reserve was first opened between 1939 and 1955, when a small area at the portal was mined
and then abandoned. Genwal Coal Company Inc rehabilitated the old mine workings and
resumed production in 1983 (see Appendix D). Room and pillar mining was utilized and
included pillar recovery (often referred to as retreat mining) from panels.
The mine was acquired by Nevada Power in 1989. In 1990, 50% interest was purchased by the
Intermountain Power Agency (IPA), a political subdivision of the State of Utah. In 1995,
Andalex Resources Inc (ARI), a Delaware corporation operating in Utah, acquired Nevada
5
Power’s 50% ownership of the Crandall Canyon Mine. The other 50% ownership was retained
by IPA. ARI operated the mine through its subsidiary Genwal Resources Inc (GRI). Also in
1995, GRI contracted Agapito Associates, Inc. (AAI), a mining consultant group based in Grand
Junction, Colorado, to conduct technical studies for longwall mining the remaining reserves.
Reports for these studies were finalized in November and December, 1995. The Main West
entries, inby crosscut 107, were mined in 1995 with the intention of developing north-south
oriented longwall panels from them. However, AAI’s fracture orientation report (Fracture
Orientation Study and Implications on Longwall Panel Orientation) recommended an east-west
orientation for longwall panels, so the longwall entries were not developed from the Main West.
AAI continued to provide consulting services to GRI, including a study to refine their ground
control model for the Crandall Canyon Mine in 1997. In June 1999, a longwall district north of
Main West was completed and sealed, leaving a 448-foot wide barrier north of Main West
(North Barrier).
A longwall district south of Main West was mined from 1999 to 2003. The Main West entries
were separated from these longwall panels by a 438-foot wide minimum dimension barrier
(South Barrier). During this period, the Main West entries provided a return air course for the
longwall bleeder system through a connection at the western end of these entries. This longwall
district was sealed in April 2003, and longwall production moved to the eastern portion of the
mine. The Main West was sealed inby crosscut 118 in November 2004 due, in part, to
deterioration of roof and coal pillars caused by abutment loads from the adjacent longwall
districts. GRI had planned to mine the Main West Barriers inby crosscut 118 by accessing them
through Main West. The need to seal the Main West prompted GRI to propose revised mining
projections to BLM. Also in 2003, GRI opened the adjacent South Crandall Canyon Mine and
the two operations shared surface facilities.
The last longwall panel at the Crandall Canyon Mine was completed in October 2005. Mining
was then limited to pillar recovery in the South Mains. Rooms were developed into barrier
pillars adjacent to the South Mains, just ahead of the northward retreating pillar line. With this
approach, barrier pillars outby the section loading point remained intact.
John T. Boyd Company, mining and geological consultants, conducted a coal reserve estimate
for ARI in December 2005 that identified recoverable reserves in the Main West as areas outby
the crosscut 118 seals. The map of the reserve estimate illustrated that both barriers would be
recovered east of crosscut 118 by mining a series of 3-4 rooms north and south from the original
5-entry Main West, similar to the method used to recover the South Mains. In January 2006,
Rothschild Inc. prepared a “Confidential Information Memorandum” for ARI to assist potential
transaction parties. This document included a map entitled “Crandall Canyon Mine Recoverable
Reserves As Of January 1, 2006” that also showed no projected mining in the Main West
barriers west of crosscut 118.
Early in 2006, GRI devised a plan to develop and recover the Main West North and South
Barriers inby crosscut 118. In April 2006, GRI contacted AAI to evaluate ground control and
pillar stability associated with this plan. AAI provided a draft report to GRI (see Appendix F),
which concluded that GRI’s plan should be “a workable design and limit geotechnical risk to an
acceptable level.”
On August 9, 2006, UtahAmerican Energy Inc. (UEI), a Utah corporation, acquired ARI,
including its wholly owned subsidiary GRI. UEI was wholly owned by Murray Energy
Corporation, an Ohio corporation. Murray Energy Corporation’s stock was wholly owned by
6
Robert E. Murray. AAI continued to work for GRI, and provided further analyses confirming
the viability of GRI’s plan to recover the Main West barriers (see Appendix G). Coal production
ceased at the South Crandall Canyon Mine at the end of August.
During the last quarter of 2006, pillar recovery in the South Mains was completed and mining of
the North Barrier section was initiated. Four entries were developed through the Main West
North Barrier beneath overburden ranging from 1,500 to 2,240 feet. AAI visited the section on
December 1, 2006, and reported that “There was no indication of problematic pillar yielding or
roof problems that might indicate higher-than-predicted abutment loads” (see Appendix H).
Pillar recovery began in February 2007. The two southern pillars were extracted and the
northernmost pillar was left intact to establish a bleeder system.
On March 10, 2007, a non-injury coal outburst accident occurred on the North Barrier section
that severely damaged pillars and ventilation controls and caused GRI to abandon the section.
Mining equipment was moved to the South Barrier section while coal was produced on a spare
section in the 3rd North Mains. The North Barrier section was sealed on March 27, 2007, inby
crosscut 118, and GRI commissioned AAI to refine the pillar design for the South Barrier
section. In this area, AAI recommended that GRI develop larger pillar dimensions, slab the
barrier south of the No. 1 entry, and avoid skipping pillars during recovery under the deepest
overburden (see Appendix I).
Four entries were developed through the length of the Main West South Barrier with entry
centerlines spaced 80 feet apart and crosscut centerlines every 130 feet (80 x 130-foot centers)
beneath overburden ranging from 1,300 to 2,160 feet. A 55-foot wide barrier separated the
section from room notches mined off the No. 1 entry of the Main West, and a 121-foot wide
barrier separated it from the sealed longwall Panel 13 to the south. The average mining height
was approximately 8 feet. During development up to 5 feet of bottom coal was left in the
western portion of the section.
Pillar recovery of the South Barrier section began on July 15, 2007, and continued until the
August 6, 2007, accident. The approved roof control plan permitted mining up to 40 feet deep
cuts into the barrier pillar south of the No. 1 entry during pillar recovery, except in the area
between crosscuts 139 and 142 (see Appendix J). This area was to remain unmined to protect
the bleeder entry where the section had been narrowed to three entries. Additional production
was gained during pillar recovery by ramping down into the bottom coal during cuts from the
pillars. Safety precautions for this type of mining were not addressed in the approved roof
control plan.
Officials for parties controlling the mine operation at the time of the accidents included:
Robert E. Murray .............................President, Murray Energy Corporation
P. Bruce Hill............................... President and CEO of UEI, ARI, and GRI
Robert D. Moore ........................................Treasurer of UEI, ARI, and GRI
Michael O. McKown .................................Secretary of UEI, ARI, and GRI
Laine Adair ................................... General Manager of UEI, ARI, and GRI
James Poulson..................................Safety Manager of UEI, ARI, and GRI
Gary Peacock ...................................................Mine Superintendent of GRI
Bodee Allred .............................................................Safety Director of GRI
7
Table 1 shows recent Non-Fatal Days Lost (NFDL) accident incidence rates for the mine prior to
the fatal accidents, and the comparable national rates for mines of similar type and classification.
A fatal accident (powered haulage) occurred at the Crandall Canyon Mine in 1997.
Table 1 - Accident Incidence Rates
Calendar
NFDL Incidence Rate Total Incident Rate
Year
National/Crandall
National/Crandall
2005
5.16/2.46
7.34/4.92
2006
4.83/2.50
6.99/2.50
2007
4.60/3.47*
6.35/3.47*
*2007 values for Crandall Canyon Mine are for January-June.
MSHA completed its last quarterly regular health and safety inspection of Crandall Canyon Mine
on July 2, 2007. MSHA started a new inspection on July 5, 2007, which was ongoing at the time
of the accidents.
DESCRIPTION OF THE ACCIDENT
August 6 Accident Description
Night shift mechanics Jameson Ward and Tim Harper started their shifts at 5:00 p.m. on
August 5, 2007. Ward entered the mine at 5:10 p.m. and drove to the South Barrier section.
Harper gathered supplies from the warehouse before entering the mine to set up a new scoop
charging station at the junction of Main West and the 3rd North entries. When Ward arrived on
the section, he parked his pick-up truck in the No. 1 entry, near the section charging station, and
walked to the continuous mining machine in the No. 1 entry to see if they were having any
maintenance problems. The day shift production crew was mining the barrier pillar between
crosscuts 140 and 141. After 20 minutes, Ward returned to the section charging station and
started repairing a scoop.
The night shift production crew entered the mine at 6:00 p.m. and traveled to the South Barrier
section. Crew members included: Benny Allred (section foreman), Kerry Allred (shuttle car
operator), Brandon Phillips (utility man), Jose Luis Hernandez (shuttle car operator), Manuel
Sanchez (continuous mining machine operator), Don Erickson (shuttle car operator/step-up
foreman), and Juan Carlos Payan (mobile roof support operator). They arrived on the section at
6:25 p.m. and relieved the day shift crew, which had mined a total of four cuts from the barrier
pillar. Larry Powell (maintenance foreman) also arrived on the section at this time and helped
Ward repair the scoop at the section charging station. Mining resumed in the barrier pillar after
shift change.
At 7:44 p.m., a magnitude 2.2 seismic event originated near the section. Erickson was
conducting the preshift examination near the charging station when he and Powell heard a noise
that sounded like a large cave inby the pillar line. Erickson went to the face to investigate. He
did not report any hazards during the preshift examination.
Gale Anderson (shift foreman), Benny Allred, and Powell were scheduled to attend training the
next morning and planned to leave work early. Anderson traveled to the section and met with
Erickson about his duties as responsible person and section foreman in their absence. They
reviewed mining plans and work assignments. Mining in the barrier pillar was approaching
8
crosscut 139. At this point, breaker posts would need to be set and the conveyor belt and power
center would need to be moved outby before pillar recovery between the Nos. 1 and 3 entries
could resume. Shortly after 9:00 p.m., Benny Allred gave his notebook and PED light to
Erickson. Erickson gave his preshift report to Benny Allred to record in the examination book.
Benny Allred asked Ward to help Erickson that night, if needed. Anderson, Benny Allred, and
Powell left the section. Before leaving the mine, Anderson and Benny Allred met with outby
mine examiners Brent Hardee, Tim Curtis, and Brian Pritt. Anderson provided them with a list
of tasks and Benny Allred asked them to retrieve his Self-Contained Self-Rescuer (SCSR) from
the section.
At approximately 11:30 p.m., Ward finished repairing the scoop and started helping Phillips
move the first aid trailer and rock dusting machine outby. Curtis drove to the section and
retrieved Benny Allred’s SCSR before helping Hardee and Pritt clean out an area for storing
conveyor belt structure at Main West crosscut 18. At 11:43 p.m., Richard Maxwell (material
man) arrived at the mine and started making repairs to his diesel-powered supply tractor.
Maxwell drove the tractor into the mine at 1:33 a.m., August 6, 2007, to check supplies on the
section.
By 2:00 a.m., Ward and other section crew members had started setting breaker posts inby
crosscut 139. Harper had finished work on the 3rd North charging station, but his truck would
not start and he called Ward for assistance. Ward checked with Erickson to see if he could leave
the section to help Harper. Erickson agreed, but told Ward that he needed to finish setting the
breaker posts before leaving.
Hardee, Curtis, and Pritt completed cleaning the area at Main West crosscut 18 and drove their
pick-up trucks outside, exiting the mine at 2:09 a.m. While on the surface, they unloaded
material gathered from the work site. Pritt and Curtis reentered the Crandall Canyon Mine in a
pick-up truck at 2:21 a.m., as Hardee prepared to conduct preshift examinations in the South
Crandall Canyon Mine.
At approximately 2:30 a.m., Maxwell arrived at crosscut 133 of the South Barrier section and
checked section supplies. No supplies were needed. He turned his tractor around and started
driving back outby. At 2:36 a.m., Hardee entered the South Crandall Canyon Mine to conduct
examinations. By 2:45 a.m., Ward had finished setting breaker posts. He called Harper to tell
him he was on his way and left the section.
At 2:48 a.m., as the section crew continued mining the barrier pillar near crosscut 139, a
catastrophic coal outburst accident initiated near the pillar line in the South Barrier section and,
within seconds, pillar failures propagated outby to approximately crosscut 119. Coal was
violently expelled into the entries where Kerry Allred, Don Erickson, Jose Luis Hernandez,
Juan Carlos Payan, Brandon Phillips, and Manuel Sanchez were working. All approaches to the
section were blocked, entrapping the six miners. The barrier pillars to the north and south of the
South Barrier section also failed, inundating the entrapped miners’ work area with lethally
oxygen-deficient air from the adjacent sealed area(s).
The resulting magnitude 3.9 mining-induced seismic event shook the mine office, located on the
surface three miles from the section, where it was felt by Leland Lobato and Mark Toomer,
atmospheric monitoring system (AMS) operators. AMS alarms reported communication failure
from sensors throughout the South Barrier section and the Nos. 6 and 7 conveyor belts stopped.
Air displaced by the ground failure rushed outby in a dust cloud that destroyed or damaged
9
stoppings from the accident site outby to crosscut 93 and the overcasts at crosscut 90 and 91.
The resulting short circuit to the ventilation system reduced fan pressure by 1 inch water gauge
(w.g.).
Ward had just exited the South Barrier section entries and was driving through Main West
crosscut 109 when he was struck by the air blast, causing his truck to slide sideways (refer to
Figure 2 for location of miners). Realizing that ventilation was disrupted, he got out of his
vehicle to assess the situation. After confirming that the nearest two stoppings were destroyed,
he drove to a phone at Main West crosscut 103.
Figure 2 - Location of Miners during August 6 Accident
Maxwell was driving outby from the section at Main West crosscut 91 when his supply tractor
was hit by the air blast. He was pelted in the open vehicle by dust and pieces of foam sealant
from the destroyed ventilation controls. He continued driving outby to crosscut 85. After the
dust cleared, he turned around and started driving inby.
Harper was waiting for Ward at Main West crosscut 35 when he heard a large rumble, which
roared past him, high up in the mine roof. A large gust of air followed, blowing two nearby
metal airlock doors open and closed. He was peppered with small rocks and his right eardrum
was injured. Thinking that the event was a large roof fall close to his location, Harper went to a
nearby phone and called Lobato, who was trying to contact the section. Lobato told Harper that
the section had lost power, Nos. 6 and 7 belts were down, the water gauge on the fan changed,
and the building he was in outside shook hard.
Pritt and Curtis were driving toward the mine entrance and did not feel the effects of the pillar
failure. Hardee also did not feel the event from his location in the South Crandall Canyon Mine.
When Ward reached the phone at crosscut 103, he called Harper and they discussed their
observations. Harper asked Ward to pick him up so they could travel to the section and find out
10
what had happened. As Ward continued driving outby, Harper called Lobato and told him to
contact Erickson and let him know that they were headed his way. Lobato sent a message to the
PED light Erickson had been given, instructing him to call the AMS operator. As Ward reached
crosscut 88, he passed Maxwell, who had stopped at a phone to call Lobato. Lobato told
Maxwell that he thought an earthquake had occurred. Maxwell told Lobato to start calling the
section. Lobato continued attempting to contact miners in the working section, without success.
Maxwell drove inby crosscut 93, where he saw damaged stoppings and turned around and started
driving outby.
Pritt and Curtis were unaware of the collapse when they exited the mine at 2:53 a.m. Pritt
dropped Curtis off to start examining the No. 1 conveyor belt. Pritt drove his pick-up truck back
into the mine to begin his preshift examination of the No. 2 conveyor belt. When he reached the
Main West entries, at 3:01 a.m., Pritt received a PED message instructing him to call the AMS
operator. He went to a nearby phone at Main West crosscut 4 and called Lobato, who briefed
him on the situation. Pritt told Lobato to send a PED message to Erickson and let them know
that he was on his way to the section. Pritt asked Lobato to contact Curtis and have him continue
walking the belts inby until Pritt found out what was going on. Pritt also spoke to Harper, just
before Ward arrived at crosscut 35. Ward picked up Harper and they sped toward the section, as
Pritt started driving inby from crosscut 4. Lobato sent PED messages to Curtis, Hardee, and
Erickson.
Ward and Harper encountered thick dust inby crosscut 96, where they saw destroyed stoppings.
At approximately 3:12 a.m., they stopped just inby crosscut 113 where a large piece of coal
blocked the roadway. Harper walked to a phone near crosscut 112 and called Lobato. Harper
instructed him to call Gary Peacock (mine superintendent) and tell him that there was a cave-in,
that all the stoppings were blown out inby crosscut 96, and that they were going to try to advance
into the section. Meanwhile, Pritt met Maxwell near crosscut 88. Maxwell parked his supply
tractor and got into Pritt's truck. They called Lobato and instructed him to notify Peacock that
something had happened. Lobato telephoned Peacock at his home. Pritt and Maxwell continued
driving toward the section as Ward and Harper explored inby crosscut 113.
Pritt and Maxwell arrived near crosscut 112, called Lobato, and confirmed that the phone
worked. Pritt tried to contact the section and received no response. Maxwell returned to his
supply tractor to gather materials for reestablishing ventilation.
While exploring inby crosscut 113, Ward and Harper heard loud, deep rumbling from continued
movement of the surrounding strata and observed sloughing of the ribs and mine roof. Debris in
the travelway and poor visibility hindered their travel. They returned to the phone where they
met Pritt. Pritt convinced Ward that they needed to wait for mine rescue apparatuses before
attempting to advance inby. Pritt called Toomer and asked him to bring in as many mine rescue
breathing apparatuses as he could find. During this call, the AMS operators relayed Pritt’s
information to Peacock by telephone. Pritt also told Peacock that they lost communications with
the section and that stoppings were down.
Hardee finished his preshift examination of the South Crandall Canyon Mine and drove to the
foremen’s room, located inside the Crandall Canyon Mine, at 3:22 a.m. As he prepared to record
his examination results, Hardee overheard Pritt requesting breathing apparatuses. Hardee joined
the conversation and volunteered to get the apparatuses. At 3:25 a.m., Hardee drove his pick-up
truck to the mine office building and ran upstairs to the AMS office, where Lobato was on the
phone with Peacock. Hardee briefly spoke with Peacock to tell him he was going into the mine.
11
Peacock told Hardee that an overcast at crosscut 91 was damaged, and he wanted him to check
that out before he went any farther inby. Curtis had completed the preshift examination of the
No. 1 conveyor belt and called the AMS operator in response to several PED messages. Hardee
answered, informed Curtis of the accident, and arranged to pick him up at Main West crosscut 4.
Hardee located four mine rescue apparatuses (Dräger BG174 A, 4-hour units) and two Dräger
30-minute fire-fighting units in the mine office building and loaded them into his pick-up truck,
along with materials to repair ventilation controls. He entered the mine at 3:36 a.m. and drove to
Main West crosscut 4, where he picked up Curtis, and then continued driving inby toward the
section.
Peacock started notifying other mine officials at 3:30 a.m. Peacock first called Bodee Allred and
told him to get the mine rescue team headed to the mine and to contact MSHA, in that order. At
3:37 a.m., Allred called Jeff Palmer and Hubert Wilson (mine rescue team members) and told
them to start calling other team members. Allred called the MSHA toll-free number for
immediately reportable accidents at 3:43 a.m. He reported that there was a bounce, they had an
unintentional cave while pillaring in the mine, and they lost ventilation. Allred also indicated
that they could not see past crosscut 92 and they did not know if stoppings were knocked out. At
3:51 a.m., the MSHA toll-free phone operator notified William Denning (MSHA District 9 staff
assistant) in Denver, Colorado, who initiated MSHA’s response.
The seismic event associated with the accident was detected by the University of Utah
Seismograph Stations (UUSS) network. Several minutes later Dr. Walter Arabasz (Director of
UUSS) was paged by an automated system. The page indicated that a local magnitude 4.0 event
had been detected. Protocol for events larger than 3.5 magnitude required some personnel to go
to the network operations center and issue a press release. A check of the automated posting on
the UUSS website indicated that the event was in central Utah. Dr. James Pechmann (University
of Utah seismologist) was also paged by the system. Working from his home computer, Dr.
Pechmann quickly reviewed the data. He then proceeded to the network operations center.
At the network operations center, Dr. Arabasz met Dr. Pechmann and Relu Burlacu (seismic
network manager). Notifications were made to parties on a prescribed list. UUSS decided to
notify the Carbon and Emery County Sheriffs’ Offices because it was believed they might
receive calls from the public. Dr. Arabasz told the Sheriffs’ Offices that, from the general
character of the seismic event, it might be a mining-related event. Neither Sheriff’s Office had
received any reports or information on the event. The notification phone call was made to the
Emery County Sheriff’s Office at 3:47 a.m. Five minutes later, Toomer called the Emery County
Sheriff's Office and reported, “We had a big cave in up here, and we're probably going to need
an ambulance. We're not for sure, yet, because we haven't heard from anybody in the section.”
An ambulance and an Emery County Sheriff's Officer were then dispatched to the mine.
The Carbon County Sheriff’s Office called UUSS back at approximately 4:00 a.m. and reported
that there had been a collapse at the Crandall Canyon Mine. Dr. Arabasz called the Emery
County Sheriff’s Office back to inquire if the mine operator had publicly confirmed a collapse.
Based on this conversation, Dr. Arabasz determined that they had not. Operating under the
belief that it was more appropriate for the mine operator to release the details of the collapse,
between 4:10 and 4:20 a.m., UUSS called the Associated Press and relayed only the location,
magnitude, and time of the event.
12
Meanwhile, Pritt, Ward, and Harper waited near crosscut 113 for Hardee and Curtis to deliver
mine rescue apparatuses. Hardee and Curtis stopped at crosscut 91, where they confirmed that
the overcasts were damaged. They determined that a nearby regulator was intact, which would
limit the short-circuit of air caused by the damaged overcasts. As they continued driving inby,
light dust was still suspended in the air from crosscut 93 to 109. Inby crosscut 109, dust limited
visibility to one crosscut. Shortly before 4:00 a.m., Hardee and Curtis met Pritt, Ward, and
Harper and they started exploring the No. 1 entry together. Near crosscut 115, Curtis detected
between 19.0 and 19.5% oxygen. All five miners retreated to their vehicles to obtain breathing
apparatuses to cope with the dusty atmosphere. However, the four, 4-hour mine rescue
apparatuses brought in by Hardee were outdated and unusable. Only the two 30-minute, firefighting units were ready for use.
Since Curtis and Pritt were trained members of the fire brigade, they wore the 30-minute firefighting units while resuming exploration in the No. 1 entry. Harper and Ward donned their
SCSRs and followed Curtis and Pritt. Hardee did not don any type of unit. He trailed behind the
group and eventually turned back to reestablish ventilation. As the group advanced, they
encountered increased depths of coal and destroyed stoppings covered with debris. After
advancing a few crosscuts, the roof started working and they retreated to crosscut 113. A few
minutes later, they resumed exploration in the No. 1 entry and advanced to approximately
crosscut 123. After encountering oxygen levels of 16% and adverse roof conditions, they
returned to crosscut 113 and developed a plan to explore the No. 3 entry.
Pritt, Ward, Curtis, and Harper then traveled in the No. 2 entry, before crossing the belt into the
No. 3 entry. They soon encountered very unstable ground conditions and retreated outby. As
they crossed back over the belt, Pritt tried to communicate with the entrapped miners by beating
on the waterline, but there was no response. When they returned to the phone near crosscut 112,
they called and briefed Peacock, who had arrived at the mine.
Pritt and Harper remained at the phone while Curtis, Hardee, and Ward traveled outby to
reestablish ventilation. Curtis and Hardee assessed damage as they walked the belt entry toward
each other from crosscuts 93 and 103, respectively, while Ward drove outside to obtain
ventilation materials. Maxwell was already on the surface, loading his supply tractor with
ventilation materials.
By 4:20 a.m., other mine officials and emergency vehicles, including an ambulance and an
Emery County Sheriff's Officer, began arriving at the mine. Denning informed William Taylor
(MSHA supervisory coal mine inspector) of the accident. Taylor called Barry Grosely (MSHA
Coal mine inspector) and assigned him to travel to the mine, issue a 103(k) order, and call Taylor
at the MSHA Price Field Office with an update. Taylor traveled to the field office and gathered
equipment needed to respond to the accident.
At 4:30 a.m., Curtis and Hardee completed their assessment of ventilation controls in the belt
entry and traveled to the phone near the No. 5 conveyor belt drive to report their findings. All of
the metal stoppings and some of the block stoppings inby crosscut 93 were damaged or
destroyed. Hardee stopped the No. 5 conveyor belt and requested that the remaining conveyor
belts be shut off from the surface. Hardee and Curtis started working outby, beginning repairs
while awaiting additional supplies from the surface. Ward exited the mine at 4:36 a.m. and
loaded his truck with polyurethane foam spray packs. Six minutes later, Maxwell reentered the
mine with his supply tractor loaded with ventilation materials, followed by Ward.
13
At 4:41 a.m., Grosely called the mine and issued an order pursuant to section 103(k) of the Mine
Act that prohibited all activity in the section until MSHA determined that it was safe to resume
normal mining operations in the affected area. The order also required the mine operator to
obtain prior approval from an authorized representative for all plans to recover or restore
operations to the affected area. Five minutes later, a magnitude 2.1 seismic event occurred near
the South Barrier section, followed by two smaller events within the next two minutes.
Underground Rescue Efforts
Underground rescue efforts were initiated on the morning of August 6. These efforts included
exploring approaches to the South Barrier section, restoring ventilation, cleaning up the rubble in
approaches to the South Barrier section, and breaching the No. 1 seal in Main West. Grosely, the
first MSHA employee on site, arrived at 5:44 am. Thereafter, MSHA evaluated the mine
operator’s specific rescue plans and approved them under the 103(k) order. GRI’s command
center was established on the second floor of the warehouse building as required in their
Emergency Response Plan. The MSHA Mine Emergency Operations (MEO) mobile command
center vehicle arrived from Price, Utah, at 10:15 a.m. It was parked near the entrance to the
mine portal access road, adjacent to GRI’s command center. MSHA and GRI jointly coordinated
the rescue efforts from these locations. Efforts also were made to locate the entrapped miners
with seismic equipment and by drilling boreholes.
Allyn Davis (MSHA District 9 manager) arrived on the afternoon of August 6 and assumed
control of MSHA’s onsite responsibilities. Richard Stickler (Assistant Secretary of Labor) and
Kevin Stricklin (Administrator for Coal Mine Safety and Health) arrived during the afternoon of
August 7. Three MSHA Technical Support roof control specialists worked onsite during the
rescue and advised MSHA decision-makers on roof control issues. They consulted with other
Technical Support employees and outside experts. Details of the rescue efforts are explained in
the following sections of this report.
Attempts to Explore South Barrier Section and Main West Sealed Area
The operator developed a plan to remove debris from the South Barrier No. 4 entry and to use
mine rescue teams to search for an access route to the entrapped miners. Under this plan, mine
rescue teams would explore all approaches to the South Barrier section. If no route to the section
could be found, the operator intended to breach the Main West No. 1 seal. Mine rescue teams
would explore for a route through the Main West entries to a point adjacent to the entrapped
miners, where they could drill or mine through the remaining barrier pillar into the working
section. The operator presented this plan to MSHA and, at 6:00 a.m. on August 6, Grosely
modified the 103(k) order to “permit the necessary personnel to travel underground to make
repairs to damaged ventilation devices, work on installing a belt tailpiece and feeder breaker at
crosscut 120 in the number two entry, clean and advance in the No. 4 entry towards crosscut 124
and to open the number one seal in the Old Main West entries inby crosscut 118 and use mine
rescue teams to explore within established mine rescue procedures. Ventilation will be
established as necessary for the operation of necessary mining equipment. Additional equipment
and materials will be moved underground as deemed necessary for current recovery
operations.”
At 6:40 a.m., fourteen members of the UEI mine rescue teams entered the mine to explore
approaches to the section (see Figure 3). Eighteen other miners remained in the mine to repair
ventilation controls, set up the feeder/breaker, belt tailpiece, and begin the clean-up work. All
other miners were evacuated from the mine. At 7:40 a.m., Taylor debriefed Harper, Ward, and
14
Pritt. Ward told Taylor that the crew was mining off the No. 1 entry at crosscut 139 into the
barrier before he left the section.
After 8:00 a.m., mine rescue team members from Energy West Mining Company also entered
the mine. Grosely, Randy Gunderson (MSHA coal mine inspector), and a group of miners,
including mine rescue team members, explored approaches to the South Barrier section by
traveling back and forth between the Nos. 1 and 4 entries in an attempt to find a route to the
entrapped miners. Entries and crosscuts were largely filled with debris, while intersections were
less filled. They advanced to crosscut 126 where they encountered debris within inches of the
roof and oxygen below 16%. A decision was made to retreat.
Figure 3 - South Barrier Section Rescue Area
Showing Ground Conditions and Rescue Attempts.
Rescuers attempted to provide breathable air to the entrapped miners by utilizing the fresh water
pipeline along the conveyor belt. The water was shut off and the pipeline was drained as much
as possible by opening fire valves. A PED message stating “OPEN VALVE ON H2O 4 AIR”
was sent to the cap lamp Erickson was wearing. Erickson was the only entrapped crew member
wearing a PED device. A compressor was set up between crosscuts 109 and 110 in the No. 2
entry. The compressor was attached to the water line and started. A second PED message
stating “PUMPING AIR THRU WATERLINE” was sent at 11:04 a.m.
By noon, the mine rescue teams had established a fresh air base (FAB) one crosscut outby the
No. 1 seal and began the arduous work of breaching the seal. At 1:55 p.m., the teams reported
to the command center that a 3 x 3-foot area of material, 8 inches deep into the seal, had been
removed. By 2:50 p.m., a small opening through the seal had been made and by 3:20 p.m., a
2 x 2-foot hole was completed through the seal.
Brad Allen (MSHA coal mine inspector/Mine Emergency Unit (MEU) member) and five mine
rescue team members entered the sealed area and began exploration at 4:42 p.m. The
15
irrespirable atmosphere behind the seal contained 6.0% to 6.8% oxygen, 62 parts-per-million
(ppm) carbon monoxide, and no methane. The team advanced in the Nos. 1, 2, and 3 entries to
near crosscut 121 where they encountered impassable roof falls. They attempted to advance into
the No. 4 entry but the roof had deteriorated and it was unsafe to travel. During the exploration,
the ground was working and bounces were occurring. Because of these unstable conditions and
the fact that travel routes were impassable in Nos. 1, 2, 3, and 4 entries, the team retreated to the
FAB.
After evaluating the information from the team’s exploration, the command center requested that
they attempt to advance into the No. 5 entry. At 5:02 p.m., as the team prepared to reenter the
sealed area, a fall or burst in the sealed area (registering as a magnitude 2.6 seismic event) forced
low oxygen through the breached seal and over the FAB. All personnel located in the FAB
quickly evacuated to a safe area outby. The team returned to the seal and covered the opening
with curtain to limit air leakage. Due to the poor conditions encountered behind the seals, all
attempts to explore the sealed area were suspended and mine rescue team members were
withdrawn from the mine.
While the exploration was continuing, the UUSS issued the following press release at 3:40 p.m.
explaining that further analysis had revised the location and magnitude of the seismic event:
The preliminary location and magnitude of today's earthquake are consistent with the
shock being a type of earthquake that is induced by underground coal mining. The
general region of the earthquake's epicenter is an area that has experienced a high level
of mining-induced earthquake activity for many decades. The largest of past mininginduced earthquakes had magnitudes in the 3.5 to 4.2 range, which encompasses the size
of today's earthquake (3.9). On the basis of present evidence, however, the possibility
that today's shock was a natural earthquake cannot be ruled out. The broad region of
central Utah experiences normal tectonic earthquakes in addition to mining-induced
earthquakes. For example, in 1988 a magnitude 5.2 earthquake occurred 40 km
southeast of today's earthquake.
Seismologists have not conclusively determined how the earthquake of August 6 might be
related to the occurrence of a collapse at the nearby Crandall Canyon coal mine that, as
of midday August 6, had left six miners unaccounted for. The epicenter of the seismic
event is close to the mine. We do not have an authoritative report of the time at which the
collapse occurred. If the collapse occurred nearly simultaneously with the earthquake,
we would consider it likely that the earthquake is the seismic signature of the collapse.
At this point, more information-- both from the mine and from more seismological
analyses--will be needed to piece together cause and effect relations for today's M3.9
earthquake.
Rescue Efforts in South Barrier Section Nos. 3 and 4 Entries
Soon after exploratory efforts indicated that entries were impassible, GRI developed a plan to
use mining equipment to reestablish a route to the missing miners. Fallen roof rock encountered
in the No. 1 entry precluded using that entry initially because a roof bolting machine was not
immediately available. The No. 2 entry contained section belt structure that would have
hindered the recovery process. At that time, conditions in Nos. 3 and 4 entries were most
conducive for the underground rescue effort. The recovery plan was implemented in No. 4 entry.
The South Barrier section loading equipment was inby the blocked entries. Therefore, two loadhaul-dump (LHD) diesel powered loaders were borrowed from a nearby mine to move the
16
material. Additional equipment was moved to the rescue site from other areas of the mine,
including an electrical power transformer, a radio remote controlled continuous mining machine,
and a feeder breaker.
The removal of material from the entries began during the afternoon of August 6, 2007. Initially
material was cleared for installation of a feeder breaker in No. 2 entry outby crosscut 120.
Rubble was also cleared from crosscut 120, between Nos. 1 and 4 entries. The two LHDs were
used to remove material in the No. 3 entry to crosscut 121, in crosscut 121 between the Nos. 3
and 4 entries, and in the No. 4 entry inby crosscut 121. The rubble was loaded and dumped
outby in accessible areas near crosscuts 116, 117, and 118. Entries were cleared by taking a
single LHD bucket width down the center of the entry. Coal was left along both rib lines.
Timbers were set for support in crosscut 120 between the Nos. 3 and 4 entries. The crosscut was
not traveled after timbers were set. The day shift crew was relieved at approximately 7:00 p.m.
and clean-up work continued into the night shift. The feeder breaker and belt were being
installed but were not operational as the diesel loaders were used to remove debris.
On August 7, 2007, a burst occurred in the clean-up area. UUSS registered a magnitude 2.8
seismic event at 1:13 a.m., which coincided with the approximate time of the burst. Ron Paletta
(MSHA coal mine inspector) was standing near the feeder breaker with Benny Allred and Gale
Anderson. The burst knocked Paletta to the ground and again damaged or destroyed ventilation
controls to crosscut 93. The burst put a large amount of dust into suspension throughout the area
and limited visibility to only a few feet. There were no injuries associated with this event.
However, the burst partially refilled approximately 300 feet of entry that had been cleared (see
Figure 4). Neither LHD was in the area refilled by burst material. One LHD was loading loose
coal near the feeder between the Nos. 2 and 3 entries and the other LHD was outby the feeder in
the No. 3 entry. All miners were withdrawn to crosscut 109 and accounted for.
Figure 4 - View of No. 3 Entry after August 7 Burst
Entry cleaned by diesel loaders refilled with rubble (view indicated by arrow in index map insert).
17
Rescue Efforts in South Barrier Section No. 1 Entry
Laine Adair, Gary Peacock, and Josh Fielder (section foreman) traveled underground to crosscut
120, evaluated the effects of the August 7 burst, and developed a new plan that was subsequently
approved by MSHA. The new plan relocated the rescue operation from the No. 4 entry to the
No. 1 entry (see Figure 3). The No. 1 entry was adjacent to the 121-foot wide barrier and
appeared to be in the best condition. In addition to the 18 miners already assigned to work in the
area, 12 miners were assigned to complete work outby crosscut 109 in preparation for advancing
in the No. 1 entry.
Before clean-up in the No. 1 entry was initiated, MSHA deployed a small portable seismic
detection system consisting of several sensors and a receiver/recorder. The portable system was
transported from its storage location in Pittsburgh, Pennsylvania, taken underground on
August 7, 2007, and deployed in the No. 1 entry at crosscut 121. This system was designed to
locate people over short distances, up to approximately 200 feet. The sensors were placed on
roof bolts and on the mine floor and monitored for 30 minutes. No signals from miners were
detected. The unit was then moved to the No. 2 entry at crosscut 120, where sensors were
attached to the section water supply pipe. After pounding on the pipe, the system was monitored
for 30 minutes. No response was detected. The portable system was not used again.
Preparation for Rescue Effort in No. 1 Entry
On August 8, 2007, the 103(k) order was modified to allow recovery operations to continue in
accordance with approved site specific plans. The initial site specific plan used for cleaning and
advancing in the No. 1 entry of the South Barrier section was also approved on August 8, 2007.
This was the base plan throughout the remaining rescue effort, with revisions or addendums
approved as needed. This approach eliminated the need to modify the 103(k) order each time
there was a change in work procedures or method of cleaning up, without compromising the
MSHA approval process. Once the plan was agreed upon by the company and MSHA, it was
ready for implementation.
In the initial plan, electrical power to the clean-up area was supplied through a power center
located in crosscut 119 between the No. 1 and No. 2 entries. The coal was to be loaded with a
continuous mining machine. Shuttle cars or scoops would transport the material to the feeder
located in the No. 2 entry between crosscuts 119 and 120 and the material would be carried out
of the mine by conveyor belts.
The plan stipulated that the ventilation system would utilize the No. 1 entry for intake with the
No. 2 entry being the belt haulage entry and the Nos. 3 and 4 entries would be utilized as the
return air course. Ventilation to the area would be established by constructing ventilation
controls at the following locations:
•
•
•
•
Between No. 1 and No. 2 entries at crosscuts 90-119.
Between No. 2 and No. 3 entries at crosscuts 90-119.
In No. 2 entry between crosscut 120 and 121 (belt entry isolation curtain).
Between No. 1 and No. 2 entries from crosscut 121 to 137 as recovery work advanced in
the No. 1 entry.
The clean-up work did not begin immediately in the No. 1 entry. All of the ventilation controls
that had been damaged or destroyed by the August 7 burst were rebuilt before loading was
started. Stopping repairs were completed on August 8, at 1:55 a.m. The continuous mining
machine was moved to the No. 1 entry inby crosscut 120 and the electrical power center was
18
relocated to crosscut 119 between the No. 1 and No. 2 entries. A fresh air base was established
at crosscut 119. A pager phone was connected between the clean-up area and the FAB. A
person was stationed at the FAB at all times to maintain communication with the clean-up area
and the command center on the surface.
The approved site specific plan also addressed the roof support system to be installed in the
clean-up area. As clean-up advanced in the No. 1 entry, additional roof and rib control measures
were implemented. The roof support portion of the plan required:
(A) As cleanup progresses roof support will be installed on 2.5' centers using rock props
[sic] or 8"x8" square sets on both sides of the entry. The square sets will be capped
with Jack Pots for active support.
(B) Screen mesh will be installed between the rib and the entry to confine rib roll and
protect employees and roadway.
(C) As each crosscut is completed 5/8" cable will be wrapped around these props to
secure them from pushing out.
Since 6 x 8-inch hard wood timbers were stronger and more immediately available than the
8 x 8-inch pine square sets specified in the plan, Item A was modified to include them at
1:05 p.m. on August 8, as follows:
(A) As cleanup progresses roof support will be installed on 2.5' centers using rock props
[sic] or 8"x8"pine square sets or, 6X8 hard wood with 8" dimension perpendicular to
the rib, on both sides of the entry. The square sets and the 6X8 hard wood will be
capped with Jack Pots for active support.
In addition to the items required for equipment setup, the initial plan listed several special
precautions:
(A) The continuous miner operator will be protected by a 4'x8' sheet of ½" thick Lexan
secured at top and bottom. Conveyer belting may be used in place of Lexan until
Lexan arrives.
(B) All unnecessary persons will be kept outby the fresh air base located at x-cut 119.
(C) Life Line will be maintained in the entry up to the continuous miner operator
location. Additional reflective tape will be added to life line.
(D) If mining conditions change significantly, mining will stop and the plan will be reevaluated before mining resumes.
(E) Additional SCSRs will be stored at the fresh air base at x-cut 119; so that every
person inby x-cut 115 will have access to two SCSRs.
The roof had deteriorated between the No. 1 and No. 2 entries at crosscut 120. This area
extended from the No. 1 entry to the location of the feeder breaker in No. 2 entry and required
additional roof bolting before the area could be safely traveled. Thus additional mining
equipment, including a twin boom roof-bolting machine, had to be moved into the area.
As specified in the plan, pressurized roof-to-floor standing supports were installed along pillar
ribs for protection from pillar bursts. On August 8, 6 x 8-inch hardwood wood posts were
installed on both sides of the No. 1 entry beginning at crosscut 118, narrowing the roadway to
14 feet. These posts were capped with Jackpots to actively preload each support between the
roof and floor (see Figure 5). The wood posts were installed in the No. 1 entry to midway
19
between crosscut 119 and 120 until RocProps (telescoping steel supports expanded with high
pressure water) were available. Thereafter, RocProps were used exclusively as roof-to-floor
support (see Figure 6). After the supports were installed, chain-link fence was installed between
the rib and the row of supports to confine dislodged coal and to protect miners and the roadway.
Additionally, 5/8-inch steel cables were wrapped around the RocProps to secure them from being
dislodged.
Figure 5 - Hardwood Posts Installed with Jackpots in No. 1 Entry
Figure 6 - RocProps, Cables, and Chain-link Fencing Installed in the No. 1 Entry
20
On the evening of August 8, the underground RocProp installation was completed to the
continuous mining machine located just inby crosscut 120 in the No. 1 entry. Just prior to
beginning the clean-up efforts, company officials accompanied by MSHA inspectors brought
news media personnel into the mine. The news media crew was in the clean-up area for a short
period of time filming the rescue efforts.
Material Clean-Up from the No. 1 Entry
Clean-up work began at approximately 6:00 p.m. on August 8, 2007, in the No. 1 entry and
advanced as rescue workers developed efficient means to remove coal, install standing support,
address damaged roof supports, and advance ventilation and cables. Initially, material was
hauled by electric shuttle cars. After clean-up in the No. 1 entry had advanced inby crosscut 122,
diesel Ramcars arrived from another mine and were used to transport material to the feeder.
On August 10, 2007, an addendum to the approved plan was implemented. The addendum
addressed three concerns:
•
•
•
No one, including equipment operators, was allowed inby the support (props or timbers).
If the continuous mining machine was not advancing, personnel may be allowed to work
inby the RocProps and timbers as long as the roof is supported to perform maintenance of
the equipment, limited support work, removal of debris from the rubble, etc.
The maximum clean-up distance was not to exceed the inby end of the shuttle car
operator’s cab. The shuttle car operators cab shall not extend beyond the last row of
RocProps and/or timbers.
The rock dust was to be applied in conjunction with the installation of roof support to the
furthermost extent of those supports.
Also, on August 10, MSHA approved a plan for two people, one from MSHA and one
representing UEI, to explore the No. 1 entry inby the continuous mining machine. At
12:43 p.m., Barry Grosely and Gary Peacock left the FAB and crawled over the rubble inby the
continuous mining machine at crosscut 123 in the No. 1 entry. Radios were provided for
communication with outby rescue workers during the exploration and the team carried multi-gas
detectors. Since neither carried a mine rescue-breathing apparatus during this excursion, they
were to retreat immediately if the oxygen content fell below 19.5% or the carbon monoxide level
elevated to 50 PPM. If bumping or bouncing occurred, they were to retreat to a supported area
immediately. The two-man team advanced to near crosscut 124 where they lost communication
and retreated outby. Another attempt was made in the No. 4 entry by Bodee Allred and Peter
Saint (MSHA coal mine inspector and MEU member). Saint was able to crawl to near crosscut
126 where the entry was impassable and they retreated. Air quality readings taken at the deepest
point of advance indicated 20.9% oxygen. These were the last attempts to explore in advance of
the clean-up operation.
As loading advanced inby crosscut 123, rescuers observed that part of the barrier south of the
No. 1 entry had moved northward as a result of the initial August 6 ground failure. The barrier
rib had shifted northward as a unit, as much as 10 feet. In some areas the displaced barrier slid
along the immediate roof and tore loose the original roof mesh (see Figure 7). In other areas, the
immediate roof was carried northward and damaged the original installed roof bolts (Figure 8).
21
Figure 7- Damaged Roof Bolts and Torn Mesh after August 6 Accident
Resulting from Northward Movement of Southern Barrier
Figure 8 - Damaged Roof Bolts in No. 1 Entry after August 6 Accident
Resulting from Northward Movement of Southern Barrier. Mesh shown was installed during
rescue operations, over damaged original roof bolts. Camera view is indicated by arrow in index map insert.
The procedures for advancing in the No. 1 entry were again modified on August 11, 2007. The
additional requirements were focused on limiting the exposure of the workers and strengthening
the support system. Under this revision, workers were not allowed in the clean-up area unless
they were designated by the foreman. The clean-up distance that could be advanced before the
support system had to be installed also was restricted. The advancement of the continuous
mining machine was limited to the distance it took to set three sets of RocProps. There was a
22
stipulation that this distance could be increased if conditions improved. However, both MSHA
and UEI had to agree on the increased distance prior to implementation. To limit the exposure of
workers inby supports, the RocProps were required to be set one at a time.
Another modification required three steel cables to be installed outside the RocProps instead of
the one cable previously required. The cables were to be installed at the top, middle, and bottom
of the supports. Each steel cable would wrap around a RocProp and be fastened to itself in
40-foot increments. Each cable was required to be connected to a separate RocProp and
terminated using three clamps.
Additional ventilation requirements were also stipulated in this modification. Permanent
ventilation controls were to replace the temporary controls inby crosscut 120. A handheld
detector was to be placed in the No. 3 entry on the return side of the door at crosscut 120 until an
atmospheric monitoring system oxygen sensor could be installed. Also, all shuttle car operators
were required to have an extra SCSR in the operator’s compartment at all times.
On August 11, 2007, Peacock reported that ground stress had migrated eastward and affected
pillars outby the Main West seals. MSHA examined the area and mapped these ground
conditions in the Main West entries and the North and South Barrier workings outby crosscut
119. Pillar damage was noted up to three crosscuts outby the seals, to near crosscut 115 (see
Figure 3). The damaged ribs were sloughed due to abutment stress from the area to the west. At
that time, it appeared that the ground stress had stabilized and was no longer progressing
eastward. Clean-up in the No. 1 entry had advanced near crosscut 124.
On August 12, roof deterioration was observed near crosscut 115 in the No. 1 entry. Steel
channels were installed for additional support in this area (see Figure 9). The channels were
supported on both ends with hardwood posts. At the time, clean-up in the No. 1 entry had
advanced just inby crosscut 124. The No. 1 entry was packed with rubble the full width and
height of the original mined opening. The continuous mining machine was loading from a
rubble pile that resembled an unmined coal face (see Figure 10 and Figure 11). Observations of
RocProps tilted from vertical prompted MSHA to install a measurement point to monitor
horizontal movement between crosscuts 123 and 124.
Figure 9 - Steel Channels Installed in No. 1 Entry to Support Deteriorated Roof
23
Figure 10 - No. 1 Entry Packed with Coal Rubble Inby Crosscut 124
Figure 11 - Continuous Mining Machine in Loading Area Inby Crosscut 124
24
A revised plan for loading loose material in No. 1 entry was approved on August 13, 2007. This
was the last addendum to the rescue and recovery plan, which stipulated the following:
1.
After miner loads ram car with loose material, the continuous miner operator will
back the miner to the location where rock props [sic] need to be set. The exact
location will be determined by the length of the hose needed to set the pressure on
the rock prop.
2.
Immediately after the ram car is 25 feet outby the location of the 6 men and heading
to the feeder, up to 6 men who are in the closest x-cut to the end of the prop line that
provides a minimum of 5 feet of clearance behind the rock props will begin setting
support.
3.
The support setters shall wear reflective vests so they can be easily seen by any
approaching individual. Reflective vests are on order.
4.
A miner will be stationed at least 100 feet, but not more than 200 feet outby the
support setters to be assigned to signal any approaching piece of equipment that the
support setters are in the entry. If the designated signal person sees the rock prop
setters in the entry, he will stop the approaching equipment at least 100 feet short of
the support setters.
5.
As the ram car approaches the continuous miner, the support setters will move back
into the x-cut.
6.
This process will apply for any work associated with rock props, any square sets,
j-bar, chain link fence, ventilation controls or wire rope or any support work.
7.
Ram cars loaded with rock props [sic] or any other roof support material will not
return to the outby area from the continuous miner without a load of coal.
8.
If a ram car is taking material to the continuous miner, the car should be loaded
while another car is at the miner. The car should be staged in number one entry just
out-by the x-cut 120.
Item 1 refers to the continuous mining machine being used as the hydraulic power source for the
water pump for installing the RocProps. However, a scoop or roof bolting machine also was
used as a power source for the RocProp water pump. Items 3, 4, and 5 were procedures to cope
with the close clearance between the mobile equipment and the installed RocProps.
At approximately 6:30 p.m. on August 13, MSHA mine rescue personnel using breathing
apparatuses installed 3/8-inch plastic tubing to the Main West seals. This allowed air samples to
be taken remotely in fresh air at crosscut 120 near the feeder. Clean-up in the No. 1 entry had
advanced to the vicinity of crosscut 125 at the time the air sample tubes were installed.
On August 14, a slight widening of roof joints was observed outby the FAB in the No. 1 entry
between crosscuts 115 and 117. RocProps were installed along the pillar ribs through this area to
reinforce the roof in the entry. Clean-up in the No. 1 entry had advanced to midway between
crosscuts 125 and 126.
On August 15 at 2:26 a.m., a burst initiated from the right pillar rib in the clean-up area of the
No. 1 entry inby the RocProps where the continuous mining machine was working. The burst
threw coal across the mining machine and registered as a 1.2 magnitude seismic event. The
machine was working 107 feet inby crosscut 125. It was reported as a significant event with
ventilation controls damaged at crosscut 125. No injuries occurred; however, the mining
25
machine cutter motors required repair work as a result of the burst. By 4:00 a.m. the mining
machine was repaired and clean-up work resumed in the No. 1 entry. Later that day, reports of
rock noise emanating from locations outby crosscut 119 prompted MSHA to install convergence
monitoring stations. Ten roof-to-floor convergence stations were installed at crosscuts 111, 113,
115, 117, and 119 in the No. 2 and No. 4 entries and sixteen monitoring locations were
established on RocProps inby crosscut 116 in the No. 1 entry.
August 16 Accident Description
On the morning of August 16, 2007, the No. 1 entry of the South Barrier section had been
cleared to just inby crosscut 126. At 6:25 a.m., Brandon Kimber (foreman), Dale Black
(foreman), Lester Day (continuous mining machine helper), Phil Gordon (Ramcar operator), and
Steve Wilson (Ramcar operator) were the first five miners on the day shift crew to arrive on the
section. They were joined by Casey Metcalf (support crew) at 6:51 a.m. and Randy Bouldin
(Ramcar operator), Carl Gressman (support crew), Mitch Horton (support crew), and Brandy
Fillingim (outby man) at 7:16 a.m. MSHA coal mine inspectors, Donald Durrant, Peter Saint,
and Rodney Adamson arrived on the section approximately 15 minutes later. Durrant monitored
activities in the clean-up area, Saint manned the FAB at crosscut 119, and Adamson monitored
air quantity and quality outby.
Two MSHA supervisory mining engineers, Joseph Cybulski and Joseph Zelanko, from the
Pittsburgh Safety and Health Technology Center’s Roof Control Division (RCD) accompanied
Durrant, Saint, and Adamson to the section that morning. The purpose of their visit was to
evaluate ground conditions in the work area and to measure the convergence stations they had
installed on August 15. Cybulski and Zelanko observed conditions between crosscuts 111 and
120 in the Nos. 2 and 4 entries and between crosscut 111 and the clean-up face in No. 1 entry.
None of the stations displayed any significant convergence and ground conditions had not
changed. They left the section and arrived outside at 10:10 a.m.
The day shift crew began the shift by installing roof supports in the clean-up area of the No. 1
entry. The roof bolting machine hydraulics powered the water pump that was used to pressurize
the RocProps. The continuous mining machine was trammed inby and the clean-up and support
cycle continued in the No. 1 entry.
The rescue efforts were interrupted at 10:04 a.m. when a burst occurred in the coal pillar between
the No. 1 and No. 2 entries. The burst, which registered as a magnitude 1.5 seismic event,
displaced approximately 4 feet of the pillar rib inby the RocProps, filling the entry on the right
side of the continuous mining machine to a depth of approximately 2.5 feet. No injuries were
sustained and no RocProps were dislodged by burst coal. The crew backed the continuous
mining machine outby, cleared the debris, and continued the clean-up cycle.
At 1:16 p.m., the crew was joined by Jeff Tripp, a supervisor from the Century Mine in Ohio,
operated by American Energy Corporation, a subsidiary of Murray Energy Corporation. This
was Tripp’s first day working at the Crandall Canyon Mine.
At 1:30 p.m., Cybulski and Zelanko returned to the section to take a second set of measurements
at the convergence stations. The measurements were being taken to establish the historical trend
and baseline for the convergence data. Again, measurements and observations were made in the
Nos. 1, 2, and 4 entries. No significant changes were noted.
26
At 2:58 p.m., MSHA coal mine inspectors, Gary Jensen, Frank Markosek, and Scott Johnson
arrived at the clean-up area to relieve Durrant, Saint, and Adamson for their 8-hour regular shift
rotation. Jensen and Johnson were members of MSHA’s MEU. Cybulski and Zelanko returned
to the surface with Durrant, Saint, and Adamson.
By the end of day shift, the crew had advanced the clean-up efforts in the No. 1 entry close to
crosscut 127. After the last Ramcar was loaded, Jensen informed the crew that they needed to
set RocProps. Jensen also recommended that steel channels be installed across the last two rows
of RocProps. As Wilson drove the loaded Ramcar to the feeder, crew members entered the
clean-up area to install supports. Gordon unloaded his Ramcar at the feeder, changed out with
Wilson, and parked in crosscut 125. Bouldin parked his Ramcar near crosscut 126 and walked to
the clean-up area to help install ground supports. Brandy Fillingim, who had been working
outby, came to the clean-up area at the end of the shift and assisted the crew. Fillingim, Bouldin,
and Horton installed RocProps and steel channels on the right side of the entry, while Black,
Day, and Kimber set them on the left side. Gressman was operating the control valve on the
pump used to pressurize the RocProps. Metcalf and Tripp were tightening the steel cables on the
left side. Jensen and Markosek were near the tail of the continuous mining machine, monitoring
the activities. Johnson was outby the clean-up area, taking air measurements at the Panel 13 seal
at crosscut 107.
At 6:38 p.m., as the crew completed installing ground support in the clean-up area, the coal pillar
between the No. 1 and No. 2 entries burst. Coal was thrown violently across the No. 1 entry
during the magnitude 1.9 seismic event. The burst created a void up to 20 feet deep into the
pillar at the roof line (see Figure 12 and Figure 13, view indicated by arrow). The dislodged coal
threw eight RocProps, steel cables, chain-link fence, and a steel channel toward the left side of
the entry, striking the rescue workers and filling the entry with approximately four feet of debris
(see Figure 14). Heavy dust filled the clean-up area, reduced visibility, and impaired breathing.
Oxygen deficient air from the inby area migrated over the miners. The dust and oxygen
deficiency were slow to clear due to damaged ventilation controls.
Figure 12 – Damage to Outby Portion of Pillar on Right Side of No. 1 Entry (Outby August 16 Accident Site)
27
Figure 13 - 20-foot Deep Void over Pillar on Right Side of No. 1 Entry following August 16 Accident
Figure 14 - August 16, 2007, Coal Burst Effects and Location of Injured Miners
Bouldin, Horton, and Fillingim had just walked out of the clean-up area when the burst occurred
behind them. Bouldin was knocked down by the thrown material and injured his back. He was
able to stand, but had difficulty seeing and breathing in the heavy dust. Fillingim and Horton
were not injured. Fillingim was near the edge of the dust cloud and continued out of the cleanup area, unaware of the severity of the accident. Bouldin and Horton were disoriented in the dust
and could hear injured miners shouting for help. Bouldin told Horton to go to the phone and get
help. Bouldin returned inby to assist the injured miners.
28
MSHA coal mine inspector Scott Johnson heard the burst from crosscut 110 while walking
toward the clean-up area. Protocol for the rescue efforts established that communication
between the clean-up crew and outby workers would occur following a bounce or burst. When
miners working near crosscut 113 informed Johnson that they had not heard from the clean-up
area, he hurried to the fresh air base phone at crosscut 119.
Gordon had just gotten out of his Ramcar and was standing near a pager phone in crosscut 125
when the burst occurred, knocking out the stopping next to him. He looked toward the clean-up
area and observed Fillingim walking out of a large cloud of dust. Wilson, located at the feeder,
felt a bounce and paged the crew. As Gordon answered Wilson’s page, Horton ran out of the
clean-up area and told Gordon that the crew was covered up. Wilson asked†, “Everything...Is
everybody all right in the face, Phil?” Gordon replied, “Hey, we need some help in here, now.”
“Okay, what do you need?” asked Wilson. Gordon answered, “Get some vehicles up here.”
Wilson replied, “Vehicles, right now.” Gordon continued, “Hey, get some help up here and get
some people.”
As Bouldin reentered the clean-up area, he could hear Day’s muffled voice calling for help.
Bouldin asked Day where he was. Day replied that Bouldin was standing on him. Bouldin
looked down and saw part of Day's shoulder exposed through the rubble and his head buried
beneath large pieces of coal. Bouldin uncovered Day and helped him to his feet before leaving
the clean-up area to catch his breath. Day attempted to help the other injured miners even though
he felt blood running down over his shoulders and realized that his head had been injured. Day
found Tripp buried in coal from the waist down and told him that he was going to get help. After
catching his breath, Bouldin resumed his attempts to dig out the injured miners who were
partially covered by debris from the burst.
Gordon told Fillingim to call outside and get help. He then entered the clean-up area to assess
the condition of the injured rescue workers. Fillingim and Horton called the AMS operator,
requesting “We need help in here now, in the face. We need everybody you can get in here
now…We need stretchers, we need bridles, we need everything...Hurry!” Gordon found Jensen
partially covered in coal, but responsive. Metcalf was conscious and lying against the left rib
entangled in chain-link fencing. Black was covered in material up to his waist. Markosek and
Gressman were severely injured, but alert. Kimber was located farther inby. Gordon checked
Black and Kimber for vital signs, but none were detected.
MSHA personnel stationed in the mobile command center vehicle were Bob Cornett (assistant
district manager), Danny Frey (MSHA supervisory coal mine inspector), and Dewayne Brown
(MSHA coal mine inspector trainee). Brown was manning the pager phone and maintaining the
command center log. Brown reported the call for help to Cornett, who assigned Frey and Brown
to remain in the vehicle to monitor communications and maintain the log. Cornett also assigned
C.W. Moore (MSHA mining engineer) to the Emergency Medical Services (EMS) staging area
to get the names and condition of everybody that they brought out, which he was to report to
Frey. Cornett then joined Adair in the command center.
†
Audio files of actual voice communications via the pager phone system were digitally recorded on August 16,
2007. Quoted conversations of pager phone communications were obtained from these recordings for this report.
29
The night shift crew members were traveling toward the clean-up area when the accident
occurred. Benny Allred, Chris Armstrong, Ronnie Gutierrez, Richard Hansen, Natalio Lema,
Ignazio Manzo, Dallen McFarlane, and Juan Zarate were walking toward the loading point when
they heard the burst and realized that airflow had been disrupted. Gale Anderson, Dave Blake,
Jeff Beckett, Keith Norris, and Jason Bell arrived at the fresh air base just behind Allred’s group.
Anderson told Benny Allred’s group to install curtains from the loading point at crosscut 120 to
the accident area. Anderson and the remaining night shift crew members continued inby to the
accident site and began helping the injured miners. Tim Harper, Ryan Mann, and Jameson Ward
were waiting by the phone at crosscut 89 when they overheard Fillingim’s call to the AMS
operator. Harper asked the AMS operator, “What's going on?” AMS replied, “I don't know, he
just told me we need everything in the face.” Harper told the AMS operator that they were at
crosscut 89 and they were going to the face.
Johnson arrived at the fresh air base and instructed miners to get the six stretchers stored there
ready. He also told the miners to load the stretchers into a truck and transport them to the cleanup area. Johnson then ran to the accident site.
Mine management had just finished a meeting to discuss progress and work plans for continued
rescue work in the No. 1 entry. Bodee Allred, Adair, Peacock, and several other managers exited
the meeting into the hallway near the AMS room. Allred overheard the AMS operator talking to
Harper. Allred picked up a phone in his office, which was located adjacent to the AMS room,
and called the fresh air base. Mike Elwood answered the phone at crosscut 123 and Bodee
Allred asked, “Hey, what's going on in there?” Elwood replied, “We had a bump. I don't know
exactly what went on...we called up to see how everybody was doing, they called for trucks...so
we're going, we are on our way up to the face, now, to see what's happening.” Allred asked if
they needed EMS. Elwood replied: “I would, just to be on the safe side. I don't know what we
got.” During this conversation, Bodee Allred motioned for Adair and informed him of the
accident. Adair immediately turned to Peacock and a few other managers and told them that
they had a big bounce and to get in the mine. Allred handed the phone to Adair and left the
office to go underground.
As Elwood briefed Adair, Bouldin was having difficulty breathing and went to the phone at
crosscut 125 to call for brattice. Bouldin interrupted, “Can anybody outby bring some rag?
Bring some brattice!” Adair announced, “They want brattice and rag, take it in there…get
moving, anybody outby in the mine, head toward the face.” Bouldin left the phone and returned
to the accident site where he was joined by night shift crew members, who began digging out the
injured miners and providing first aid treatment.
At 6:45 p.m., Adair attempted to resume contact with the accident site as Jeff Palmer and Bodee
Allred drove quickly up the portal road to enter the mine. They slowed down to speak to a
person at the portal before continuing into the mine, just as communication with the accident site
resumed. “You guys okay up there?” someone asked. “No, there's a bad accident, about eight
people…” The person at the portal called the AMS operator and reported, “I got Jeff and Bodee
heading into the face,” talking over the miner still speaking from accident site. The miner at the
accident site continued, “…we need lots of shovels, and pick, we need bridles…to hook on the
miner…we can't get them unburied.” “Okay, we'll bring all we got, bud.” “All right, try, hurry
fast.” Some of the information from the miner at the accident site was inaudible due to the
interruption for post accident tracking of personnel movements through the mine. Adair ordered
over the pager phone system, “This is Laine Adair. I want everybody off this line that's not
necessary.”
30
At 6:48 p.m., Adair paged the accident site. Gordon finished assessing the miners’ injuries and
answered the phone, “Hey this is Phil, we're on the face. Who have I got?” Adair replied, “This
is Laine, what do you need, buddy?” Palmer and Bodee Allred interrupted to report that they
were entering Zone 2 (see Appendix C). Gordon requested, “Everybody off the phone but
Laine.” Adair again ordered everybody off the phone. Gordon, speaking short of breath,
continued, “I think there's five or six…Dale Black and Brandon Kimber, is all that I can tell
right now, are fatalities…We got to have air, from the tail piece in, because we have no air up in
there, okay?” Gordon also requested first aid supplies and a medical team.
Johnson entered the clean-up area and detected 16% oxygen. Dust suspended in the air still
limited visibility to approximately 20 feet. He informed the workers recovering the injured
miners of the low oxygen but they did not want to leave the area. Johnson returned outby to
crosscut 125 and instructed miners arriving at the accident site to install brattice in the clean-up
area. Johnson paged the command center and reported, “They’re running short on air.” Adair
replied, “Start pushing that air in from the belt line. Check every crosscut. Start taking rag and
get that air pushed in.” Johnson returned to the clean-up area as Benny Allred and his crew
continued repairs to the ventilation system.
As Harper, Mann, and Ward traveled toward the accident site, they were stopped by Gutierrez.
Gutierrez informed them they needed brattice because the bounce had blown out stoppings.
They loaded the material Gutierrez had gathered into Harper’s truck and traveled inby. Harper
assisted in reestablishing ventilation while Mann and Ward continued inby. They met Day
walking out of the clean-up area. Mann had a first-aid trauma kit and bandaged Day’s head
wounds.
At 6:51 p.m., Peacock, Robert E. Murray, and Jerry Taylor (corporate safety director) entered the
mine, followed by several miners in a pick-up truck loaded with stretchers and supplies. Also,
an Emery County Sheriff’s Officer radioed his office and requested that Huntington EMTs be
paged out to respond to the mine. Four ambulances, in addition to the one already stationed at
the mine, were dispatched. Three emergency medical transport helicopters were also dispatched
to the mine. Ambulances were staged at the entrance to the portal access road, near the MSHA
mobile command center vehicle.
At 6:52 p.m., Elwood informed Adair that a temporary stopping had been built in crosscut 125,
and airflow to the clean-up area was re-established. Adair expressed a concern for low oxygen
coming into the rescue area. He told Elwood to get some detectors in the clean-up area and
monitor for low oxygen. Johnson also briefed the command center at 6:54 p.m.
Harper rejoined Mann and Ward. Harper helped Day get a ride outside while Mann and Ward
continued inby to assist other victims. As the miners were working to free the injured miners,
several factors were slowing their efforts. Not only were rescuers dealing with the quantity of
burst material, the roof and rib support that had been installed to protect the workers was now
part of the rubble. The electrical cable and water line used to operate the continuous mining
machine, along with the line curtain used for ventilation of the clean-up area, were also hindering
the recovery of the injured miners (refer to Figure 15).
31
Figure 15 – Clean-up Area Following the Fatal August 16, 2007, Accident
The direction and location of camera view is denoted by black arrow in the insert.
At 6:59 p.m., Bodee Allred arrived at the accident site, where he met rescuers carrying Brandon
Kimber to a pick-up truck. Allred helped place Kimber in the truck and started performing
cardiopulmonary resuscitation (CPR). Allred continued CPR until reaching the surface at
7:14 p.m. EMT personnel provided medical attention and continued CPR while in route to
Castleview Hospital in Price, Utah.
Day arrived at the surface at 7:18 p.m. and was taken to an ambulance where he was assisted by
Bodee Allred and attended to by EMT personnel. Markosek was brought out of the mine at
7:27 p.m. and placed in the ambulance with Day, which transported them to Castleview Hospital.
Markosek was later airlifted to Utah Valley Regional Medical Center in Provo, Utah. Tripp was
brought out of the mine at 7:33 p.m. and transported by ambulance to Castleview Hospital.
Gary Jensen was brought out of the mine at 7:40 p.m. and airlifted to Utah Valley Regional
Medical Center.
At 8:11 p.m., the last victim, Dale Black, was removed from the accident site. Metcalf and
Bouldin exited the mine at 8:13 p.m. and were transported by ambulance to Castleview Hospital.
Gressman arrived on the surface at 8:19 p.m. and was airlifted to University Hospital in Salt
Lake City, Utah. Black was brought out of the mine at 8:30 p.m.
At 9:17 p.m. the last group of the rescue workers exited the mine. Due to the large number of
people assisting in the rescue efforts, it took several minutes and a thorough head count to ensure
that everyone was out of the mine. To facilitate this effort, as workers exited the mine they were
directed to the shop area. Once everyone was in the shop area, MSHA and the mine operator
conducted a debriefing to verify who was in the mine at the time of the accident and to gather
specific information about the accident. At 9:55 p.m., mine management verified that everyone
32
was out of the mine. At 11:35 p.m., MSHA modified the 103(k) order and prohibited anyone
from traveling inby Main West crosscut 107.
The August 16, 2007, accident resulted in fatal injuries to rescue workers Dale Black and
Brandon Kimber and MSHA coal mine inspector Gary Jensen. Randy Bouldin, Lester Day, Carl
Gressman, Casey Metcalf, Jeff Tripp, and MSHA coal mine inspector Frank Markosek suffered
severe injuries.
Following the August 16 accident, a panel of independent ground control experts was convened
at the mine site to reevaluate the rescue effort. Although underground rescue efforts were
suspended until the conditions were reevaluated, efforts to locate the miners from the surface
continued.
Surface Rescue Efforts
Attempt to Locate Miners - Boreholes
Seven boreholes were drilled from the surface to the mine workings to locate the entrapped
miners and assess conditions in the affected area. Mine coordinates for each borehole were
determined from the mine map. These mine coordinates were then transferred and translated as
surface coordinates and located on the surface using global positioning satellite surveying. If
miners were located after a borehole intersected the mine, the hole could be used to communicate
and provide fresh air and sustenance until they were rescued. The first three boreholes were
drilled as the underground rescue efforts were ongoing. The next four boreholes were completed
after the accident on August 16, 2007.
The mine operator contracted the services of two companies to drill the boreholes into the mine.
A road, 1.7 miles in length, and a drill pad were constructed with bulldozers while the drill rigs
were being transported to the mine. These roads and drill pads were constructed in mountainous
terrain (see Figure 16). Surface locations for the boreholes were surveyed by a contractor for the
mine operator. The first borehole was started on August 7, 2007, at 7:30 p.m. and the last
borehole was completed at 4:30 a.m., August 30, 2007.
Figure 16 - Mountainous Terrain where Roads and Drill Pads were Constructed
33
Borehole No. 1 was drilled using a small rotary core drill fitted with a full hole, polycrystalline
diamond bit. This drill rig was transported by helicopter from another mine to the drill pad for
Borehole No. 1 at 4:30 p.m. on August 7, 2007 (see Figure 17). The diameter of Borehole No. 1
was approximately 3 inches for the first 450 feet and 2.4 inches from 450 feet to its full depth of
1,871 feet. This drill did not have any directional control capability.
Figure 17 - Heliportable Drill Rig
The other six boreholes (Nos. 2–7) were drilled with a larger drill rig that was driven to each drill
pad location (see Figure 18). This drill rig arrived at the site at approximately 3:00 a.m. on
August 8, 2007, and started drilling Borehole No. 2 at approximately 1:20 p.m. that day. The
first 20 feet of all six boreholes were drilled 14.75-inch in diameter with a hammer bit and cased
with 10.75-inch steel pipe. The remaining lengths of the boreholes were drilled 8.75-inch in
diameter with a tri-cone bit. Borehole No. 2 was cased from 20 feet down to the top of the coal
seam with 7.0-inch outside diameter by 6.375-inch inside diameter steel pipe. Boreholes
Nos. 3-7 were uncased beyond 20 feet in depth. The larger drill rig utilized directional control
and boreholes intersected the mine within a few feet of their intended locations. Figure 19
illustrates the locations of these boreholes relative to the mine workings. Figure 20 illustrates the
location of these boreholes on the surface. Table 2 summarizes the borehole parameters and
locations.
34
Figure 18 - Drill Rig at Borehole No. 4
Figure 19 - Borehole Locations Intersecting Underground Workings
35
Figure 20 - Surface Location of Boreholes
Table 2 - Summary of Borehole Size, Depth, Drill Rate, Location, Voids, and O2 Concentration
Borehole
No.
Dia.
(In)
Depth
to Mine
(Ft)
Drill
Time
(Hrs)
Drill
Rate
(Ft/Hr)
Mine
Intersection
Time/Date
9:58 pm
Aug 9
12:57 am
2*
8.75
1886
59.6
31.6
Aug 11
10:11 am
3*
8.75
1414
36.0
39.3
Aug 15
9:16 am
4*#
8.75
1587
41.5
38.2
Aug 18
8:30 am
5
8.75
2039
58.3
35.0
Aug 22
4:02 pm
6
8.75
1783
48.0
37.1
Aug 25
4:15 am
7
8.75
1865
48.3
38.6
Aug 30
* Air was injected into these boreholes with a compressor
# Robot was lowered into mine through this borehole
Note: Borehole Depth to Mine = Depth reported to BLM by GRI
1
2.4
1871
50.5
37.0
36
Mine
Intersection
Location
Crosscut 138,
Entry 2
Crosscut 137,
Entry 2
Crosscut 147,
Entry 4
Crosscut 142,
Entry 4
Crosscut 133,
Entry 1
Crosscut 138.5,
Entry 1
Crosscut 137.5,
Entry 3
Void
(Ft)
5.5
5.7
8.0
4.0
0.5
0.0
2.7
Initial O2
Date
8.17%
August 10
Borehole used
for air injection
16.88%
August 16
11.97%
August 18
Borehole
blocked
Borehole
blocked
Borehole
blocked
When a borehole intersected the mine opening, attempts were made to contact the entrapped
miners by striking the drill steel. MSHA and company personnel would listen for a response by
placing a microphone or a person’s ear against the drill steel. MSHA’s seismic location system
was also monitored. The drill steel was then lowered into the mine opening in two-foot
increments with pounding and listening taking place at each increment for about ten minutes.
This procedure would continue until the drill steel met solid resistance. There were no responses
to these activities at any of the boreholes.
The drill operators were able to determine when the boreholes intersected the mine opening by
observation of the hydraulic weight indicator gauge. The value on this gauge increased abruptly
when the mine opening was intersected. The mine void distance was determined for each
borehole by measuring the distance that the drill steel was lowered, after it intersected the mine
opening, until it met solid resistance.
Air quality was measured in Borehole No. 1 by drawing an air sample from the drill steel. The
air quality was determined in Borehole Nos. 2–7 when the holes were exhausting by collecting
air samples near the collar of the hole. The results of air sample analyses from the boreholes are
shown in Table 3.
A microphone and camera were lowered into the 8.75-inch boreholes. The camera was equipped
with lights and could be rotated 360 degrees. Once evaluations at Borehole No. 2 were
completed, a compressor was used to pump fresh air into the mine. The process was repeated at
Borehole Nos. 3 and 4.
Description of Boreholes
Borehole No. 1 was started at 7:30 p.m. on August 7, 2007, while preparations were underway to
begin the underground rescue in No. 1 entry. The underground rescue efforts had advanced to
just inby crosscut 122 in the No. 1 entry when this borehole intersected the mine at 9:58 p.m. on
August 9. The mine void was 5.5 feet high at this location. A camera was not lowered into this
borehole because of the small diameter. The initial air samples collected at this hole, at
12:00 a.m. on August 10, 2007, contained 20.73% oxygen. However, it was discovered that the
holes in the bit were clogged and that this initial sample did not represent the air quality in the
mine. After the bit was flushed with water, another air sample taken at 1:45 a.m. on August 10
contained 8.17% oxygen. Since the penetration location was not known at that time, it could not
be determined whether the low oxygen concentration was associated with the South Barrier
section or a sealed area of the mine. Therefore, a borehole survey was conducted on August 10.
The survey determined that the borehole had intersected the mine level at crosscut 138 in the
No. 2 entry 85 feet south of its intended location. The large deviation was due to the lack of
directional control with this rig and it was only by chance that the hole intersected the mine
opening.
The location for Borehole No. 2 was in the belt entry in the intersection outby the section feeder.
Drilling of this borehole started at 1:20 p.m. on August 8, 2007. The borehole intersected the
mine at crosscut 137 in the No. 2 entry at 12:57 a.m. on August 11, 2007. This was the projected
mine location for this borehole. The underground rescue efforts had advanced to between
crosscuts 123 and 124 in the No. 1 entry when this borehole intersected the mine. The mine void
was 5.7 feet at this location. A camera that was lowered into this borehole revealed that the
intersection was mostly open but the entries and crosscuts leading into the intersection were
almost completely filled with rubble. The belt was embedded in rubble inby and outby the
intersection.
37
Table 3 - Analysis Results of Air Samples Taken at Boreholes
38
On August 11, 2007, MSHA’s rescue capsule arrived on mine property from Beckley, West
Virginia. The 92-inch high by 21.5-inch diameter, one-man rescue capsule required a larger rig
to drill a minimum 30-inch diameter hole into the mine opening to provide clearance for the
capsule. The rescue capsule was available for use should signs of life be detected during rescue
efforts.
The location chosen for Borehole No. 3 was in the bleeder entry of the South Barrier section.
Drilling of this borehole started at 10:12 p.m. on August 13, 2007. The borehole intersected the
mine at crosscut 147 in the No. 4 entry at 10:11 a.m. on August 15, 2007. This was the projected
mine location for this borehole. The underground rescue efforts had advanced to 120 feet inby
crosscut 125 in the No. 1 entry when this borehole intersected the mine. The mine void was the
full entry height or approximately 8 feet at this location. After penetrating the mine, the drill
steel was struck three times with a hammer. A signal, repeating at 1 to 2 second intervals, was
detected by the MSHA seismic location system. These signals were received at only one subarray location (sub-array four). Dr. Jeffrey Kravitz (MSHA chief of scientific development),
reviewed the record and determined that the signals were too strong for that expected from an
entrapped miner. These signal recordings prompted the decision to move the proposed location
of Borehole No. 4 to a location near the sub-array where the signal was received to determine if
the entrapped miners might be in that vicinity.
Underground rescue efforts were suspended indefinitely after the accident on August 16, 2007.
Borehole No. 4 was being drilled at this time. Borehole No. 4 was completed and three more
boreholes were drilled in an effort to locate the entrapped miners after the underground rescue
efforts were suspended. The location for Borehole No. 4 was in the South Barrier section
bleeder entry, five crosscuts outby Borehole No. 3. Drilling of this borehole started at 3:45 p.m.
on August 16, 2007. Borehole No. 4 intersected the mine at crosscut 142 in the No. 4 entry at
9:16 a.m. on August 18, 2007. This was the projected mine location for this borehole. The mine
void was 4 feet at this location. After penetrating the mine, the drill steel was struck with a
hammer to signal the miners. No response was heard. A quiet time was established by shutting
down all surface operations. A series of explosive charges were set off to signal the miners.
First, three 100-pound charges were detonated at 12:16 p.m. At 12:53 p.m., three 50-pound
charges were detonated. No response was detected by MSHA’s seismic location system.
The location for Borehole No. 5 was in the primary escapeway entry of the South Barrier section.
Drilling of this borehole started at 10:15 p.m. on August 19, 2007. The borehole intersected the
mine at crosscut 133 in the No. 1 entry at 8:30 a.m. on August 22, 2007. This was the projected
mine location for this borehole. The mine void was 0.5 feet at this location. An attempt to lower
a camera into this borehole was aborted because the hole was blocked with mud at 511 feet from
the surface.
The location chosen for Borehole No. 6 was near the last known area where mining was taking
place in the South Barrier section. Drilling of this borehole started at 4:00 p.m. on August 23,
2007. The borehole intersected the mine halfway between crosscuts 138 and 139 in the No. 1
entry at 4:02 p.m. on August 25, 2007. This was the projected mine location for this borehole.
No mine void was encountered.
The location chosen for Borehole No. 7 was in the kitchen/transformer area of the South Barrier
section. This was near the area in which Borehole No. 1 was intended to intercept the mine.
Drilling of this borehole started at 4:00 a.m. on August 28, 2007. The borehole intersected the
mine level between crosscuts 137 and 138 in the No. 3 entry at 4:15 a.m. on August 30, 2007.
39
This was the projected mine location for this borehole. A 7-foot rubble depth and a 2.7-foot void
height were encountered. An immediate attempt to lower a camera into this borehole was
thwarted because water and mud had blocked the hole approximately 9 feet from the mine level.
A camera-equipped robot was quickly designed and assembled specifically for the Crandall
Canyon Mine drilling rescue efforts. The robot was lowered into Borehole No. 3 on August 27,
2007. The robot was lowered into the mine with a winch and tripod arrangement as shown on
Figure 21 and Figure 22. The robot was unable to enter the mine because the borehole had
partially closed.
Figure 21 - Arrangement for Lowering Robot into Mine Through a Borehole
Figure 22 - Robot Being Lowered Into Borehole
On August 30, 2007, the robot was lowered into Borehole No. 4 in the same manner as was
attempted with Borehole No. 3. However, it was only able to travel a short distance in the mine
due to the rubble. While retrieving the robot from Borehole No. 4, it became wedged in the
borehole and could not be retrieved.
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Attempt to Locate Miners - MSHA’s Seismic System
MSHA maintains a truck-mounted seismic location system at the Pittsburgh Safety and Health
Technology Center. The system is designed to detect and locate entrapped miners. The truckmounted system consists of a seismic truck, generator truck, and a supply trailer. The system is
unique compared to typical seismic monitoring equipment. The system is tuned specifically to
detect the frequencies generated by miners signaling by pounding on the roof.
Kravitz was notified of the accident at 5:58 a.m. MDT on August 6, 2007, and began to ready the
system. The system was airlifted from Pittsburgh, Pennsylvania, to Grand Junction, Colorado,
and arrived at approximately 4:00 a.m. on August 7, 2007. The two trucks were driven to the
mine and arrived at 10:30 a.m. that morning.
The seismic location system utilizes geophone sub-arrays which detect and transmit signals to
the seismic truck. Each array consists of several geophones, preamp and telemetry unit with
antenna. A line-of-sight path is required from the sub-array antennas to the truck for the
telemetry to function. Due to the steep terrain, the seismic location truck was set up to the west
of the mine in Joes Valley. This provided a clear line of communication to each sub-array.
While the truck was being positioned in Joes Valley, other members of the MEU set up the subarrays. The system became operational at approximately 10:30 p.m. on August 7, 2007.
The sub-arrays and drilling operations were both centered over the last known location of the
entrapped miners. After the first signals were analyzed, it was apparent that noise from the
drilling operations and drill pad preparations would preclude any chance of receiving signals
from underground while drilling. System sensitivity had to be decreased during drilling. The
sub-arrays were relocated several times to maximize the chance of receiving a signal. A quiet
period was established after each borehole intersected the mine. The system sensitivity was
maximized at these times and the system was carefully monitored.
Suspension of Rescue Efforts
After the August 16 accident, a group of independent ground control experts was assembled by
GRI and MSHA to reevaluate conditions and rescue methods. On August 19, 2007, the seven
member panel convened at the mine site. The panel members, listed below, included three
NIOSH employees and four consultants.
• Keith A. Heasley, Ph.D., P.E., Professor, West Virginia University
• Hamid Maleki, Ph.D., P.E., President/Principal, Maleki Technologies Inc.
• Christopher Mark, Ph.D., P.E., Mining Engineer, NIOSH Pittsburgh Research Laboratory
• Anthony T. Iannacchione, Ph.D., P.E., Mining Engineer, NIOSH Pittsburgh Research
Laboratory
• Reid W. Olsen, Business Manager, Bruno Engineering, P.C.
• Morgan Moon, Engineering Consultant, Morgan Moon Co.
• Peter Swanson, Ph.D., Research Geophysicist, NIOSH Spokane Research Laboratory
The panel was charged with two objectives: evaluate the overall stability of the mine and the
underlying and overlying strata in the Main West area, inby crosscut 107; and quantify the risks
and recommend potential ground control methods of gaining access to the last known location of
the miners. On August 20, 2007, the panel issued a written statement and presented it to
41
representatives of the mine operator and MSHA at the mine site. The panel stated “that the
overwhelming preponderance of data indicates that the entire Main West area remains in a state
that is structurally unstable. We are highly concerned that dangerous seismic activity and pillar
instability are likely to continue, and that it is not possible to accurately predict the timing or
location of these events. No matter how a miner might access the Main West area, seismic
activity and pillar instability will pose a significant risk. These risks would be further increased
by any excavation of coal in the Main West area.”
The evaluation confirmed what the mine operator and MSHA had surmised from the August 16
accident when underground rescue work was suspended. The panel reinforced the opinion that
even with a much stronger support system in place, the process of disturbing the rubble for
installation of the next set of supports would endanger those installing the support system. Based
on the panel’s evaluation it was decided that rescue efforts would be limited to borehole drilling.
If miners were located, entering the mine via rescue capsule would be pursued.
Drilling continued until August 30, at which time sufficient information had been obtained to
determine that the entrapped miners could not have survived the August 6 accident due to
extensive burst damage and low oxygen on the section. As a result of information obtained from
the boreholes, the unfavorable conditions encountered underground, and the findings of the
expert panel, the families were notified on August 31, 2007, at 5:00 p.m. that all rescue efforts
were being suspended. The bodies of Kerry Allred, Don Erickson, Jose Luis Hernandez,
Juan Carlos Payan, Brandon Phillips, and Manuel Sanchez remained entombed in the mine.
Mine Closure
The decision to suspend rescue efforts was followed by the mine operator’s announcement to
cease coal production at the mine. Activities at the mine changed from rescue efforts to the
recovery of mining equipment. On September 4, 2007, at 3:55 p.m., the 103(k) order was
modified to allow work inby crosscut 90, provided that all entries were continually monitored for
oxygen, carbon monoxide, and methane. Travel inby crosscut 107 was prohibited. The order
was modified on September 14, 2007, at 2:45 a.m. to prohibit work inby crosscut 50 of the Main
West. This modification also required all persons working underground to be provided with
multi-gas detectors capable of detecting oxygen, carbon monoxide, and methane.
On September 27, 2007, BLM received a plan from the mine operator requesting approval to
grout the boreholes drilled during the rescue attempt. BLM approved the plan the following day.
On October 1, 2007, the mine operator submitted a plan to MSHA detailing the grouting of the
boreholes on East Mountain and construction of concrete block walls in the mine openings to
prevent entrance by unauthorized persons. MSHA acknowledged the plan on October 18, 2007.
The borehole abandonment process began on October 12, 2007, and was completed on
October 15, 2007. The actual plugging of the boreholes varied from borehole to borehole.
Uncased boreholes were extensively blocked. Boreholes were filled from the point of blockage
to within 20 feet of the surface with abandonite, a bentonite based grout mixture. The top 20 feet
of all boreholes was filled with cement.
42
INVESTIGATION OF THE ACCIDENT
The MSHA Administrator of Coal Mine Safety and Health appointed a team to investigate the
accident at the mine, led by Richard A. Gates, District Manager of Coal District 11. The
remainder of the team consisted of personnel from MSHA Coal Districts 2, 3, 6, 11, and
Technical Support’s Pittsburgh Safety and Health Technology Center. The investigation was
conducted jointly with the State of Utah Labor Commission. Sherrie Hayashi, Labor
Commissioner served as the state representative. The team received assistance from MSHA
personnel in Headquarters, Educational Field Services, and Program Evaluation and Information
Resources. The team also received assistance from personnel at The University of Utah, West
Virginia University, United States Geological Survey, and Neva Ridge Technologies. The
investigation team was announced on August 30, 2007, and arrived at MSHA’s Price, Utah,
Field Office on September 5, 2007.
Representatives of the miners and GRI participated in the on site investigation. At the mine, the
investigative procedures included mapping specific underground areas of the mine including the
August 16, 2007, accident scene, and photographing the affected areas. Unstable ground
conditions inby crosscut 107 of Main West limited the underground investigation to two
underground visits focusing on the August 16 accident scene. However, the team was able to
take advantage of in-mine information obtained during the rescue efforts from August 6 through
August 16. Pertinent records and documents were obtained and reviewed during the course of
the investigation. Information and records were obtained from MSHA District 9 offices, GRI,
and AAI.
The investigation team identified people who had knowledge relevant to the accident and
conducted 80 interviews. These people included current and former employees of Genwal
Resources Inc, UtahAmerican Energy Inc. and other Murray Energy Corporation operations,
MSHA, Bureau of Land Management, University of Utah, Agapito Associates, Inc., and Energy
West Mining Company. The interviews were conducted at:
• Southeastern Utah Association of Local Governments Building, Price, Utah,
• Residence Inn, Salt Lake City, Utah,
• City Hall Building, Spring City, Utah,
• University of Utah, Salt Lake City, Utah,
• National Mine Health and Safety Academy, Beckley, WV,
• Agapito Associates, Inc., Grand Junction, Colorado,
• Hall & Evans LLC, Denver, Colorado,
• MSHA Approval and Certification Center, Triadelphia, WV.
The interviews with MSHA were voluntary. A number of witnesses declined to give interviews
to MSHA, including current and former employees of Murray Energy Corporation operations
and AAI.
In addition to this accident investigation and the independent review noted in the Preface, there
have been several other governmental investigations and hearings related to the Crandall Canyon
Mine accidents. These include those conducted by: the Utah Mine Safety Commission; the
Senate Appropriations Subcommittee on Labor, Health and Human Services, Education and
Related Agencies; the Senate Committee on Health, Education, Labor, and Pensions; the House
Committee on Education and Labor; and the Office of the Inspector General of the U.S.
Department of Labor.
43
DISCUSSION
The Crandall Canyon Mine accident investigation was somewhat unique among MSHA
investigations in that (1) it examined two separate but related fatal accidents and (2) it utilized a
variety of technical analyses. It was obvious at the most fundamental level that the accidents at
Crandall Canyon Mine were precipitated by pillar failures in the South Barrier section. One
could envision that the South Barrier was the last substantial block of coal supporting the
mountain and, as it was removed, the mountain was simply too heavy for the pillars. Similarly,
the August 16, 2007, accident could be attributed to the inability of the installed support system
to protect rescuers from an unanticipated pillar burst. However, MSHA’s investigation augments
these observations with detailed analyses intended to provide sufficient insight to prevent a
recurrence.
The following sections provide information pertaining to both accidents. Since these accidents
were associated with dynamic pillar failures, detailed technical analyses of ground behavior and
mine design are included. In some instances, the results of the analyses are important in
explaining what happened. In other instances, it is important to understand the methodologies
that were used. Sufficient technical detail has been included to describe the analyses and allow
industry practitioners to apply the findings of the investigation to prevent future incidents.
Additionally, each major section includes an introduction and summary which provide a general
understanding of the issues.
August 6 Accident Discussion
The August 6 accident occurred as a result of the rapid failure of a large number of pillars.
Although it was a single catastrophic event, the failure was the culmination of a series of
decisions, actions, events, and conditions that were made or occurred over a period of more than
12 years (i.e., from the time the Main West entries in the vicinity of the accident site were
developed).
Pillars developed in 1995 in Main West proved to be adequate for development but deteriorated
when adjacent longwall panels were mined. These pillars were protected from more extreme
longwall abutment loading by large barriers (~450 feet wide) and the system, though damaged,
remained stable. Mining through the barriers on both sides of Main West in 2007, however,
disrupted the balance.
Between late 2006 and February 2007, the 448-foot wide barrier north of Main West was
developed by driving four entries parallel to the existing Main West entries. Smaller barriers
remained on either side of the new section entries (53 feet wide on the south side and 135 feet
wide on the north side). The 135-foot wide barrier that separated the North Barrier section from
the adjacent longwall panel gob was insufficient to isolate the workings from substantial
abutment loading. Despite the high stress levels associated with deep cover (up to 2,240 feet of
overburden) and longwall abutment stress, the section remained stable during development.
However, as pillar recovery operations retreated under a steadily increasing depth of overburden,
conditions worsened and culminated in a March 10, 2007, outburst accident of sufficient
magnitude to cause the mining section to be abandoned.
Between March and July 2007, four entries were developed in the barrier south of Main West.
Pillar dimensions were increased in an effort to mitigate the type of outburst failure that had
occurred in the North Barrier section. The longer pillars were about 16% stronger but, at the
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same time, a narrower barrier pillar (121 feet versus 135 feet in the previous section) exposed the
section to higher abutment stress from the adjacent longwall gob. The net effect was that the
mining experience in the South Barrier section was quite similar to that in the north. Once again,
the section was developed without incident but conditions worsened during pillar recovery and
culminated in the catastrophic August 6, 2007, outburst accident.
The August 6 event affected a much broader area than the March 10 outburst accident in the
North Barrier section. The primary reason for this was that entry development in both Barrier
sections had segmented the original, ~450-feet wide Main West barriers into relatively small
pillars; these pillars formed a large area of similarly sized and marginally stable pillars. When
the North Barrier section was developed, the overall system (i.e., the North Barrier section, the
Main West, and the 53-foot barrier between the two) effectively created a nine-entry system of
similarly sized pillars. When the South Barrier section was developed, the system was expanded
to a 13-entry system albeit with slightly stronger section pillars. With this large area of similarly
sized and marginally stable pillars, once failure initiated at any point in the system, the system
was set to fail in domino fashion and on August 6 it did.
GRI relied upon several engineering analyses to validate that their mining plan was sound.
However, the results proved to be misleading in some cases because the analyses were wrong
and in others they were misinterpreted. Three separate methods of analysis employed as part of
MSHA’s investigation confirm that the mining plan was destined to fail. Results of the first
method, Analysis of Retreat Mining Pillar Stability (ARMPS), are well below NIOSH
recommendations. The second method, a finite element analysis of the mining plan, indicates a
decidedly unsafe, unstable situation in the making even without pillar recovery. Similarly, the
third method, boundary element analysis, demonstrated that the area was primed for a massive
pillar collapse (see Appendix K).
All three analysis methods show that the area was destined to fail. However, additional analyses
were required to understand how and why it failed. Boundary element models provided insight
to the strata mechanics associated with the failure. These results demonstrate that if material
properties and loading conditions are exactly uniform throughout the Main West area, then some
stimulus such as a gradual weakening of the coal over time or joint slip in the overburden may
have triggered the event. On the other hand, if the properties and loading conditions are not
uniform (a reasonable geologic assumption), the event may have been triggered by pillar
recovery in the active mining section. The boundary element modeling only identified possible
triggers, and by itself could not distinguish the most likely trigger. However, seismic analyses
and subsidence information employed in the investigation provide further clarification that the
collapse was most likely initiated by the mining activity.
Analyses of the seismic event associated with the August 6 collapse indicate that it originated
from a point near the last row of recovered pillars, just inby the last known location of the
entrapped miners. Soon after the collapse, an initial location of the event was calculated
automatically and posted on UUSS and USGS web sites. This calculation process provides
expedient information of value to seismologists but it and other routine location procedures lack
the precision required for this investigation. In the months following the accident, UUSS
employed a variety of advanced seismological methods to improve source location accuracy and
to determine other characteristics of the collapse. UUSS determined that the magnitude 3.9
event lasted only seconds, calculated that the mine opening decreased in height by approximately
one foot over an area of 50 acres, and noted that movement likely occurred along a north-south
oriented vertical plane on the west end of the collapse area. UUSS’s description of strata
45
displacements is very consistent with other observations and analyses conducted during the
investigation.
Satellite radar images were used to determine surface displacements over the Crandall Canyon
Mine. A comparison of images acquired shortly before and after the accident revealed the
development of a large surface depression over the accident site. Vertical movements greater
than ¾ inches were observed on the surface over an area approximately 1 mile (east-to-west) by
¾ miles (north-to-south). A maximum displacement of nearly 12 inches was observed over the
121-foot wide barrier pillar about 500 feet outby the last known location of the entrapped miners.
Borehole No. 5 penetrated the mine workings near the point of maximum displacement and
confirmed that the void space in an intersection was only 0.5 feet.
Traditional surface elevation surveys between 1999 and 2004 show that strata overlying about
half of the longwall panel south of the working section had not completely subsided and was
cantilevered from the Main West South Barrier. Both traditional and satellite surveys conducted
after the accident demonstrate that the surface over the panel and the barrier displaced downward
as much as 12 inches. Furthermore, the satellite analysis indicates that the strata movement that
occurred was much more abrupt at the southern and western edges of the depression (as
evidenced by the steeper subsidence contours). The abrupt displacement on the western side is
consistent with UUSS’s theory that some movement may have occurred on a steeply dipping
(near vertical), north-south oriented plane. The abrupt displacement on the southern edge is
consistent with substantial failure of the 121-foot wide barrier and an associated downward
movement of cantilevered strata over the adjacent longwall gob. The volume of cantilevered
strata likely provided the additional loading necessary to initiate the collapse event from the
working section.
Pillar recovery operations by their nature create a zone of high stress in adjacent workings. As
pillars are removed, the weight of overburden that they once supported must then be carried by
neighboring pillars. Abutment loads can be diminished if or when sufficient roof caving and
compaction occurs in the gob to allow the weight of overburden to be transmitted into the floor
where the pillars were removed; due to the limited dimensions of the South Barrier pillar
recovery area, however, it is unlikely that gob compaction had occurred there. Abutment loads
were present from the active retreat line and the adjacent longwall gob. Also, overburden depth
(and the associated stress level) was increasing as pillar recovery progressed outby. Ultimately,
it is most likely that the stress level exceeded the strength of a pillar or group of pillars near the
pillar line and that failure initiated a rapid and widespread collapse that propagated outby
through the large area of similarly sized pillars.
As pillars were recovered in the South Barrier section, bottom coal was mined from cuts made
into the production pillars and barrier. The effect of this activity was to reduce the strength of
the remnant barrier behind the retreating pillar line. Bottom mining was not addressed in AAI’s
model to evaluate the mine design or in GRI’s approved roof control plan. Similarly, barrier
mining was conducted in violation of the approved roof control plan. A portion of the barrier
immediately inby the last know location of the miners was mined even though it had been
specified to be left unmined. Although neither of these actions is a fundamental cause of the
August 6 collapse, they increased the amount of load transferred to pillars at the working face
and reduced the strength of the barrier adjacent to it.
The following sections of this report provide details that support the observations and
conclusions of the investigation of the August 6 accident. Included are discussions of: the
46
geology and mining methods at the mine; the relevant ground control history of the mine; the
various analyses that were used to determine the nature and extent of the failure; a critique of the
previous analyses that provided the basis for the implemented mining plan; and other safety
issues (e.g., mine ventilation, emergency response, and training) pertaining to the August 6
accident.
Background for Ground Control Analysis
Since both accidents at Crandall Canyon Mine were essentially ground control failures, factors
such as geology, mining dimensions, ground support, and mining method have direct or indirect
relevance to the accident or implications regarding conditions encountered afterward. An
overview of each of these subjects is provided below.
General Mine Geology
The Crandall Canyon Mine is located in the Wasatch Plateau coal field, within the Hiawatha coal
seam. The Hiawatha coal seam typically ranges from 5 to 13 feet thick in the Crandall Canyon
Mine reserve. Mining had been undertaken primarily where the coal seam height exceeded
7.5 feet. The Hiawatha coal seam is at the base of the Blackhawk formation (Upper Cretaceous
age). Corehole and geophysical data indicate that the overburden above the Hiawatha seam
consists of 49% to 68% sandstone. The immediate mine roof typically consists of 0 to 2 feet of
interbedded siltstone, shale, and sandstone overlain by bedded sandstone. The Star Point
Sandstone, which consists of massive sandstone beds interbedded with shale, lies beneath the
Hiawatha seam. A general stratigraphic column for the mine is shown in Figure 23.
The mine portal is at approximately 7,900 feet above sea level in the eastward trending Crandall
Canyon. Overburden ranges from less than 100 feet at the mine portal to 2,300 feet under the
higher ridges due to the steep mountainous terrain. The Blackhawk formation overlying the
Hiawatha coal seam consists of approximately 650 feet of interbedded sandstone and siltstone
with an occasional coal seam. The Blind Canyon coal seam lies 55 to 100 feet above the
Hiawatha coal seam. Within the Crandall Canyon Mine reserve, the Blind Canyon seam is
typically less than 3 feet thick and is not mined. Overlying the Blackhawk formation is the
approximately 250-foot thick, cliff forming, Castlegate Sandstone consisting predominantly of
sandstone interbedded with shale and siltstone. Alternating sandstone, siltstone, and shale of the
Price River and North Horn formations exist above the Castlegate Sandstone.
Geologic structure in the area consists of faults, joints, and igneous dikes. The most significant
geologic structure is the north-south oriented Joes Valley Fault system that delineates the
western perimeter of the mine reserve (see Appendix D). In the overlying Castlegate Sandstone
and Price River formation, the joint orientation trends north to N20ºE. In the southwest and
southern portion of the reserve an igneous dike system oriented at approximately N80ºW exists
near the southern reserve boundary.
Within the mine property, the coal seam gradually dips at 2.5º to 4º in all directions from a high
region in the northwest area (intersection of 2nd North Main and longwall Panel 7 development
entries). In the eastern portion of the mine, the face coal cleat (dominant cleat) trends N65ºW.
Within the central and western portion of the mine, the face coal cleat mostly trends N40ºE.
Sandstone immediate roof and sandstone channel scours of the coal seam have been encountered
in some areas.
47
Figure 23 - General Stratigraphic Column for Crandall Canyon Mine
Mining Horizon and Mining Width
The mining height throughout most of the Crandall Canyon Mine was maintained at 7.5 to 8 feet.
When the Hiawatha coal seam was less than 8-foot thick, the mined opening had rock roof and
floor. However, coal seam thickness often exceeded the mining height. In these areas, coal was
left unmined in either the floor or roof. Most of the North and South Barrier sections were
developed in the upper portion of the seam; the Main West entries were developed in the lower
portion of the seam.
For the mining of the North Barrier section, the roof control plan initially specified that no roof
coal would be left in place. While mining in the North Barrier, on January 18, 2007, the plan
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was modified to allow roof coal to be left in place in areas of weak immediate roof. The plan
specified that the minimum bolt length would be 6-foot in the roof coal areas. Prior experience
had shown that roof coal would help support weak roof rock. However, the roof coal did not
remain intact during retreat mining in the North Barrier section. Therefore, South Barrier section
entries and crosscuts were mined to the overlying rock.
While recovering pillars in the North and South Barrier sections, coal left in the floor during
development (bottom coal) was being mined. After the upper portion of a cut had been made,
the bottom coal would be mined. The continuous mining machine would ramp down into the
bottom coal (up to 5 feet in the western portion of the South Barrier section), starting at the edge
of the pillar and continuing to the end of the cut. The mining of bottom coal was not addressed
in the approved roof control plan.
Areas of Main West developed with continuous haulage were mined an average of
approximately 20 to 21 feet wide (based on measurements from 1991 era mining east of crosscut
107). In the newer development, entries and crosscuts were mined 18 feet wide, although the
approved roof control plan permitted a maximum mining width of 20 feet. Throughout the mine,
pillars showed an hour glass rib profile (see Figure 24). Consequently, mining widths measured
at mid pillar often were wider than the original excavated width. The hour glass rib profile was
evident when overburden exceeded approximately 1,100 feet and was more pronounced as the
depth increased. For example, measurements made during the accident investigation beneath
1,500 feet of cover indicated that older entries, which averaged 20.6 feet on development, had
hour glassed to 24.7 feet. Similarly, recently mined 18.5-foot wide openings had hour glassed to
an average of 22.4 feet.
Figure 24 - Hour Glass Shape of Stressed Pillars
Primary and Supplemental Roof Support
Prior to 1997, the primary roof support typically consisted of ¾-inch diameter, 5-foot long, fully
grouted roof bolts. Five bolts were installed per row, spaced 4 feet apart within a row and 4 to
5 feet between rows. In 1997, the primary support practice transitioned to six roof bolts per row
with 3- to 4-foot bolt-to-bolt spacing within the row and wire mesh was installed with the
primary roof bolts. Since 1997, six roof bolts per row and wire mesh were used for development
and rehabilitation. Wire mesh consisted of welded wire panels 17 feet wide with 4 x 4-inch
49
grids. In mid-2005, the mine adopted a 0.914-inch diameter x 5-foot fully grouted bolt as the
primary roof bolt for development mining and rehabilitation roof bolting. For the mining of the
North and South Barrier sections, the roof control plan specified six bolts per row with a
maximum distance of five feet between rows.
Wood posts, wood cribs, Cans (steel cylinders filled with light-weight concrete), and cable bolts
were used for supplemental support. Prior to 2004, wood posts were used as the only
supplemental support during pillar recovery. However, beginning in early 2004, four 800-ton
capacity Mobile Roof Support (MRS) units were used in conjunction with breaker posts for pillar
recovery.
Accidents Related to Ground Control Failures
Standardized form reports must be completed by an operator and sent to MSHA within ten
working days of each accident, occupational injury, or occupational illness that occurs at a mine,
as required by 30 CFR 50.20. The term “accident” includes the following non-injury ground
control related events, as defined in 30 CFR 50.2 (h):
• An unplanned roof fall at or above the anchorage zone in active workings where roof
bolts are in use;
• An unplanned roof or rib fall in active workings that impairs ventilation or impedes
passage;
• A coal or rock outburst that causes withdrawal of miners or which disrupts regular
mining activity for more than one hour.
Data from the standardized form reports are collected and maintained by MSHA. Mine
operators also must maintain a map on which roof falls, rib falls, and coal or rock bursts are
plotted. MSHA uses all of this information when reviewing roof control plans for adequacy
pursuant to 30 CFR 75.223 (d). In addition to submission of standardized form reports, 30 CFR
50.10 requires operators to immediately contact MSHA following an “accident” (as defined, in
part, above) at the toll-free number, 1–800–746–1553. MSHA procedures for responding to
accidents reported to the toll-free number ensure that the appropriate MSHA manager is rapidly
engaged in the decision-making process for initiating accident investigations and for determining
that the operator has taken appropriate action to protect miners and prevent a similar occurrence
in the future.
Since 1984, GRI submitted form reports for 23 ground control related injuries, 4 non-injury
accidents where a longwall tailgate travelway passage was impeded by ground failures, and
8 non-injury roof falls. However, only two of these roof falls were plotted on the mine’s roof fall
map required by 30 CFR 75.223(b). Prior to 2007, 8 injuries related to coal bursts and bounces
were reported. Seven of the eight events occurred during pillar recovery and longwall mining.
A 2-entry yield pillar longwall gate configuration was introduced for the deeper longwall
Panels 8 to 18 to minimize burst potential and roof instability in the vicinity of the longwall face.
Bounces sometimes occurred when the longwall panels retreated to a distance equal to the face
length (panel width) or when longwall mining was being conducted under the deeper
overburden. Records and interview statements show some bounces and bursts were severe
enough to cause reportable injuries. Accident records and interview statements indicate five
injuries from bursts and bounces occurred while longwall mining. Accident records also indicate
that a miner was injured during pillar recovery from a coal burst in December 1993 and another
was injured from a rib fall (reported as a bounce) in January 1994. Both accidents occurred
during pillar recovery in the 7th Left Panel off 1st North.
50
Room and Pillar Retreat Coal Mining Overview
At the time of the August 6 accident, pillars were being recovered on the South Barrier section.
Pillar recovery is undertaken at approximately 30% of the 638 underground coal mines in the
United States. Approximately 5% of the 638 underground coal mines project pillar recovery in
overburden exceeding 1,250 feet. In pillar recovery operations, a series of pillars are first
developed using a continuous mining machine and the associated mining equipment.
Subsequently, the same equipment is used to remove the pillars. The process generally involves
retreating from the deepest point of advance by taking sequential cuts from pillars with the
continuous mining machine (typically radio remote controlled) as illustrated in Figure 25.
Adjoining pillars are sequentially mined, one pillar row at a time. The regions where the coal
pillars are removed are allowed to cave. The border between the remaining pillars being
recovered and the area where the roof is expected to break is known as the pillar line. The
immediate work area is protected by the intact surrounding pillars and supplemental support
systems. The Crandall Canyon Mine used pillar recovery early in its history (until 1995) and
restarted pillar recovery in early 2004 (see Appendix D).
Figure 25 - Example of a Pillar Recovery Cut Sequence
Nature and Extent of Failure
The August 6, 2007, outburst accident was a rapid, catastrophic failure of pillars in a large area
of the mine. Rescue attempts in the South Barrier section entries and in the sealed portion of the
Main West entries provided direct observations of the nature and outby extent of the failure.
Boreholes from the surface provided insight on the inby side. These observations were
substantiated by survey and satellite borne radar subsidence data, and seismological records.
Seismological analyses indicate that the 3.9 magnitude event associated with the August 6 failure
was characteristic of a collapse event and not a naturally occurring earthquake. The mine
collapse resulted in a surface depression up to 12 inches. The greatest vertical movements (and
51
corresponding pillar damage at seam level) were located east of the last known location of the
entrapped miners. However, pillar damage of varying degrees extended over a much broader
area. The most accurate measure of the initiation time of the August 6 accident was 2:48:40 a.m.
(MDT). This time was determined from the seismological analysis and confirmed using records
from the atmospheric monitoring system in operation at the mine at the time of the accident.
Underground Observations
Within minutes of the accident, mine workers attempted to reach the South Barrier section to
assist their coworkers. These initial efforts and additional attempts in the following days
demonstrated that bursting had damaged pillars as far outby as crosscut 119, approximately
½ mile outby the entrapped miners. Debris from the outburst blocked access to all South Barrier
entries inby crosscut 126 (see Figure 26). Attempts to reach the miners by breaching a seal and
entering the Main West entries revealed poor ground conditions there as well. Inby the seals at
Main West crosscut 118, the ground was working and bounces were occurring. Pillar
deterioration (rib sloughage) had narrowed walkways to no more than 2 to 3 feet. Roof bolts
were showing signs of excessive loading.
Figure 26 - Extent of Pillar Rib Damage Outby Crosscut 119
On August 11, 2007, ground conditions were mapped in the Main West entries and the North and
South Barrier workings outby crosscut 119. Pillar damage was noted up to three crosscuts outby
the seals (see Figure 26). The damaged ribs did not appear to be the result of bursting. Rather,
the damage appeared to be associated with abutment stress transferred from inby the seals.
Figure 27 and Figure 28 illustrate the difference between damaged and undamaged pillar rib
conditions. Figure 27 shows normal Main West pillar rib conditions and Figure 28 shows recent
pillar rib sloughage from abutment stress.
52
Figure 27 - Normal Main West Pillar Rib Conditions
Figure 28 - Main West Pillar Rib Condition showing Recent Sloughage from Abutment Stress
53
Borehole Observations
Conditions determined by the boreholes and visual observations from borehole cameras set the
western boundary of the collapse between Borehole Nos. 3 and 4. Borehole No. 4 and others to
the east of that location indicated that the mine openings contained rubble. Boreholes in the
entries were filled or nearly filled with rubble while boreholes in the intersections contained less
rubble. Figure 29 depicts the borehole locations.
Figure 29 - Borehole Locations and Conditions Observed
Surface Subsidence Determined from GPS Surveys
Surface subsidence had been monitored over the Main West and the adjacent longwall panels
since 1999. Longwall subsidence data and characteristics are described in Appendix L. Initially,
a baseline survey was done to establish monuments along a north-south line south of crosscut
133 in the Main West (crosscut 129 in the South Barrier). Follow-up surveys were done
annually from 2000 to 2004. Aerial photogrammetric surveys were conducted in 2005 and 2006.
The aerial survey data lacked the accuracy required to supplement the land surveys.
On August 17, 2007, the subsidence monitoring line was resurveyed over a portion of the South
Barrier section and longwall Panels 13 to 14. The GPS survey was conducted along the line of
existing surface monuments to provide an updated profile of subsidence. Some of the
monuments that previously had been used to monitor subsidence were dislodged. Although the
data are incomplete, the profile indicates that a substantial downward movement
(approximately1 foot) occurred over the South Barrier between July 30, 2004, and August 17,
2007 (see Figure 30). However, some of the deviation noted in this and earlier time periods may
reflect accuracy limitations of the GPS surveys (±0.2 feet).
The longwall subsidence behavior observed in Figure 30 is somewhat typical of the Wasatch
Plateau. In this region, strong, thick strata in the overburden control caving characteristics and
are responsible for the high abutment stresses and long abutment stress transfer distances
discussed in the ground control analysis portion of this report. Subsidence data collected
elsewhere in the region indicates that the amount or extent of cantilevered strata at panel
boundaries varies. Data presented in Figure 30 indicate that subsidence adjacent to the South
Barrier section was incomplete over more than half the width of Panel 13. The figure also
demonstrates that additional subsidence over the panel and the adjacent barrier was observed
between 2004 and 2007. To determine how much of the recorded movement during the 3-year
period was associated with the August accidents, Interferometric Synthetic Aperture Radar
(InSAR) analyses were conducted.
54
Figure 30 - Subsidence Profiles over Panels 13 to 15
Measurements from 2004 and 2007, vertical scale exaggerated
Surface Subsidence Determined from InSAR Analyses
Interferometric Synthetic Aperture Radar (InSAR) analyses provide precise surface deformation
measurements using satellite radar images. The process compares satellite images taken over a
study area at different times to determine surface changes (see Appendix L). Although this
technique is relatively new to the U.S. coal industry, it has been used extensively to study ground
movement, including that due to earthquakes, groundwater loss, and volcanic activity.
Analyses of the Crandall Canyon Mine initially were conducted by the Radar Project of Land
Sciences at the U.S. Geological Survey’s Earth Resources Observation and Science Center in
Vancouver, Washington (USGS). Several time intervals were evaluated to assess surface
deformation before and after the August accidents. InSAR subsidence analyses for four time
intervals between: June and September 2006, December 2006 and June 2007, June and
September 2007, and September and October 2007 were evaluated. Three of the four intervals
displayed no significant subsidence. However, comparison of satellite images acquired on
June 8, 2007, and September 8, 2007 (a relatively short span of time within which the August
accidents occurred) revealed the development of a large subsidence depression over the accident
site.
Neva Ridge Technologies (Neva Ridge) in Boulder, Colorado, subsequently was contracted to
provide an independent InSAR analysis. The Neva Ridge report (see Appendix M) confirmed
the lateral extent and vertical displacements determined by USGS. Maximum vertical
displacement at the center of the depression was 12 inches (30 centimeters). Vertical subsidence
from the Neva Ridge study is shown on Figure 31. Calculations, based on coal density (in situ
and post mining) and mining geometry (pillar and entry volumes) demonstrate that surface
subsidence of this magnitude is consistent with extensive coal pillar bursts and substantial filling
of entries. A discussion of the two studies is included in Appendix L.
55
Figure 31 - Surface Deformation from Neva Ridge InSAR Analyses (June to Sept. 2007)
MSHA made visual surveys of the ground surface above Main West before the InSAR data was
available. These surveys were conducted from a helicopter and on foot. Mining related surface
deformation was not visible. However, a maximum of 12 inches (30 cm) of vertical subsidence
over such a broad area may not form visible slips or cracks. Soil slumps were noted but could
not be associated with the August accidents.
The InSAR analysis generally confirms the magnitude of subsidence determined in the GPS
survey and further constrains the time in which the subsidence occurred. The analysis also
provides insight to the lateral extent of the collapse zone. As illustrated in Figure 31, the surface
area affected by the collapse extends approximately 1 mile east-to-west and ¾ miles north-tosouth. At seam level, subsidence principles suggest that the extent of the collapse would be less
laterally but greater vertically than the surface expression implies.
The depth of burst coal in the No. 1 entry of the South Barrier section increased from crosscut
120 until it blocked access to all entries at approximately crosscut 126. Above crosscut 119, the
InSAR analysis indicates there was almost 2 inches (5 cm) of vertical subsidence; above
crosscut 126, the subsidence was approximately 6 inches (15 cm). The 15 cm subsidence
contour encompasses all of the area above the South Barrier section from crosscuts 126 to 142.
If the 15 cm contour is used as an indication of pillar damage severe enough to block all travel,
then the surface subsidence indicates that the entire working section was severely damaged. The
region of Main West between the longwall panels that subsided vertically 6 inches (15 cm) or
more was approximately 69 acres in area, centered near crosscut 135.
56
The area of greatest subsidence, and therefore the greatest damage at seam level, was centered on
the 121-foot wide barrier between the South Barrier section and longwall Panel 13. A maximum
displacement of nearly 12 inches was observed over the barrier pillar about 500 feet outby the
last known location of the entrapped miners. Borehole No. 5 penetrated the mine workings near
the point of maximum displacement and confirmed that the damage was severe there as
demonstrated by the observation that the void space in that intersection was only 0.5 feet.
It is noteworthy that the maximum surface displacement occurred near crosscut 135, a location
nearly equidistant from the ridge top (deepest overburden at ~crosscut 129) and the pillar line
(crosscut 142). This observation implies that either the coal pillars were weaker at this point or
the stress levels were higher than would be anticipated (i.e., if stress magnitude was based on
overburden and abutment load transfer from the active pillar line). However, additional
observations of both InSAR and GPS survey data suggest that stress rather than coal strength
controlled the location of the failure.
Traditional surface elevation surveys between 1999 and 2004 show that strata overlying about
half of the longwall panel south of the working section had not completely subsided and was
cantilevered from the Main West South Barrier. Both traditional and satellite surveys conducted
after the accident demonstrate that the surface over the panel and the barrier displaced downward
as much as 12 inches. Furthermore, the satellite analysis indicates that the strata movement that
occurred was much more abrupt at the southern and western edges of the depression (as
evidenced by the steeper subsidence contours). The abrupt displacement on the southern edge is
consistent with substantial failure of the 121-foot wide barrier and an associated downward
movement of cantilevered strata over the adjacent longwall gob. The volume of cantilevered
strata likely provided the additional loading necessary to initiate the collapse event from the
working section. The abrupt displacement on the western side is consistent with seismological
analyses that indicate that some movement may have occurred on a steeply dipping (near
vertical), north-south oriented plane.
Seismology
The seismic event created by the August 6 collapse was detected by a regional network of
seismographs maintained by the University of Utah. The preliminary location of the seismic
event near the Joes Valley fault apparently led to speculation by some that the event was a
naturally occurring earthquake. However, additional analyses of the event by both the
University of Utah 2, and the University of California at Berkeley and Lawrence Livermore
National Laboratories 3, determined that the seismic event was the result of the mine collapse.
Months after the August accidents, the University of Utah Seismograph Stations (UUSS)
reevaluated event locations using a “double difference” location method. This methodology can
only be used after subsequent events with known locations are available. At Crandall Canyon
Mine, the method used the known location of the August 16 accident to improve location
accuracy. The revised location indicated that the August 6 accident originated near the No. 3
entry of the South Barrier section between crosscuts 143 and 144.
Analyses of events recorded after the initial August 6 event provided additional insight to strata
behavior and the nature of the mine collapse. For example, seismologic records demonstrated
that activity persisted for more than 1-½ days after the initial failure. The UUSS reported this in
an August 9, 2007, 5:00 p.m. (MDT) press release:
57
Twelve seismic events were recorded by the University's seismic network in the
first 38 [sic] hours following, and in the vicinity of, the large event of August 6.
These smaller events range in magnitude from less than 1.0 to 2.2. A shock of
magnitude 2.1 occurred about 17 hours after the main event (at 8:05 PM MDT,
August 6); another of magnitude 2.2 occurred about five hours later (at 01:13
AM, August 7). These shocks are interpreted to reflect settling of the rockmass
following a cavity collapse.
The seismic record in this time period is consistent with underground observations of noise
emanating from the strata as the initial rescue efforts were underway.
Refined double difference locations of seismic events for the period of August 6 to August 27,
2007, are shown in Figure 32. These refined locations were unavailable until three months after
all rescue efforts had been suspended. The August 6 event is indicated by the red circle and the
twelve events that occurred within 37 hours afterward are represented as tan circles; the radius of
each circle corresponds to the relative magnitude of the events. Activity during the first 37 hours
after the accident was predominantly located on the outby side of the collapse area. Conversely,
seismic activity for the time period August 8-27 (shown as blue and magenta circles) was
concentrated on the inby side of the collapse area. Very few events were located near the north
and south boundaries of the collapse area.
Figure 32 – Double Difference Locations of Seismic Events, August 6-27, 2007
Seismologic analyses indicated that the August 6, 2007, event was dominantly a collapse
mechanism but the waveforms also included a smaller shear component. A likely explanation
was shear displacement along a vertical plane with movement downward on the east side. The
plane would have a strike of approximately 150 degrees azimuth. This conclusion is
substantiated by InSAR analyses which show a more abrupt displacement on the western side of
the collapse area than on the eastern side. Steeper subsidence in this region could be consistent
with movement on a steeply dipping, north-south oriented plane between the North and South
58
Barrier section gobs. Extensive near-vertical joints are a prominent geologic feature of the strata
at Crandall Canyon Mine.
Analyses also indicated that a collapse area of 50 acres moving downward approximately 1 foot
represents a plausible model to quantitatively account for 80% of the seismic moment (i.e., the
total energy) release associated with the event. Pechmann2 explains that “Although this model is
by no means unique, it serves to illustrate one possibility that is consistent with both the
seismological data and the underground observations.” A more detailed discussion of the
seismicity of the Crandall Canyon Mine is provided in Appendix N.
Time of the Accident
Seismological data and mine-specific atmospheric monitoring records provided a very precise
time of occurrence. The origin time of the seismic event was determined to be 2:48:40 a.m.
(MDT). Seismic monitoring systems incorporate very accurate clocks to ensure that events
detected by networks across the world can be correlated with one another.
An atmospheric monitoring system (AMS) was operating in the mine. The system consisted of
computers, sensors, and a network to gather and record data on carbon monoxide (CO), fan
pressure, tonnage mined, and conveyor belt status. At the time of the accident, a series of
communication failures occurred on the system. The failures began at the CO sensor on the
South Barrier section alarm box and progressed to other sensors outby. The computer-generated,
printed alarms for the initial failures showed a time of 2:51:31 a.m. However, the time display
on the AMS computer that generated the printed alarms was not accurate.
To determine an accurate time for the event, the AMS clock was synchronized with the time base
at UUSS by telephone. This was done on several occasions to account for any drift in the
monitoring system clock. Based on the AMS data, the corrected time of the communication
failure report was calculated to be 2:48:53 a.m. The 13-second difference between the
2:48:40 a.m. seismic event and the corrected AMS communication failure time can be explained
largely by the methodology used by the AMS system to report a loss of communication and by
the accuracy of the time correction.
AMS alerts and alarms typically occur some time after the actual corresponding event,
depending on the size and configuration of the system. The AMS system scans all sensors on the
system. When a communications failure occurs, repeated attempts are made to communicate
with the sensor before a failure is reported by the computer. The number of attempts can be set
by the user. The time to report a communication failure depends on the time it takes for the
system to cycle through the sensors and the number of attempts the system is set to make. It
appears that data was being collected for the “CO Main West Section Alarm Box” sensor at an
interval of 2 to 3 seconds before the accident. Because sensors were removed from the system
after the accident, the pre-accident interval could not be determined during the investigation.
Also, the number of attempts to reestablish communication for that sensor is unknown but was
reported by the manufacturer to be typically 3 to 5. The accuracy of the time correction was
estimated at plus or minus five seconds. Together, the time lag to report the communication
failure and the uncertainty of the time display can explain the difference between the seismically
determined time of event and the AMS communication failure. The most accurate measure of
the initiation time of the August 6 accident was 2:48:40 a.m. (MDT), as established by the
seismic data.
59
Summary - Nature and Extent of Failure
The nature and extent of the collapse were estimated by combining all of the underground and
borehole observations, surface subsidence, and seismic evidence previously described.
Seismological analyses indicate that the 3.9 Richter event associated with the August 6 failure
was characteristic of a collapse event and not a naturally occurring earthquake. Analyses also
indicate that it originated from a point near the last row of recovered pillars, just inby the last
known location of the entrapped miners. The collapse occurred at 2:48:40 a.m. (MDT) and it
lasted only several seconds. This time was determined from the seismological analysis and was
consistent with corrected times from the atmospheric monitoring system in operation at the mine
at the time of the accident.
Surface subsidence data (GPS surveys and InSAR analyses) indicate that a surface depression up
to 12 inches deep formed over the Main West between June 8 and September 8, 2007. Vertical
movements greater than ¾ inches were observed on the surface over an area approximately
1 mile (east-to-west) by ¾ miles (north-to-south). A maximum displacement of nearly 12 inches
was observed over the 121-foot wide barrier pillar about 500 feet outby the last known location
of the entrapped miners. Borehole No. 5 penetrated the mine workings near the point of
maximum displacement and confirmed that the void space in an intersection was only 0.5 feet.
Although the displacements observed in the InSAR analyses could have occurred at any time
between June 8 and September 8, several observations suggest that much of the movement was
associated with the August 6 accident. First, it is noteworthy that negligible amounts of
displacement were noted in analyses of time periods before June and after September. Second,
seismic activity detected in the aftermath of the event is located on the east and west margins of
the surface depressions. Finally, seismologists estimate that a relatively large volume of strata
(e.g., 50 acres of ground moving downward approximately 1 foot over the Main West) must have
been involved to account for measured seismic moment (i.e., total energy) of the event.
The satellite analysis indicates that the strata movement was much more abrupt at the southern
and western edges of the depression (as evidenced by the steeper subsidence contours). The
abrupt displacement on the western side is consistent with UUSS’s theory that some movement
may have occurred on a steeply dipping (near vertical), north-south oriented plane. The abrupt
displacement on the southern edge is consistent with substantial failure of the 121-foot wide
barrier and an associated downward movement of cantilevered strata over the adjacent longwall
gob. The volume of cantilevered strata likely provided additional loading on the South Barrier
section.
Figure 33 superimposes a variety of data used to determine the extent of the collapse, including:
the seismic data from the time of the August 6 accident to August 27, 2007, the borehole
locations, the InSAR subsidence contours, and the likely extent of damaged pillars. The eastern
boundary of the pillar failures was based on the underground observations and InSAR
subsidence data and is consistent with residual seismic activity. The western edge of the pillar
failures was based on the borehole observations and InSAR subsidence data and is consistent
with the seismic location of the accident and the additional seismicity later in August 2007.
60
Figure 33 - Combined Data and Likely Extent of Collapse
The extent coincides approximately with the 5 cm vertical subsidence line. The 5 cm line falls
between Borehole Nos. 3 and 4. The area indicating extensively damaged pillars was based on
conditions observed near crosscut 126 where the damage was more severe and the entries were
impassable. The boundary of the area follows the 15 cm subsidence contour and encompasses
Boreholes Nos. 1, 2, 4, 5, 6, and 7, all of which showed damage.
Main West Ground Control History
The history of ground conditions in Main West provides a basis for the engineering backanalyses discussed in a later section of this report. Back-analysis is a process in which known
failures or successes are evaluated to determine the relationship of engineering parameters to
outcomes. For example, the mining scenario associated with the March 10, 2007, outburst
accident in the North Barrier section provides insight to the conditions conducive to bursting at
Crandall Canyon Mine. Furthermore, the history demonstrates GRI’s failure to report outburst
accidents. The following sections detail the sequence of events and associated ground control
implications that culminated in the August 6 accident.
Main West Development
The Main West entries adjacent to the August 6, 2007, accident site were developed in 1995.
This development included five entries and crosscuts on 90 x 92-foot centers. These workings
were mined using a mobile bridge continuous haulage system. Pillar corners were rounded and
entries were mined to 20 feet or wider (particularly the middle entry, which contained the
conveyor belt system). The mining height was established at 8 feet by mining to the bottom of
61
the seam and leaving roof coal in the immediate roof. The entries were stable for several years
after development, prior to adjacent longwall mining.
Longwall Panel Extraction
Longwall panels were mined parallel to the Main West entries between 1997 and 2003. Six
panels were mined north of Main West (Panels 7 to 12) and six were mined to the south
(Panels 13 to 18). Barrier pillars measuring approximately 450 feet wide were established
between Main West and the adjacent longwall Panels 12 and 13 (see Figure 34).
Figure 34 – Initial Main West Barrier Pillars after Panel 13 Mining showing Overburden
In retreat mining operations (longwall or pillar recovery), barrier pillars are used to protect
workings from abutment loading associated with panel extraction and to separate active
workings from worked out areas. As a block of coal is mined, the immediate roof above the
block falls into the void created by mining. At shallow depths and with suitably wide panels, the
roof failure can propagate to the surface and allow much of the weight of the overburden to be
transmitted directly to the mine floor in the caved area. A portion of the overburden usually
cantilevers over the void near the edges (see Figure 35). These cantilevered strata create load on
the void boundaries in excess of the typical overburden load that would be carried.
In deep overburden and/or in narrow extraction areas, failure may not propagate to the surface.
Instead, strata near the excavation can fail and fall into the void while higher strata may simply
sag onto the fallen lower layers. The strength and stiffness of rock layers in the mine roof
generally dictate the degree to which the uncaved layers sag and transfer load into the broken
material (gob). If the rock layers are strong and thick, load can be transferred across the void
created by mining in much the same way that an arch bridge rests on abutments at either of its
ends. This abutment stress is usually highest near the excavation and lessens with distance away
from the caved area.
62
Figure 35 - Abutment Stress due to Cantilevered Strata from Mining
63
In the Main West entries, some influence of abutment stress was observed when each of the
adjacent longwall Panels 12 and 13 were extracted in 1999. Abutment stresses associated with
these longwall panels caused pillar rib sloughage and roof deterioration. A similar observation
was noted earlier as longwall panels were mined to within about 400 feet of the 2nd North Mains.
These observations imply that the Main West barriers and entry pillars were subjected to
abutment stress and effects of this stress were evident at distances beyond 450 feet (the
approximate width of the original barriers).
Abutment stress from Panels 12 and 13 caused damage in Main West that required additional
roof support to maintain stability. The area with the most roof deterioration and pillar sloughing
appeared to be the region beneath more than 1,800 feet of overburden, which was approximately
between crosscuts 123 and 150. In this region, roadways were timbered-off, roof coal was
falling from around roof bolts, and pillars showed significant rib sloughing. It was noted that
roof coal deterioration was most apparent in the middle No. 3 entry followed in severity by the
No. 2 and No. 4 entries. Efforts focused on maintaining the No. 1 entry near the south barrier
and No. 4 entry nearer the north barrier as intake and return air courses. As longwall mining
progressed southward, the Main West entries required continued maintenance particularly to
keep the stopping line intact.
After March 2003, longwall mining south of Main West was completed and the worked out
longwall district was sealed. The Main West entries were no longer needed as part of the
longwall ventilation circuit. However, the area was not sealed at that time because GRI
anticipated the possibility of recovering the Main West pillars. Later, GRI decided to forgo
pillar recovery of the Main West workings inby crosscut 118 and sealed the area in
November 2004. In a letter to the BLM dated November 10, 2004, GRI claimed that it “decided
to construct the seals for the following reasons:
1. The abutment loads from the longwall districts to the north and south of Main West in
this area have caused the roof and coal pillars to deteriorate to a point that a substantial
economic investment would be required to rehabilitate the area. This investment would
likely exceed the economic value of any recovered coal.
2. The majority of the coal resource left in place is in cover greater than 1,500 ft. MSHA
currently will not approve pillar extraction in areas where the cover exceeds 1,500 ft.
3. The amount of air necessary to keep this area ventilated is making it difficult to get
ventilation to those active areas of the mine where the ventilation is required.”
The referenced ventilation problems included the recurrent need to perform maintenance on
stoppings in the Main West entries due to continued ground deterioration. In justification of
sealing the area, a BLM inspector also noted pillar failure and several large roof falls.
Sealing the Main West had ground control implications. First, the seals prevented access for
evaluation of ground conditions west of crosscut 118. Further deterioration of pillars that could
lead to additional stress transfer to the adjacent barriers could not be observed. Second, the seals
prevented the barriers from being extracted in the manner that had been used in the South Mains.
In the South Mains, barriers adjacent to worked out longwall panels were recovered using a
“rooming out” technique. Barriers on either side of the South Mains were developed
sequentially as illustrated in Figure 36. This method helped maintain the integrity of the barrier
outby the working section since the barrier width was reduced only near the retreating pillar line.
A similar plan could not be used in the sealed Main West without extensive rehabilitation to the
existing Main West entries and crosscuts.
64
Figure 36 – South Mains “Rooming Out” Pillar Recovery Sequence
65
North Barrier Section Development
In contrast to the sequential development and recovery plan used in the South Mains, four entries
were driven on 80 x 92-foot centers through the Main West North Barrier prior to retreat. The
original 448-foot barrier width was reduced during development to 135 feet between the section
and Panel 12 to the north and to 53 feet between the section and the sealed Main West to the
south (see Figure 37). One implication of this approach was that the load bearing capacity of
these barriers (i.e., their ability to support front and side abutment loading during pillar recovery)
was reduced. Another was that entries used to access the working faces were subjected to
abutment loading during development.
Figure 37 - North Barrier Section Mining showing Overburden
Development of the North Barrier section began in late 2006 and had advanced to crosscut 123
when Agapito Associates, Inc. (AAI) personnel visited the section on December 1, 2006 (see
Appendix H). Overburden depth at this location was about 1,900 feet. Based on their
observations, AAI reported that “There was no indication of problematic pillar yielding or roof
problems that might indicate higher-than-predicted abutment loads.”
MSHA District 9 Roof Control personnel visited the developing North Barrier section on
January 9, 2007. At that time, the section had advanced to about crosscut 141, situated beneath
2,000 feet of overburden, past the deepest overburden (2,240 feet) at crosscut 132. Billy Owens
(District 9 roof control group supervisor) and Peter Del Duca (inspector trainee) observed pillar
hour glassing outby the face and were present during the failure of the rib in a crosscut. Owens
stated that “about 200 to 300 feet out from the mining face, the --- one of the pillars sloughed,
and I mean, it was almost a whole crosscut, probably 6 to 12 inches thick, the rib just set down.
But it didn't throw coal out into the walkway. It didn't expel any particles that would strike
anyone. It just laid down --- sloped down and laid down against the rib.” Owens stated further,
“I considered that to be the pillar yielding in the controlled manner that it should.”
All parties (GRI, AAI, and MSHA District 9) placed a great deal of emphasis on the nature of the
observed pillar yielding during the development phase of mining (i.e., that it was nonviolent).
66
For example, Laine Adair stated in an interview with the investigation team that “the main things
that we were really looking at that was of most interest to Billy [Owens] and to me and to
Agapito on our other visits was how the coal was yielding as these pillars yielded? Was it in a
nonviolent fashion?” Nonviolent yielding of the coal ribs was perceived as an indication that the
mine design was effective. However, a rib failure of this extent in an area where persons work or
travel is not indicative of effective rib control to protect persons from related hazards.
Similar ground conditions were noted after MSHA’s January 9 visit. Gary Peacock reported in a
memo to Adair that “We advanced the section 14 xc's from 137 to 151 in January. Even though
the amount of cover has gone from 2,200' to 1,500', we are still seeing a considerable amount of
rib sloughage. It does create some problems, but is no worse than we would expect to see
mining in the barrier like we are.” Bounces were occurring outby the face areas resulting in rib
sloughage. The resulting rib sloughage was greatest from crosscut 135 to 142 which was the
area of greatest overburden. There was some minor floor heave in this region that did not require
grading.
Development proceeded in the North Barrier more than 4,600 feet (measured from crosscut 108)
to crosscut 158. Water began flowing from the floor and roof near crosscut 145 to 146. Section
development was stopped at crosscut 158, five crosscuts short of the projected extent, due to
excessive water inflow. This was the same water zone that had been encountered in the north
side of Main West in 1995.
North Barrier Section Pillar Recovery
Pillar recovery operations were initiated in the North Barrier section on February 16, 2007. Two
of the three pillars in each row were extracted while the third pillar between the Nos. 3 and 4
entries was not mined to provide a bleeder entry. The section was retreated from west to east.
MRS units were used in-lieu-of turn posts near the continuous mining machine during pillar
mining. MRS units and wooden posts were used for breaker rows.
Initially, the roof did not cave immediately as pillars were removed, resulting in higher stress in
the pillars being mined. Some miners and mine management felt that the section was too narrow
to promote good caving. On February 21, 2007, after removing four rows of pillars, eight
stoppings were blown out by caving within the pillared area. The next day, foremen reported
that hard bounces were occurring and that caving remained close to the pillar line.
BLM inspector Stephen Falk visited the section on February 27, 2007. In the associated
Inspection Report, finalized on July 12, 2007, Falk noted: “So far, the crews have pulled 18
pillars or 9 rows. Currently they are pulling the pillars between crosscut 149 and 150. I have
been concerned about pulling pillars in this environment with mining a narrow block with little
coal barriers to mined out blocks on both sides. Fortunately, the beginning depth on the west
end toward the Joe's Valley Fault is somewhat shallow starting at 1300 feet. So far no
inordinate pillar stresses have been noted, though things should get interesting soon. The face is
under 1600 feet of cover now and will increase to over 2000 feet by crosscut 139. The working
face looks ok and coal is good. There is some cap rock in the roof that is not holding up during
mining.” Foremen also reported “good bounces” occurring that day.
Beginning on February 28, 2007, in the vicinity of pillar Nos. 23 and 24 at 1,880 feet of
overburden, foremen regularly reported problems with the immediate roof, bounces, blown out
stoppings, and associated production delays. The roof coal and soft rock above it broke into
small pieces that fell onto the wire mesh and caused it to sag down between the roof bolts.
67
Larger stumps were left unmined in the pillars to avoid the sagging wire mesh. On March 3, a
Murray Energy Corporation employee emailed a copy of Crandall Canyon Mine’s production
report for the night shift ending March 1, 2007, to Jerry Taylor (Corporate Safety Director):
“Fyi…this is at least the third time they have noted walls blown out by caves on the pillar
section. Must be pretty violent. You see they had to pull the [continuous mining machine] out
and had stone between the [continuous mining machine] and the MRS supports.”
Stoppings were blown out during both shifts on Sunday, March 4. The next day, Bruce Hill
(president and CEO of UEI, ARI, and GRI) reported to Murray: “The mine should continue to
perform well for the next three months as we pull pillars. The one potential obstacle remains the
depth of cover. We are now approaching 2,000 feet of cover. MSHA has never allowed pillar
recovery at this depth. I was in the mine on Sunday and while the pillars were bumping and
thundering, the conditions remain good.” Also on March 5, foremen reported “ran steady until
around 3:00 PM, had a couple hard bounces that knocked top coal loose in #2.” Eight-foot bolts
were installed in the affected area, delaying production for eight hours.
A coal burst occurred during the night shift beginning March 6 and ending March 7, 2007. A
lump of coal ejected during the burst struck a miner in the face. An entry in the shift foremen’s
report noted, “Bouncing real hard on occasion. Smacked little Carlos [Payan] up aside of the
haid [sic] with a pretty good chunk.” Payan received a small cut on the side of his head, which
required first aid treatment only, and he continued working in his normal duties.
A non-injury coal outburst accident during the following day shift on March 7 knocked miners
down and damaged a stopping. The shift foreman’s report described the event as: “Had 1 real
hard bounce, blowed ribs down in 2-3 crosscut & beltline…” The production report showed a
delay in mining of 70 minutes after the event. MSHA was not immediately notified of the March
7 coal outburst accident as required by 30 CFR 50.10. GRI did not file an accident report with
MSHA as required by 30 CFR 50.20.
On March 8, a coal burst tripped a breaker on an MRS unit, requiring the crew to set timbers
prior to resetting the breaker. This event caused a 30-minute production delay.
On March 9, 2007, in an attempt to alleviate the poor ground conditions, GRI stopped pillar
recovery between crosscuts 137 and 138 and resumed mining between crosscuts 134 and 135.
However, the following morning, foremen reported that the section was “still bouncing pretty
hard.” Hill also reported to Murray: “The mine is experiencing heavy bouncing and rib
sloughage. We moved the section back two crosscuts to provide a barrier.” Although Hill
characterized the decision to skip several rows as providing “a barrier,” the move was not made
in consideration of specific concerns about abutment stress. Peacock made the decision to “get
to where we hadn’t left any of the top coal and where the initial roof was good.” Mining
resumed in an area of greater overburden.
The concept of skipping pillar rows was consistent with AAI’s recommendations at that time. In
an August 9, 2006, email report to Adair from Leo Gilbride (AAI principal) the report stated:
“The plan affords the contingency to leave occasional pillars for protection during retreat if
conditions warrant, thus providing additional control of the geotechnical risk” (refer to
Appendix G). AAI cautioned against this practice after the March 2007 outburst accidents.
68
March 10, 2007, Coal Outburst
At 5:22 p.m. on March 10, 2007, a non-injury coal outburst accident occurred on the working
section while mining the first cut of the southernmost pillar from the No. 1 entry between
crosscuts 133 and 134. The associated seismic event registered magnitude 2.3. The outburst
threw coal into entries and crosscuts between 131 and 139 and suspended dust in the air for 5 to
10 minutes, obstructing vision. Most of the damage was in the Nos. 3 and 4 entries and rendered
the bleeder entry unsafe for travel. Coal expelled from the ribs was up to four feet deep in some
entries and crosscuts. A scoop was blocked by coal debris in the No. 3 entry between crosscuts
133 and 134.
During the following shift, crew members cleaned coal from the entries and crosscuts with the
continuous mining machine. They also set timbers, retrieved the scoop, and repaired stoppings.
Peacock was notified of the burst at approximately 10:00 p.m. and he traveled to the mine later
that night to observe conditions on the section. On March 11, Peacock noted in an email to
Adair and Hill that “conditions in the pillar section have deteriorated to the point that I don’t
think it is safe to mine in there any longer. We are pulling the equipment out and setting up to
mine south. The bad conditions consist of some huge bounces and the stopping line is no longer
intact back in the bleeder entry. It is not safe to have people in there repairing the stoppings. I
talked to Dave Hibbs this morning, he is looking into the possibility of not needing a new MSHA
plan to mine south until we go past the seals. I realize pulling out early could change the way
MSHA views the plan on the south side. I also realize we have used all the tricks we know of to
pull these pillars and I no longer feel comfortable we can do it without unacceptable risk.”
Mining was temporarily moved to the 3rd North spare section while the South Barrier section was
prepared for mining.
MSHA was not immediately notified of the March 10 coal outburst accident as required by
30 CFR 50.10. Later, on March 12, GRI contacted MSHA District 9 personnel by telephone. In
a documented call to Owens, Adair indicated that the section was pulling out due to damage to
the bleeder entry. Later that day, GRI left a phone message with William Reitze (District 9
ventilation group supervisor) stating that it was not safe to travel to the approved bleeder
measurement point location (MPL) due to a bounce but that there were no plans to immediately
seal the area. On March 13, GRI contacted Reitze by telephone and requested to replace
damaged permanent ventilation controls adjacent to the bleeder entry with curtains. Reitze
denied the request. GRI then proposed a possible relocation of the MPL. When this request was
also denied (because ventilation of the worked out area could not be adequately evaluated from
the proposed location), the mine operator requested approval to seal the area. During a regular
inspection, Randy Gunderson (MSHA coal mine inspector) was informed by GRI that mining
had ceased because “the country got rough.” He did not travel to the damaged area. These
communications with MSHA minimized the extent of the adverse conditions and failed to
accurately portray the degree of the damage.
Records indicate BLM personnel were also notified of the March 10 event on March 12. As
noted earlier, some of the Crandall Canyon coal reserves were leased from the Federal
government and managed by BLM. BLM has a mandate to manage these coal resources to
maximize economic recovery whenever possible. GRI had to obtain BLM’s approval to leave
behind coal that would otherwise be mined.
BLM inspector Stephen Falk visited the North Barrier section on March 15. He noted damage
on a map filed with his inspection report. He verbally approved GRI’s request to cease mining in
the North Barrier, to seal the area at crosscut 118, and to mine the one entry of the Main West
69
South Barrier on the BLM coal lease. A written approval from BLM to GRI dated August 27,
2007, confirmed the verbal approval. The written approval indicated that GRI reported adverse
ground conditions with damaging bounces as justification to BLM for leaving the rest of the
pillars in the North Barrier section.
At the request of Adair, AAI personnel observed conditions in the section on March 16, 2007.
The site visit was documented by photographs and a map showing pillar, entry, and crosscut
conditions from crosscut 131 to 145. Figure 38 and Figure 39 illustrate a damaged stopping and
conditions in the No. 4 entry from a collection of photos taken on March 16, 2007 (see Appendix
O to view additional pictures). AAI’s notes and photographs confirmed Falk’s representation of
conditions on the section in his report. The North Barrier section was sealed on March 27, 2007.
Figure 38 – Stopping Damaged during March 2007 Coal Outburst Accident on North Barrier Section
Figure 39 –Damage in No. 4 Entry after the March 2007 Coal Outburst Accident on North Barrier Section
70
GRI contracted AAI to refine the pillar design for the South Barrier section based on the
conditions encountered during the mining of the North Barrier section. AAI evaluated ground
conditions resulting from the coal outburst accident, analyzed the proposed South Barrier
mining, and made recommendations for mining the Main West South Barrier (see Appendix I).
South Barrier Section Development
In an effort to mitigate the potential for a failure similar to the one that occurred in the North
Barrier section, two changes were implemented during development of the South Barrier section
and a third was implemented during pillar recovery:
• entries were mined to the rock in the roof (as opposed to leaving roof coal),
• crosscut spacing was increased from 92 to 130 feet, and
• the width of the caved area was increased by slabbing the barrier between the No. 1 entry
and the adjacent longwall Panel 13.
After the March 10, 2007, coal outburst accident, AAI made recommendations for mining in the
South Barrier that included a precaution that “Skipping pillars should be avoided in the south
barrier, particularly under the deepest cover.” Bagging of roof coal had contributed to the
operator’s decision to skip pillars in the North Barrier section. By mining to the rock, the
operator effectively eliminated the potential for a recurrence of this type of roof control problem
and the resulting need to skip pillars.
In the South Barrier section, pillar length was increased by 38 feet (from 92 to 130-foot centerto-center – see Figure 40). AAI indicated that this change “increases the size and strength of the
pillars’ confined cores, which helps to isolate bumps to the face and reduce the risk of larger
bumps overrunning crews in outby locations.”
Figure 40 - South Barrier Section Mining showing Overburden
Development of the South Barrier section began on March 28, 2007. By late April 2007, four
entries were being driven on 80 x 130-foot centers from crosscut 118 through the length of the
Main West South Barrier. The original 438-foot barrier width was reduced during development
to 121 feet between the section and Panel 13 to the south and to 55 feet between the section and
the Main West No. 1 entry room notches to the north. A sump had been mined southward from
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the Main West No. 1 entry at crosscut 150. The South Barrier section No. 4 entry was not mined
through between crosscuts 140 and 141 to ensure that a minimum 50-foot barrier remained
between the section and the sump. The entries and crosscuts were mined eight feet high and
18 feet wide. No coal was being left against the roof. Loose rock was also being mined from the
roof. Coal was left in the floor where coal seam thickness exceeded 8 feet. The section was
typically dry with one wet area at crosscut 140.
During development mining, roof and rib conditions were better than in the North Barrier. Mine
management attributed the improvement to the larger pillars. Owens and Jensen visited the
section on May 22, 2007. Owens determined that pillars were yielding closer to the face (which
he interpreted as being favorable) and that pillars outby appeared to be more stable than in the
North Barrier. Despite these improvements, reports indicated that bounces occurred and the ribs
showed significant signs of hour glassing and sloughage. The South Barrier section was mined
to crosscut 149, its projected limit, with development completed on July 15, 2007.
South Barrier Section Pillar Recovery
Pillar recovery began in the South Barrier section on July 15, 2007. The section was retreated
from west to east. Pillars between the No. 1 and 3 entries were extracted and the barrier to the
south was slabbed to a depth up to 40 feet. Pillars between No. 3 and 4 entries on the north side
of the section were not mined. These pillars remained in place to protect the No. 4 entry which
served as a bleeder. MRS units were used during pillar recovery and bottom mining was taking
place in pillar cuts and in barrier cuts (slabbing) south of the No. 1 entry. Barrier slabbing was
intended to facilitate better caving inby the pillar line by creating a wider span. Better caving, in
turn, was intended to reduce abutment stress transferred to the pillar line.
Grosely was conducting an inspection in the South Barrier section on July 17 and 18, 2007.
Removal of the first pillar was taking place during his inspection. He did not hear any bounces
and the pillars on the section looked stable. He observed some floor heave in the belt entry.
This was the last time MSHA was on the section before the August 6 accident.
The cut sequence when mining a row of pillars is shown in Figure 41. Half of the No. 1 pillar
and the barrier to the south were mined simultaneously, right and left, from the No. 1 entry
(Sequence A). The remainder of the No. 1 pillar and the No. 2 pillar were then mined as they
had been in the North Barrier section (Sequences B, C, D, E, F, and G).
Figure 41 - South Barrier Section Pillar Recovery Cut Sequence
72
During pillar recovery, eight pillars and the barrier between crosscuts 139 and 142 (where the
South Barrier section was reduced to three entries) were designated to remain unmined. This
unmined area was intended to protect the bleeder entry from abutment stresses associated with
the eventual caved areas to the west and east.
The first large intentional cave within the pillared area of the South Barrier section occurred
July 21, 2007, after recovery of two rows of pillars. The caving roof caused an air blast that
blew out five stoppings, and delayed production for nearly three hours. As the South Barrier
section retreated toward deeper overburden, rib failures and floor heave became more frequent.
On July 30, 2007, a bounce occurred at the working face, which broke a torque shaft on the
continuous mining machine. Two days later, an intentional cave inby the pillar line damaged
stoppings and disrupted production for approximately two hours.
On August 3, 2007, at 4:39 a.m., a non-injury coal outburst accident occurred at the face as the
night shift crew mined the first cut to the north of No. 2 entry from the pillar between crosscuts
142 and 143. Coal was thrown into the entries along the entire length of the pillar, dislodging
timbers and burying the continuous mining machine cable. The continuous mining machine
operator was struck by coal. He was not injured, but the lower half of his body was covered with
material. A stopping was damaged and a separation was observed between the mine roof and the
damaged pillar. The crew retrieved the continuous mining machine, removed debris, and
replaced some of the dislodged timbers before leaving the section at 6:00 a.m. When the day
shift crew arrived on the section at 8:35 a.m., they repaired the damaged stopping and finished
cleaning roadways and resetting timbers in the No. 2 entry. The accident was not immediately
reported to MSHA as required.
Coal production resumed at 10:35 a.m., as the day shift crew mined the remaining cuts from
either side of the No. 2 entry inby crosscut 142. Adverse ground conditions in the No. 3 entry
prevented mining the north half of the damaged pillar (cut F and G as shown on Figure 41).
Crew members (including the section foreman) discussed the possibility that management would
decide to pull out of the South Barrier section due to similarities between the outburst accident
that morning and the events in the North Barrier. The section was visited by mine management,
who discussed the conditions with the section foreman. After this discussion, the section
foreman informed the crew that they were to begin mining the barrier and skip some pillar rows.
The crew moved the continuous mining machine outby crosscut 142 in the No. 1 entry and
mined a lift from the barrier pillar. Six cuts were mined from the barrier during the night shift,
retreating to near crosscut 141. Mining in the barrier between crosscuts 139 and 142 was
prohibited by the approved roof control plan.
On August 4, 2007, the day shift crew moved the section loading point and power center outby
to crosscut 138. They also moved the section equipment. The floor had heaved, making the
move difficult. The night shift crew routed two MRS unit cables through the No. 1 entry to
continue mining in the barrier pillar before leaving the section at 5:30 a.m.
On August 4, 2007, Gary Peacock emailed agenda information to Bruce Hill and Laine Adair for
a management meeting scheduled for August 7, 2007. He described conditions in the South
Barrier section: “The conditions have been very good, we are getting a lot of good floor coal and
85%+ of recovery on the pillars. The cave is good and high and staying right with us for the
most part.” In anticipation of the August 7 pillar line location, he also wrote: “We just started
on the row outby the area where the 3 rows were left, this week will be critical to get the
maximum out of each pillar to start a good cave without having the weight go over the top of
73
us.” Although Peacock characterized conditions as very good, numerous bounces and a noninjury coal outburst accident had occurred as the pillar line approached crosscut 142.
At 7:30 a.m. on August 5, 2007, the day shift crew arrived on the section. Before mining, they
graded floor heave to provide clearance for shuttle cars from the loading point at crosscut 138 in
the No. 2 entry to the face in the No. 1 entry. At 11:25 a.m., the crew started mining cuts from
the barrier pillar between crosscuts 140 and 141. Production was interrupted from 2:25 p.m. to
3:25 p.m. by an electrical power outage during a lighting storm, after which mining continued
until the end of the shift. The night shift crew arrived on the section at 6:25 p.m. and relieved the
day shift crew, which had mined a total of four cuts from the barrier pillar. The night shift
continued mining the barrier until the time of the August 6 accident, as detailed in the August 6
Accident Description section of this report. Analysis of conveyor belt scale data and information
obtained from miners who were on the section shortly before the accident indicated that the night
shift crew was mining in the barrier pillar near crosscut 139 at the time of the August 6 accident.
Summary – Main West Ground Control History
Ground conditions encountered historically in the Main West demonstrate that the mine design
was insufficient for pillar recovery in deep overburden. Main West workings were affected by
abutment stress as adjacent longwall panels were extracted and these workings deteriorated over
time. Subsequent development mining in the barriers on either side of Main West encountered
high stress levels, particularly under the deepest overburden. During pillar recovery in both the
North and South Barrier sections, increased stress levels contributed to increasingly difficult
ground conditions that culminated in coal outburst accidents.
Historical ground conditions in Main West also provide a basis for engineering back-analyses of
strata behavior. As indicated earlier, back-analysis is a process in which known failures or
successes are evaluated to determine the relationship of engineering parameters to outcomes.
Longwall abutment stress transfer was observed in the Main West more than 450 feet away from
the mined-out panels. Of particular significance for stability analysis is the mining scenario
associated with the March 10 non-injury coal outburst accident in the North Barrier section. This
event demonstrated that 60-foot wide coal pillars at the Crandall Canyon Mine were prone to
bursting under high stress attributed to deep cover and abutment stress.
Analysis of Collapse
Mine design is somewhat unique in comparison to other engineering structural design projects.
In other disciplines, designers choose among a variety of materials with different mechanical or
aesthetic properties. Often the materials are man-made (e.g., steel or concrete) with precisely
controlled properties and known behavior. In contrast, mine design is limited by the properties
of the coal or ore that is extracted and the host rock surrounding it. Usually, these geologic
materials contain weaknesses (e.g., bedding planes or joints) and other inherent variations that
complicate design because properties (and often applied loads) cannot be precisely determined or
controlled. As a result, most if not all engineering analyses of geologic structures incorporate
various generalizations, simplifications, and assumptions. Furthermore, uncertainties in material
properties and applied loads necessitate designs that err on the side of safety.
A variety of analyses are available to assess ground stability in mine design. The basis for the
analyses can be empirical (e.g., based on statistical treatment of case histories), analytical (i.e.,
based on fundamental principles of mathematics and/or mechanics), or numerical (i.e., based on
an iterative mathematic process to find an approximate solution controlled by a complex
interaction of variables). Various analyses rely on different input parameters or different
74
representations of the same parameter. For example, pillar stability analyses may rely on
empirically derived coal strengths or they may be determined from laboratory tests or minespecific back-analysis. Despite these differences, when used properly, each analysis can provide
valid and valuable insight to mine design.
As part of the Crandall Canyon Mine accident investigation, three approaches and computer
programs were used to evaluate ground behavior in general and pillar response in particular:
•
Analysis of Retreat Mining Pillar Stability (ARMPS15) calculations,
•
Finite Element Method (UT2 4) modeling, and
•
Boundary Element Method (LaModel 5) modeling.
In these analyses, the pillar dimensions and extraction widths were determined from mine maps.
The overburden was determined by translating and rotating the USGS topographic map into the
mine area based on state plane coordinates and corresponding mine local coordinates. The
USGS topographic contours were digitized and then used with the digital mine top-of-coal
contours to calculate the overburden for the mine area. The resulting overburden map was
similar to the overburden contours on the Crandall Canyon Mine map. However, the map
generated for the investigation contained more overburden contour detail.
The following sections provide detailed discussions of each analysis. It is important to note that
input values (e.g., coal strength) vary between methods but each is valid for the type of analysis
in which it is used. Similarly, thresholds used to interpret safety or stability factors are not
directly comparable between methods. Although the three approaches differ substantially from
one another, all three indicate that a widespread catastrophic pillar failure was central to the
events at the Crandall Canyon Mine. ARMPS analyses revealed that stability factors (relative
measures of stability) were below NIOSH’s recommended minimums and also below the mine’s
historical experience. Finite element analyses indicated strong potential for a rapid catastrophic
failure of the North and South Barrier sections and the Main West pillars between them.
Similarly, boundary element analyses confirmed that the Main West was vulnerable to widespread failure; these results also provided insight to the factors that contributed to the overall
collapse and potential means of triggering the event.
Safety/Stability Factors
Engineering analyses often evaluate the reliability of a design by calculating a factor that relates
the strength of a design to its loading condition. The three programs used in this investigation
(ARMPS, UT2, and LaModel) use different methods to calculate a measure of stability.
Consequently, values or criteria from one type of analysis must not be related or compared
directly to values from another type of analysis.
ARMPS. The ARMPS program calculates a stability factor (StF) which has the following
relationship:
StF =
Pillar Load Bearing Capacity from the Mark Bienawski Equation
Pillar Load from geometric configuration and field data
In the literature, the ARMPS stability factor is expressed with the term: “SF.” To avoid
confusion with the factors calculated in UT2 and LaModel, ARMPS stability factor in this report
is designated as “StF.” Based on a mining database of successful and unsuccessful case
histories, recommended StF design criteria were developed. ARMPS design criteria are
75
empirically derived and should not be used with factors derived from UT2 and LaModel which
have a different calculation basis.
UT2. In the UT2 analyses, a safety factor (SF) from material modeled as linear elastic can be
determined by the following relationship:
SF =
Strength
Stress
or
Load Carrying Capability at Elastic Limit
Applied Load
The SF values in the UT2 analysis follow the typical engineering safety factor relationship where
material strength is divided by applied stress.
LaModel. In the LaModel analysis a safety factor (SF) from material modeled as strainsoftening or elastic-plastic can be determined for a particular element by the following
relationship:
Peak Strain
SF =
Applied Strain
The LaModel SF is a strain-based (deformation-based) safety factor. Traditionally, safety factors
are calculated on a stress basis. For LaModel analyses using nonlinear materials, strain-based
safety factors are more appropriate.
Analysis of Retreat Mining Pillar Stability (ARMPS)
Pillar stability was evaluated using the ARMPS program developed by Christopher Mark and
others at the National Institute for Occupational Safety and Health (NIOSH) Pittsburgh Research
Laboratory (a former US Bureau of Mines research center). This program is considered an
empirical approach because it is based on a statistical analysis of case histories. More than 250
case histories (including successful and unsuccessful experiences) have been documented and
used to develop the ARMPS database of stability factors (StF). StF’s are similar to safety factors
(SF) in that they are calculated as the ratio of strength to stress (or load carrying capacity to
applied load). StF’s in ARMPS, however, are computed specifically for pillars using two basic
assumptions. First, pillar strength is computed using an empirical pillar strength formula (the
Mark-Bieniawski equation). Second, pillar load is estimated using geometric relationships and
stress distribution criteria developed from field data.
ARMPS can be used to provide a first approximation of the pillar sizes required to
prevent pillar failure during retreat mining. It also provides a framework for evaluating
the relative stability of workings in an operating mine. For example, ARMPS stability
factors can be calculated for both successful and unsuccessful areas at a given mine site.
This approach, referred to as “back-analysis,” can be used to establish a minimum StF
that has been shown to provide adequate ground conditions. This minimum then can be
used as a threshold for design in subsequent areas as changes occur in the depth of cover,
coal mining height, or pillar layout.
Site-specific criteria used in lieu of NIOSH’s recommendations should be developed
cautiously using multiple case histories with known conditions at a given mine. Backanalysis is most appropriate for mines that have a proven track record of retreat mining.
In these cases, proper examinations of individual mine data may demonstrate that
stability factors above or below NIOSH’s recommended values are warranted. Proper
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examination would entail an analysis of the broad experience at a mine site rather than a
focus on isolated case(s) that represent the extreme.
The ARMPS software calculates stability factors using 15 user-provided input parameters:
1. Entry Height
9. Barrier Pillar Width
2. Entry Width
10. Depth of a slab cut
3. Number of Entries
11. Loading Condition
4. Entry Spacings
12. In Situ Coal Strength
5. Crosscut Spacing
13. Unit Weight of the Overburden
6. Crosscut Angle
14. Breadth of the Active Mining Zone (AMZ)
7. Depth of Cover
15. Abutment Angle
8. Extent of Active Gob
Parameters 1 to 10 are dimensions of individual mine openings and the overall mining section
that must be established by the user (see Figure 42). Item 11 is associated with the sequence in
which panels of pillars are recovered and is defined in the ARMPS help files. Parameters 12 and
13 are properties of the coal seam and rock comprising the overburden; defaults values are
provided in the software and should be used if the user plans to utilize NIOSH recommended
StF’s. The last two parameters are program specific values that establish the geometry used to
estimate abutment loading of pillars. Again, defaults values are provided in the software and
should be used if the user plans to utilize NIOSH recommended StF’s.
Input parameters for each of the case histories in the NIOSH database were used to compute
StF’s for both successful and unsuccessful cases. The unsuccessful cases included pillar
squeezes, massive pillar collapses (usually accompanied by air blasts) and coal bursts.
According to NIOSH, pillar squeezes account for approximately two-thirds of the failures in the
database. In addition, there were 14 sudden collapses and 17 bursts.
Figure 42 - Illustration of ARMPS Input Related to Panel Geometry
(after Chase et al.15)
77
ARMPS StF’s, depth of cover, and outcomes (successful or unsuccessful) comprising the
NIOSH database are illustrated in Figure 43. At depths below 650 feet, NIOSH noted that 88%
of the failures occurred when the ARMPS stability factor was less than 1.5. In contrast, the
ARMPS stability factor was greater than 1.5 in 78% of the successes.6 They concluded that an
ARMPS StF of 1.5 or greater is appropriate at these depths. At depths greater than 650 feet,
Chase et al. (2002)7 noted that StF's less than 1.5 can be employed successfully. The solid line
drawn across Figure 43 represents minimum StF’s recommended by NIOSH for various depths
of overburden. However, NIOSH’s analyses also noted that the use of large barrier pillars at
depths greater than 1,000 feet substantially increased the likelihood of success. NIOSH
incorporated this factor into their recommendations.
Figure 43 - ARMPS Case History Data Base (Chase et al.7)
In addition to calculating StF’s for “production” pillars that are recovered (PStF), ARMPS also
determines stability factors for barrier pillars (BPStF) that separate pillar recovery sections from
adjacent pillared workings (see Figure 42). Only one failure (out of 12 cases) in the NIOSH
deep cover database occurred when the PStF was greater than 0.8 and the BPStF was greater
than 2.0. Conversely, 30 case histories had a PStF less than 0.8 and a BPStF less than 2.0 and
60% of these cases were failed designs. Based on these data, NIOSH recommended the criteria
shown in Table 4:
Table 4 - NIOSH Pillar Design Considerations
ARMPS
Stability Factor
Pillar (PStF)
Barrier Pillar
(BPStF)
Overburden (H)
650’ ≤ H ≤ 1,250’
1,250’ ≤ H ≤ 2,000’
H › 1,000’
Weak and
Intermediate Roof
Strength
1.5 – (H- 650) / 1,000
0.9
≥ 2.0
Strong Roof
1.4 – (H-650) / 1,000
0.8
≥ 1.5 (Non-bump prone ground)
≥ 2.0 (Bump prone ground)
(see Appendix Y for definition of bump prone ground)
78
The ARMPS stability factor for a given mining configuration represents the average value for
pillars in an area near the pillar line, the active mining zone (AMZ – see Figure 42), rather than
for individual pillars. NIOSH explains the rationale in a Help file in the ARMPS software:
ARMPS calculates the Stability Factor for the entire AMZ, rather than
stability factors for individual pillars, because experience has shown that
the pillars within the AMZ typically behave as a system. If an individual
pillar is overloaded, it will normally transfer its excess load to adjacent
pillars. If those pillars are adequately sized, the process ends there.
With regard to barrier pillar stability (BPStF), the program calculates stability factors for barrier
pillars on either side of the pillar line. Furthermore, since barrier dimensions can change due to
barrier slabbing (see Figure 42), the program provides BPStF’s for locations outby (BPStF) and
inby the pillar line (remnant BPStF).
Pillar Recovery Analyses at Crandall Canyon Mine. Pillar recovery operations at Crandall
Canyon Mine were back-analyzed for the accident investigation using ARMPS. It is not possible
to characterize the effectiveness of these operations in every instance (i.e., the conditions
encountered during panel development and extraction are not fully known). Nonetheless,
ARMPS stability factors for pillars and barriers provide a relative measure of the designs used in
various areas of the mine. Back-analyses were performed in four pillar recovery areas: 1st North
Left block panels (continuous haulage panels between 1st North and 1st Right), the South Mains,
the North Barrier section, and the South Barrier section. These analyses were conducted at
specific locations of interest within each area (e.g. under high overburden or locations with
known ground conditions).
For each ARMPS analysis, input values related to mining geometry (e.g. number of entries, pillar
dimensions, or overburden) were determined from mine maps. An 8-foot mining height and
20-foot entry width was assumed in all cases. Similarly, ARMPS default values for coal strength
(900 psi), unit weight of overburden (162 lb/ft3), abutment angle of gob (21º), and extent of the
active mining zone were used in all cases.
The use of default values in the analyses allows the output to be compared directly with stability
factors in the NIOSH database where the default values also were employed. 7 This approach
provides a relative comparison of mining scenarios at Crandall Canyon Mine and direct
consideration of NIOSH’s minimum recommended stability factors.
1st North Left Block Panels Pillar Recovery. In early 1992, continuous haulage panel
development began to the west of the 1st North main entries. Nine panels were developed and
extracted in sequence from north to south (see Appendix D). The continuous haulage panels
were developed in a 5-entry configuration with 60º angle crosscuts. The typical panel was
driven with five entries on 74-, 56-, 82- and 82-foot centers (spacing measured perpendicular to
the center belt entry) and crosscuts on 80-foot centers. Multiple mining units were used and, as a
result, development and extraction of a panel to the south lagged slightly behind the development
and extraction of a panel positioned to the north.
Overburden increased from east to west in the 1st North panels and approached 1,800 feet near
1st Right. ARMPS analyses were done for four panels, 6th to 9th Left, under the deeper cover
(Figure 44). Results of the ARMPS analyses are included in Table 5.
79
Figure 44 - 1st North Mains Left Panel ARMPS Calculation Areas
Table 5 - Pillar Stability Factors for Continuous Haulage Panel Back-Analysis
Panel
6th Left
7th Left
8th Left
9th Left
Average
Overburden,
ft
1300
1500
1760
1680
1560
Development with Side
Gob
BPStF
PStF
2.11
0.88
1.99
0.76
1.79
0.64
1.87
0.67
1.94
0.74
Retreat with Side and
Active Gob
BPStF
PStF
1.72
0.48
1.64
0.42
1.52
0.36
1.80
0.46
1.67
0.43
The four red squares in Figure 45 represent ARMPS stability factors associated with the
1st North continuous haulage system panels. Although no catastrophic failures were reported,
pillar recovery was not trouble-free. Accident records indicate that two injuries resulted from
bounces (one of which was a coal burst) during pillar recovery in late 1993 and early 1994 in the
7th Left continuous haulage panel. Also, pillars were abandoned in each panel to alleviate some
form of difficult ground condition. Roof coal had been left during development of these panels
and this practice may have contributed to the difficulties. Regardless of the reason for leaving
the pillars, these unmined zones indicate that pillar recovery was not entirely successful.
80
Barrier Stability Factor (BPStF)
2.5
NIOSH Minimum PStF
1st North Panels 6 to
9 Pillar Recovery
NIOSH Minimum BPStF
2
South Mains Pillar
Recovery
1.5
1
NB Recovery using
Different Calculation
Methods at 2160 ft OB
0.5
0
0
0.5
1
1.5
2
Pillar Stability Factor (PStF)
Note: NB = North Barrier, SB = South Barrier, OB = Overburden
1st North Panels 6 to 9 Recovery
South Mains Pillar Recovery
NB Failure Method 2 - 2160 OB
NB Failure Method 3 - 2160 OB
SB Recovery - 2000 OB
NB Failure Method 1 - 2160 OB
SB Recovery - 1640 OB
Figure 45 - ARMPS Stability Factors at Crandall Canyon Mine
South Mains Pillar Recovery. The South Mains pillaring process involved mining a series of 3-4
rooms east and/or west from the original 5-entry main, typically 3 crosscuts deep into the
adjacent longwall barrier pillars (see Figure 36). The newly formed pillars were typically the
same dimensions as the original South Mains pillars (approximately 80 x 112-foot centers). The
new pillars and the original South Mains pillars were then extracted. This process was repeated
along the length of the South Mains, where overburden ranged from 700 to 1,520 feet.
Four areas with relatively high overburden and minimal barrier width to the longwall gobs were
selected for back-analysis using ARMPS. The areas were between longwall Panels 6 and 18,
Panels 5 and 16, Panels 4 and 15, and Panels 3 and 13 (see Figure 46). At each of these
locations, the maximum extraction area and minimum barrier widths were applied in the analysis
to subject pillars and barriers surrounding the developing gob to the highest degree of loading.
This approach was used to define the lower limit of the historical pillar stability factors
associated with pillar recovery in the South Mains. Results of the ARMPS analyses are included
in Table 6.
The light blue triangles in Figure 45 represent stability factors associated with pillar recovery in
the South Mains. Two of the cases satisfied the NIOSH criteria for minimum stability factors.
Although no catastrophic failures were reported, miners described “heavy” conditions on the
pillar line indicative of high stress and pillar bounces were reported. These conditions led the
operator to adopt a pillar recovery sequence in which pillars were extracted exclusively in one
direction rather than alternating the direction between successive rows. Reportedly, less
“thumping” was experienced on the pillar line when the pillars were extracted exclusively from
west-to-east. Also, interview statements and documents indicate pillar “bouncing” occurred
during pillar extraction in the South Mains. Two rows of pillars beneath a ridge near the center
of South Mains (1520 feet of overburden) were not extracted.
81
Figure 46 - South Mains ARMPS Calculation Areas
Table 6 - Pillar Stability Factors for South Mains Back-Analysis for Areas with Side and Active Gobs
Area Mined
Between Panels
6 and 18
Between Panels
5 and 16
Between Panels
4 and 15
Between Panels
3 and 13
Average
Overburden
(ft)
Development with Side
Gob
Retreat with Side and Active Gob
Original
West
BPStF
Original
East
BPStF
PStF
BPStF,
West
Barrier
BPStF,
East
Barrier
Minimum
BPStF
PStF
1330
7.35
2.12
1.53
5.36
2.10
2.10
0.94
1300
7.00
7.03
1.43
1.59
2.02
1.59
0.72
1200
7.84
7.81
1.55
2.28
2.03
2.03
0.87
1130
8.64
12.55
1.72
5. 65
1.78
1.78
0.78
1240
7.71
7.38
1.56
1.88
0.83
North Barrier Section. Recovery mining in the North Barrier section extracted the two southern
pillars leaving the northernmost pillar intact for a bleeder system. Prior to December 2007, the
ARMPS software did not have the capability to model bleeder system geometry directly. At
least three alternatives could be considered for determining stability factors in this scenario.
82
1. Assume that the bleeder pillar is not developed. Using this approach, the section is
modeled as a three entry system and the overall width of the barrier is the sum of the actual
barrier width plus the bleeder pillar width.
2. Assume that the entire pillar row is mined. In this model, the load bearing capacity of the
bleeder pillar is not considered.
3. Assume a greater barrier width than the actual dimension. In this approach, the load
bearing capacity of the bleeder pillar is determined and a recalculated barrier dimension is
used. The barrier dimension is chosen such that its load bearing capacity represents the
combined strength of the actual barrier pillar and the bleeder pillar (see Appendix P).
Each of these approaches uses a different assumed geometry (Figure 47) and provides a different
result. The first method generates the highest PStF and the second and third methods generate
lower and similar PStF values. Consequently, when compared to NIOSH pillar design criteria
from the NIOSH database or pillar design from mine site back-analysis, the first method is more
likely to overstate stability than the second or third method. The inappropriateness of Method 1
is evident in the fact that StF’s calculated for a retreating section using this method are actually
greater than StF’s calculated for development using actual pillar and barrier dimensions (see
Table 7). When comparing the design to NIOSH or mine site specific design criteria, the second
and third methods offer the safest approach.
Table 7 - Pillar Stability Factors for North Barrier Section
Calculation
Method
1
(215-foot barrier)
2
(135-foot barrier)
3
(147-foot barrier)
Overburden
at Failure
(ft)
Development with
Side Gob
Retreat with Side and
Active Gob
BPStF,
North
Barrier
BPStF,
North Barrier
PStF
1.39
0.40
0.88
0.24
0.96
0.22
PStF
2160
2160
0.91
2160
0.35
Since overburden at the location where the March 10, 2007, non-injury coal outburst accident
occurred was 2,160 feet, that value was used in the back-analysis for pillar recovery to establish
a minimum stability factor threshold for future pillar design. Results of the ARMPS analyses
using all three assumptions for incorporating a bleeder pillar are included in Table 7.
The magenta colored shapes in Figure 45 represent ARMPS stability factors for the North
Barrier section determined using the three methodologies discussed earlier. They are grouped
together in an oval to signify that all three correspond to the same mining scenario. Regardless
of the methodology used, both the pillar stability factor and barrier pillar stability factor fall
below the NIOSH recommended values for bump-prone and non-bump-prone ground. The low
stability factors indicate that poor ground conditions and/or section failure would be anticipated
during pillar recovery.
83
Figure 47 - Methods of Incorporating a Bleeder Pillar in ARMPS Analyses
South Barrier Section. Approximately 25% of the South Barrier section was developed in
overburden exceeding 2,000 feet. Thus, analyses to assess the overall section design were based
on that overburden depth. These calculated pillar stability values are summarized in Table 8.
The table also includes PStF and BPStF values for 1,640 feet of overburden. This is the
maximum cover that the retreating pillar line encountered in the South Barrier section prior to
the August 6 accident.
Table 8 - Pillar Stability Factors for South Barrier Section
Development with Side Gob
Method
N/A
N/A
Overburden
(ft)
2000
1640
BPStF
South
Barrier
0.91
1.18
PStF
0.46
0.73
84
Retreat with Side and Active Gob
BPStF
South
Barrier
0.76
1.00
PStF
0.23
0.35
The blue square and orange diamond in Figure 45 correspond to these two pillar recovery
scenarios. Since the bleeder pillar in this section was not adjacent to the barrier along the
Panel 13 gob, the ARMPS software could consider the South Barrier width directly (i.e., without
making adjustments like those for the North Barrier). Had the pillar line retreated to a point
beneath the deepest cover, the PStF and BPStF would have been nearly the same or less than
those associated with the March burst in the North Barrier (substantially lower than values
determined using the method with the highest risk, Method 1, and lower than the NIOSH
recommended values). Although longer pillars were employed in the South Barrier section, the
thinner barrier towards Panel 13 and the slab cut into the barrier during pillar recovery result in
larger calculated abutment loads and lower StF’s. As before, the low stability factors indicate
that poor ground conditions and/or failure would be anticipated.
Effects of Barrier Pillar Recovery on Main West Entries. ARMPS analyses typically are used to
assess the stability of a single pillar recovery panel. Other approaches such as finite element and
boundary element modeling are better suited to evaluate a catastrophic pillar collapse like the
one that occurred at Crandall Canyon Mine on August 6, 2007. However, if the effects of
longwall mining north and south of the section are neglected entirely, ARMPS provides a
simplified way of evaluating the overall stability of the Main West pillar system.
The Main West can be represented as a developed section (no pillar recovery) bounded on either
side by the North and South Barrier Section workings, as illustrated in Figure 48. On
development, the Main West PStF is 0.86 (near borderline with respect to NIOSH
recommendations) for the maximum Main West overburden of 2,160 feet. As the North Barrier
is recovered, the PStF drops to 0.70, below the recommended level, and even further to 0.66 with
extraction in the South Barrier. In fact, the actual StF’s are likely much lower given the age of
the workings (i.e., pillar degradation over time) and the influence of the adjacent longwall
workings.
NOT TO SCALE
Figure 48 - ARMPS Layout for Simplified Main West Analysis
85
Summary. ARMPS stability factors for Crandall Canyon Mine pillar recovery scenarios are
illustrated in Figure 45. In this figure the vertical and horizontal solid color lines represent
NIOSH recommended minimum stability factors (0.8 PStF and 2.0 BPStF). The recommended
NIOSH values (0.8 PStF and 2.0 BPStF) are for overburden deeper than 1,250 feet with strong
roof and bump prone ground. ARMPS stability factors that are above or below NIOSH
recommended values do not ensure success or failure. However, when stability factors are
maintained above the thresholds for both production and barrier pillars, experience (reflected in
case studies in the NIOSH database) has demonstrated likelihood for success.
With the exception of portions of the South Mains pillar recovery areas, stability factors at the
mine were below NIOSH recommendations and, as would be expected, various ground control
problems were experienced. The low stability factors in the North and South Barrier sections, as
well as in the adjacent Main West entries, show a high potential for ground failure. The
following finite element and boundary element analyses show similar results.
Finite Element Analysis
Dr. William Pariseau, Professor of Mining Engineering at the University of Utah, performed an
analysis of mining in the Main West barriers at Crandall Canyon Mine using the finite element
method (FEM). FEM analyses have been used widely in the field of civil and aerospace
engineering and in a variety of geomechanics applications as well. In FEM analysis, the area to
be studied is represented by a grid of discrete areas or elements. Properties and loadings are
assigned to each element. A system of equations is constructed and solved to determine the
stress, strain, and displacement of each element. Computer programs are utilized to prepare and
calculate results and to display the model output. To model Crandall Canyon Mine, Dr. Pariseau
elected to use a 2-dimensional FEM program, UT24, which he had previously developed. The
objective of this study was to develop a better understanding of the strata mechanics associated
with the August 6, 2007, accident at the Crandall Canyon Mine.
A complete review of Dr. Pariseau’s FEM analysis is beyond the scope of this report. However,
a report that he prepared is included in its entirety as Appendix Q. His report describes the study
methodology and results in detail.
In the FEM analysis, rock above and below the coal seam and the seam itself were modeled as
linear elastic materials. The term linear elastic implies that the materials deform at a constant
rate to an increasing or decreasing load. Generally, rock response to initial loading is considered
elastic. However, at elevated load levels beyond the elastic limit of a given rock type, fracture
and material flow lead to irreversible deformation or “yielding.” Although an elastic FEM
analysis does not consider rock failure and yielding explicitly, the models can provide insight to
ground stability by evaluating safety factors. Safety factors (SF) can be defined as follows:
SF =
Strength
Stress
or
Load Carrying Capability at Elastic Limit
Applied Load
When the load applied to a model element is greater than that element’s load carrying capability,
the SF is less than 1.0 and is considered to have failed. In reality, yielding and failure prevent
applied loads from exceeding load bearing capacity and, therefore, SF cannot be less than 1.0.
However, in an elastic model computed SF’s may be less than 1.0 and the distribution of these
lower values provides a measure of the degree of failure likely in a given mining scenario.
Elastic-plastic elements can be used in FEM analysis to model yielding behavior. However, post
failure behavior of rock materials is difficult to resolve and the analyses are complex and time
86
consuming. Generally, the effect of yielding in an elastic-plastic analysis is to “spread the load”
in a model. Element yielding essentially creates a limit above which additional loading can no
longer occur and excess loads must be transferred to adjacent elements. In contrast, an elastic
model provides an optimistic analysis of stability since stress may exceed strength. Thus, if an
unsafe condition is inferred from the results of an elastic analysis, then it is likely that any actual
instability will be even more widespread.
In the Crandall Canyon Mine analysis, a model was prepared to examine stresses and
displacements in mine strata in a two-dimensional cross-section through the Main West
workings. The cross-section measured 6,480 feet in an approximately north-south orientation
and extended 2,609 feet vertically. These dimensions encompassed worked-out longwall panels
north and south of Main West and overburden above the Hiawatha seam and 1,000 feet below
the seam. The Hiawatha seam was modeled as an 8-foot thick unit.
An overburden thickness of 1,601 feet was used in the FEM analysis to correspond with the
length of a borehole that was used to characterize the stratigraphy of Crandall Canyon Mine. In
the FEM analysis, beds of similar rock type are represented as layers with specific material
properties. These properties usually are developed from laboratory tests on rock samples
obtained from coreholes. Using fundamental principles of engineering mechanics, the FEM
computes stresses and strains induced in the rock mass by excavation.
In the Crandall Canyon Mine model, calculations were performed for four stages of excavation:
(1) excavation of the Main West entries, (2) excavation of longwall panels on either side of the
Main West entries, (3) excavation of entries in the north barrier pillar, and (4) excavation of
entries in the south barrier pillar. At each mining stage, stresses and strains were computed to
illustrate the effects of mining.
Main West Mining. Model results in the first stage of excavation, Main West development,
suggest that the roof, floor, and pillars would be stable. Pillar safety factors are greater than 2.2
(i.e., strength is more than double the applied stress). Safety factors are even greater in the roof
and floor due to the greater strength of the shale and sandstone materials.
Longwall Mining. Model results in the second mining stage, longwall panel extraction, indicate
that some areas have reached the elastic limit while others are well below (see Figure 49). For
example, 25% of the barrier pillar separating the Main West from the longwall panels has
yielded in this stage of mining. Although the remainder of the barrier adjacent to the Main West
has not yielded, it is highly stressed. The gray elements in Figure 49 indicate mine openings in
the Hiawatha seam and the black elements represent element safety factors less than 1.0.
Dr. Pariseau stated that:
“Safety and stability of an entry surrounded by an extensive zone of yielding
would surely be threatened. A pillar with all elements stressed beyond the elastic
limit would also be of great concern.”
Although yielding is isolated to the longwall side of the barrier opposite Main West, longwall
mining has had a significant effect on stress levels in the Main West pillars. The highest SF in
the Main West pillars is 1.34 which is substantially less than the values on development. Roof
and floor SF’s are in the 4 to 5 range suggesting that they continue to be stable.
87
Figure 49 - Element Safety Factors about a Barrier Pillar after Longwall Mining
North Barrier Section Development. Model results from the third stage of excavation,
development in the North Barrier, indicate that most elements in the north side barrier pillar are
now at yield (note the black elements on the right side of Figure 50 at seam level). Rib elements
in pillars adjacent to the Main West entries are also at yield. The outside entry of Main West
shows ribs yielding in the pillar between it and the new north side barrier pillar entry. The south
outside entry ribs show yielding extending 10 feet into the ribs and the highest safety factor in
any pillar element in Figure 50 is 1.2.
South Barrier Section Development. The fourth and last stage of analysis is entry development
in the South Barrier. The distribution of element safety factors at this stage is shown in Figure
51. Almost all elements in the south side barrier pillar are now at yield and all pillar elements
across the mining horizon are close to yield. Again, since purely elastic behavior leads to an
underestimate of the extent of yielding, it is likely that yielding would spread further and affect
portions of the pillars that have not yielded in the elastic model.
Peak vertical stress in the barrier pillars exceeds 38,400 psi, over 9 times the unconfined
compressive strength of the coal. Horizontal stress exceeds 7,300 psi. Even so, this high
confining pressure is insufficient to prevent yielding. The lowest vertical pillar stress is about
6,000 psi, almost half again greater than the unconfined compressive strength of the coal; the
lowest horizontal pillar stress is about 1,500 psi. Any release of horizontal confinement would
likely result in rapid destruction of pillars. Additionally, entries nearest to the mined panels are
showing reduced roof and floor safety factors. Overlying coal seams are also yielding or are
very close to yielding over portions of the barrier pillars, as seen in Figure 51. These model
results are indicative of unstable conditions.
88
Figure 50 - Element Safety Factor Distribution after North Barrier Section Development
89
Figure 51 - Element Safety Factor Distribution after South Barrier Section Development
90
Conclusions of Finite Element Analysis. Dr. Pariseau’s FEM analysis of barrier pillar mining at
Crandall Canyon Mine “indicates a decidedly unsafe, unstable situation in the making.” It is
noteworthy that the analyses used “optimistic” input values and assumptions that would tend to
make the mine workings appear to be more stable as opposed to less. For example:
•
Models assumed overburden depth of about 1,600 feet even though the actual overburden
exceeded 2,000 feet in some locations.
•
The 2-D analysis did not account for crosscuts that would increase the actual pillar stress.
•
The analysis did not account for pillar recovery that would further increase pillar stress.
•
Elastic material properties were used that limited stress transfer normally associated with
yielding behavior.
•
Laboratory strength values were used in the analysis even though rock masses tend to be
weaker.
Despite the use of these “optimistic” input values and assumptions, the results indicate a
potential for rapid destruction of the pillars with expulsion of the broken coal into the adjacent
entries.
Boundary Element Analysis
The boundary element method using the displacement-discontinuity calculation is well suited to
modeling thin, tabular deposits like coal seams (see Appendix R). In contrast to the twodimensional finite element model discussed in the previous section, BEM programs provide a
quasi three-dimensional analysis capability. As illustrated in Figure 52, entries and pillars in a
coal seam can be represented as a plane of elements bounded by a rock mass. Stress changes and
displacements associated with mining activity can be evaluated by comparing successive models
in which elements are altered to correspond with the changing mine geometry.
Figure 52 - Illustration of Boundary Element Model Components
91
Like all numerical methods, BEM results are always dependent on the input values. In
particular, properties that define the behavior of the coal seam, the gob, and the rock mass
surrounding the seam are critical (see Figure 52). Furthermore, numerical models can only be
considered to be reliable after they are adjusted (i.e., calibrated) so that they duplicate observed
field behavior.
Crandall Canyon Mine Back-Analysis. Dr. Keith Heasley, Professor of Mining Engineering at
West Virginia University, performed an analysis of mining in the Main West area using the
boundary element method. Dr. Heasley used LaModel, a BEM program which he had
previously developed. One objective of this work was to use the best available information to
back-analyze the August 6, 2007, pillar failure in order to better understand the geometric and
geomechanical factors that contributed to the collapse. Another objective was to perform a
parametric analysis of pertinent input parameters to assess the sensitivity of the LaModel results
to the input values.
A complete review of Dr. Heasley’s BEM analysis is beyond the scope of this report. However,
a report that he prepared is included in its entirety as Appendix S. His report describes the study
methodology and results in detail.
LaModel Calibration Process. In the LaModel analyses, rock above and below the coal
seam were modeled as frictionless layers of linear elastic materials. However, elements
representing the coal were modeled using strain softening material properties. Strain softening
properties simulate the failure process by defining an elastic threshold beyond which an
element’s load bearing capacity decreases; in effect, at some predetermined peak load, the
element yields and with further deformation, load bearing capacity generally decreases.
Elements near an opening may actually shed load as a result of the yielding process. Elements
further from openings yield at progressively higher peak loads and at some point may sustain the
peak load with further deformation (i.e., plastic behavior).
Numerical analyses that incorporate strain-softening or elastic-plastic behavior provide a means
of assessing element failure and any associated stress redistribution. However, in geologic
materials, these properties are not easily defined. Furthermore, the modeled behavior of pillars
comprised of groups of these elements, is affected by other model parameters (e.g., rock mass
and gob properties). The selection of appropriate material properties relies primarily on the
model “calibration” process.
Model calibration is an iterative process in which the analyst compares simulated results with
known actual conditions (or in some instances, proven analytical solutions) to verify that model
output is reasonable. The process, also referred to as “back-analysis,” essentially demonstrates
that the model is capable of duplicating known historical outcomes before it is used to evaluate
future scenarios.
Dr. Heasley’s report provides an overview of calibration as it pertains specifically to the
LaModel program. The most critical factors with regard to accurately calculating stresses and
loads, and, therefore, pillar stability and safety factors, are:
• The Rock Mass Stiffness
• The Gob Stiffness
• The Coal Strength
Each of these factors may comprise more than one input parameter (e.g., rock mass stiffness is
defined by a lamination thickness and a rock mass modulus). Furthermore, a change in one
92
factor often influences another. For this reason, model calibration is most efficient when it
follows a systematic process and relies as much as possible on the best available information
which may be measured, observed, or empirically or numerically derived. However, in
calibrating the model, the user also needs to consider that the mathematics in LaModel are only a
simplified approximation of the true mechanical response of the overburden. Because of the
mathematical simplifications built into the program, the input parameters may need to be
appropriately adjusted to account for the program limitations.
Model Development. The major effort of the back-analysis was directed toward selecting the
critical rock mass, gob and coal properties to provide the best LaModel simulation of
documented events at Crandall Canyon Mine. Initially, the mine and overburden geometries of
the Main West area of the mine were developed into LaModel mine and overburden grids. Then,
the rock mass stiffness was selected to obtain an abutment load distribution (i.e., extent)
consistent with empirical averages and local experience. Next, the gob behavior was evaluated
to provide reasonable abutment and gob loading magnitudes. For the coal properties, the peak
strength was primarily determined from back analyzing the March 10 outburst accident in the
North Barrier section, and the strain-softening behavior was optimized from the back-analysis of
the August 6, 2007, event. Throughout this process, a number of particular locations, situations,
and conditions were used as distinct calibration points. Detailed discussions of this process are
provided in Appendix S.
Models were evaluated to select optimum input values for matching the observed mine behavior
and to assess the sensitivity of the model results to the input values. These analyses provided a
broad understanding of factors that affected ground conditions at Crandall Canyon Mine and
culminated in the development of a model that simulates:
• the March 2007 bursts,
• the South Barrier section development, and
• the August 6 collapse.
In this model, mine workings were represented in a grid of 10 x 10-foot elements that measured
570 elements wide by 390 elements high. A separate grid was developed to incorporate the
influence of topography in the model. Lamination thickness was set at 500 feet, the final
modulus of the north gob was set at 250,000 psi, and the final modulus of the southern gob was
set at 200,000 psi. The coal strength in the North and South Barrier sections was set at 1,300 psi
and coal strength in the Main West was set at 1,400 psi. For the strain softening coal behavior,
the residual stress was set with a 30% reduction from the peak stress. The safety factors
presented were adjusted so that the peak pillar strength in the North Barrier pillars corresponded
to a safety factor of 1.0. This same adjustment was made to all pillar safety factor plots shown.
The model grid boundaries and calculated in situ overburden stress (i.e., stress levels due to
overburden alone and without any influence of mining) are illustrated in Figure 53.
93
Figure 53 - LaModel Grid Boundaries and Overburden Stress
LaModel Results. The results from the optimum calibrated model for Crandall Canyon Mine
are shown in Figure 54 and Figure 55. In these figures, “cooler” colors (green and blue)
correspond to safety factors greater than 1.0. “Hotter” colors (yellow, orange, and red)
correspond to safety factors less than 1.0 and, therefore, represent pillar failure. It is important to
note that LaModel does not calculate any of the details of the coal or overburden failure
mechanics. Since the program does not have any dynamic capabilities, it cannot distinguish
between a gentle controlled pillar failure and a violent pillar burst. However, coal that bursts
must be at, or very near, its ultimate strength at the time of the burst; therefore, it is reasonable in
bump prone ground to associate the point of coal failure in LaModel simulations with coal
bursts.
In Figure 54A, model results correlate reasonably well with conditions observed after the March
2007 bursts. For example, failure in the North Barrier section correlates well with observed
damage. In this illustration, only one pillar appears to have failed in the Main West at the time
of the burst. Figure 54B shows the development and retreat to crosscut 142 of the South Barrier
section. In this illustration, safety factors for pillars in the South Barrier section remain above
1.0, although 42 pillars have failed in the Main West. Figure 55 demonstrates the catastrophic
pillar failure propagation consistent with the August 6 collapse. In this simulation, 106
additional pillars fail in the Main West and 59 pillars fail in the South Barrier section. The failed
area extends from crosscut 123 in the South Barrier section inby to crosscut 146 in the bleeder
area. This optimum model simulates most of the critical observations of ground behavior at the
Crandall Canyon Mine reasonably well.
94
Figure 54 - Optimum Model Before and After South Barrier Section Mining
Figure 55 - Optimum Model after August 6 Failure
In all of these models, once the coal strength was calibrated to the March 10, 2007, North Barrier
section outburst, results indicate that the pillars in the Main West were also close to failure.
Once the South Barrier was subsequently developed, the model showed that it was very likely for
the entire Main West and South Barrier entries to collapse upon the South Barrier development,
or just a small perturbation was needed to initiate the collapse.
Modeling demonstrates that several actions could have triggered the collapse. Results
demonstrate that if material properties and loading conditions are exactly uniform throughout the
Main West area, then some stimulus is required to trigger the event with the mine configuration
present on August 6. In the simulation depicted in Figure 55, for example, six pillars within the
sealed area in Main West were simulated as having been mined and replaced with gob material
to act as a triggering mechanism. This action simulates the possibility that isolated pillar failures
(e.g., due to degradation over time and in the presence of abutment stress) initiated a collapse
which swept through the Main West pillars and down through the South Barrier section.
95
Similarly, a sudden change in stresses due to slip along a joint in the roof within the collapse area
could have been a factor in triggering the collapse. Model results also indicate that if the
properties and loading conditions are not uniform (a reasonable geologic assumption), the event
may have been triggered by pillar recovery in the active mining section.
Conclusions. An extensive back-analysis of events at Crandall Canyon Mine using the
LaModel program suggests that the August 6 collapse resulted from the failure of a large area of
similar size pillars. Pillars in the North Barrier section and Main West are nearly the same size
and strength. Also, the barrier pillars between the Main West and the North and South Barrier
sections have a comparable strength (within 15%) to the pillars in the Main West and barrier
sections. The pillars in the South Barrier section were stronger than the pillars in the North
Barrier section and Main West, but only by about 16%. Once a failure initiated, the surrounding
similar strength pillars were likely to fail in domino fashion.
An imminent failure situation was created when pillars adequately sized for development mining
were subjected to additional stress associated with retreat mining (longwall and pillar recovery).
Development pillar safety factors below 1.4 indicate that high overburden (approximately
2,200 feet) caused considerable development stress on the pillars in the middle of the Main West,
North Barrier, and South Barrier sections. Abutment stresses associated with longwall mining
north and south of the Main West contributed to even lower safety factors. Overall, the area was
primed for collapse because equal size pillars in a large area were already near failure.
Boundary element modeling alone cannot distinguish between the factors or combination of
factors that may have triggered the August 6 collapse. If conditions are assumed to be exactly
uniform throughout the Main West area, modeling suggests that some stimulus such as pillar
degradation in the sealed area or joint slip in the collapse area was required to trigger the
collapse. However, the modeling also demonstrates that if material properties or loading
conditions are not uniform, then the active mining may have triggered the collapse.
Initially, Dr. Heasley modeled the Main West using coal and gob with identical properties.
However, with this approach, he noted that the pillars in the Main West seemed to fail too soon
(or too easy) while the pillars in the South Barrier section seemed to resist failure. Results were
determined to be more consistent with known conditions when coal properties and applied load
(adjusted through changes in gob property) were not uniform in the model.
Boundary Element Analyses of GRI Mining
Separate boundary element analyses were conducted by MSHA as part of the accident
investigation in order to gauge the effects of three separate actions taken by GRI in the South
Barrier:
• The barrier between crosscut 139 and 142 was mined even though this activity was
prohibited by the approved roof control plan.
• Bottom coal was mined from pillars and the barrier even though this activity was not
addressed in the approved roof control plan.
• The widths of the barrier pillars north and south of the South Barrier section were
inconsistent with the widths evaluated by AAI.
Each of these actions had implications on ground stability during the development and recovery
of pillars in the South Barrier section. BEM models were used to assess the degree to which
GRI’s actions may have contributed to the August 6 accident. Dr. Heasley’s calibrated model
was used as the basis for each analysis but some modifications were required to generate data for
96
comparison (e.g., grids were changed to reflect conditions with and without barrier mining).
Modifications required for the three analyses are discussed individually in the following sections.
Effect of Barrier Mining. Dr. Heasley’s boundary element model was developed using the best
available information to back-analyze the August 6, 2007, accident. In this model, the barrier
pillar south of the No. 1 entry was considered to have been mined by taking 40-foot deep cuts
between crosscuts 139 and 142. The accident investigation team modified Dr. Heasley’s model
by incorporating an additional model step. This step simulated a condition in which the barrier
was not mined in this area and provided a basis for comparison of model results (i.e., with and
without barrier mining).
The impact of barrier mining was evaluated by observing the distribution of vertical stress in the
vicinity of the August 6 mining location. Vertical stresses were determined for the section
before and after mining the barrier (see Figure 56). As discussed in the Main West Ground
Control History section of this report, eight pillars and the adjacent barrier between crosscuts 139
and 142 were to remain unmined to protect the bleeder entry where it jogged around a sump in
the Main West workings. The pillars were not mined but the barrier to the south was mined.
Model results indicate that stress levels increased substantially in the pillars adjacent to the sump
and were highest in the remnant barrier near the location where the South Barrier section crew
was working at the time of the August 6 accident. These stress levels are similar in magnitude to
those in the remnant barrier pillar inby crosscut 142 before barrier mining.
Stress redistribution associated with barrier mining occurred over a relatively broad area but
diminished with distance from the extracted area. Vertical stress changes throughout the model
can be determined by subtracting model results in the grid representing an intact barrier (Figure
56, top) from those in the grid that includes barrier mining (Figure 56, bottom). Negative values
reflect stress decreases that result from either element removal (i.e., simulated mining) or
yielding. Positive values represent stress increases.
16000
14400
136
139
142
145
12800
11200
9600
8000
6400
4800
3200
1600
0
Vertical
Stress,
psi
136
139
142
145
Barrier Mining
Figure 56 - Distribution of Vertical Stress in the South Barrier Section
97
The magnitude and distribution of increased vertical stress in the vicinity of the Main West sump
are illustrated in Figure 57. Model results indicate that the highest increases (over 4,000 psi)
occurred in the remnant barrier and adjacent pillars and decreased substantially within a
relatively short distance. Stress increased in the Main West and outby in the South Barrier.
However, it is important to note that the vertical stress scale in Figure 57 has been expanded in
the interval from 0 to 500 psi to provide more detail in this range. Modeled stress increase was
less than 200 psi within five crosscuts (~500 feet) of crosscut 139. Also, it should be noted that
these values represent increases in individual elements rather than in average pillar stress.
4000
3000
2000
Barrier Mining
500
400
136
139
145
142
1000
300
200
100
0.01
0
Figure 57 - Vertical Stress Increases due to Barrier Mining
As illustrated in Figure 58, average pillar stress decreased in the pillars immediately adjacent to
the barrier mining. However, pillar yielding that caused these decreases contributed to load
transfer and increased stress levels in adjacent pillars. Stress increases were largest in the
vicinity of the bleeder entry. For example, model results indicate that vertical stress increased by
24% in a portion of the barrier adjacent to the Main West sump. The approved roof control plan
excluded mining the barrier between crosscut 139 and 142 explicitly to protect the bleeder entry
in this area. Model results indicate that mining in this area likely jeopardized the stability of the
bleeder system inby crosscut 139. This activity also increased stress levels in the remnant barrier
and pillars near the location where the South Barrier section crew was working at the time of the
August 6 accident.
4%
1%
0%
0
0
6%
2 00
2 00
7%
1 60
1 60
24%
15%
10%
5%
1%
DECREASE
6%
8%
4%
1%
1%
DECREASE
0
0
4%
DECREASE
DECREASE
2%
1%
1%
Figure 58 - Effect of Barrier Mining on Average Pillar Stress
98
Steps were added to Dr. Heasley’s model to simulate the planned pillar recovery outby crosscut
139 (with the barrier intact between crosscuts 139 and 142). Pillar safety factors associated with
pillar extraction in the rows between crosscuts 139 and 136 are shown in Figure 59. These
results indicate that even if the barrier had not been mined between crosscuts 139 and 142, pillars
in the South Barrier section likely would have failed if pillar mining continued in the next several
pillar rows. After one row of pillars is recovered, pillar SF’s are still above 1.0 as indicated by
the blue and green colors in Figure 59A. When the next row of pillars is recovered (Figure 59B),
failure occurs near the pillar line (yellow and orange) and with recovery of the third row, failure
propagates outby over a broad area as indicated by the red and orange colors in Figure 59C.
A
2.0
1.8
B
1.6
1.4
1.2
1.0
0.8
0.6
0.4
C
0.2
0
Figure 59 - Pillar Safety Factors for Pillar Recovery Outby Crosscut 139
Effect of Bottom Mining. Dr. Heasley’s boundary element model was also modified to evaluate
the effects of bottom mining during pillar recovery inby crosscut 139 in the South Barrier
section. Bottom mining refers to the recovery of coal that remains in the floor after development
mining particularly in thick seams. In the western area of the South Barrier section, up to 5 feet
or more of bottom coal remained after development. The continuous mining machine ramped
into the floor to remove this coal as pillars and barriers were recovered, even though this had not
been considered by AAI in the mine design. Bottom coal was not removed from the entries and
crosscuts, except when grading heaved bottom to maintain clearance for mining equipment.
Bottom mining creates taller pillars, which are generally weaker than shorter pillars of the same
length and width. In the South Barrier section, the affected areas were the remnant pillars and
the 80-foot wide remnant barrier labeled A and B, respectively, in Figure 60. Bottom mining in
the pillars affected pillar stability as mining proceeded within each row. However, once a row
99
was completed, this effect was negated as the roof was intended to collapse after mining was
completed.
LW
120 ft Barrier
No. 1
No. 3
No. 2
No. 4
Main West South Barrier section after development
Taller Pillar from
Ramping into Floor
B
80 ft Remnant Barrier
No. 1
A
Bleeder
No. 3
No. 2
No. 4
Main West South Barrier section after pillar recovery in the No. 1 entry
Taller Pillar from Ramping into Floor
B
A
80 ft Remnant Barrier
No. 1
No. 2
Bleeder
No. 3
No. 4
Main West South Barrier section after pillar recovery in the No. 1 and 2 entries
B
Taller Pillar from Ramping into Floor
Bleeder
80 ft Remnant Barrier
No. 1
No. 2
No. 3
No. 4
Main West South Barrier section after pillar recovery in the No. 1, 2 and 3 entries
Figure 60 - Cross-Section through South Barrier Section during Pillar Recovery
As illustrated in Figure 61, the partial pillar between No. 1 and No. 2 entry separates the mining
crew from the caved area. The stability of the work area relies largely on the stability of the
partial pillar, particularly as mining progresses outby to the intersection. Bottom mining on the
gob side of this pillar increases the pillar height and effectively reduces its strength. A similar
situation occurs when mining moves to the No. 3 entry. Thus, bottom mining can impact local
stability even though the pillars are intentionally being reduced in size and the roof is expected to
collapse. Also, bottom mining adjacent to the remnant barrier weakened the remnant barrier
inby the pillar line and contributed to overall instability of the section as it retreated.
100
Barrier Slab Cuts
Bleeder Entry
No. 4 Entry
No. 3 Entry
Mining in No. 2 Entry
X’
No. 2 Entry
Barrier Pillar
No. 1 Entry
X
Partial Pillar (A)
Caved Area
Mined Pillar
Remnant
Barrier
Plan view
A
No. 1
Entry
13 ft mined
height
No. 2
Entry
Cross-section X to X’
Figure 61 - Effect of Bottom Mining on Pillar Geometry
(e.g. inby crosscut 142)
Dr. Heasley’s model was modified to evaluate the impact of bottom mining. As illustrated in
Figure 62, one half of the remnant barrier was modeled using coal properties developed for a
mining height of 8 feet, while the other half used a weaker coal strength and lower stiffness
based on a mining height of 13 feet. Simulations with and without bottom mining were
compared to measure the relative impact of the activity.
101
B
8 ft mined
height
80 ft Wide Remnant Barrier
13 ft mined
height
B
Element properties
Based on 8 ft mined
height
Element properties
Based on 13 ft mined
height
Figure 62 - Model Representation of Bottom Mining in the Remnant Barrier
The impact of bottom mining in the barrier was evaluated by assessing vertical stress levels and
element safety factors in the vicinity of the August 6 mining location. The distributions of
vertical stress with and without bottom mining are presented in Figure 63.
16000
14400
12800
without bottom mining
11200
9600
8000
6400
4800
3200
1600
0
Vertical
Stress,
psi
with bottom mining
Figure 63 - Distribution of Vertical Stress in the South Barrier Section
102
Although there are subtle differences over a broad area, the primary impact of bottom mining is
seen in the remnant barrier. The core of the 80-foot wide remnant barrier has a higher peak and
residual strength (Figure 63 top) when bottom mining is not conducted. With bottom mining,
load that otherwise may have been supported by the barrier is redistributed to other elements.
Stress redistribution was examined by subtracting model results in the two model grids shown in
Figure 63. Negative values reflect stress decreases that result from lower element strength
and/or yielding. Positive values represent stress increases. Since no additional mining was
simulated, decreases between the models demonstrate the stress redistribution between elements.
In effect, Figure 64 shows where stress increased and decreased as a result of bottom mining.
3000
2000
1000
200
0
0
Vertical
Stress
Change,
psi
-200
-1000
-3500
-7000
Figure 64 - Differences in Vertical Stress due to Bottom Mining
The element safety factors from the model results indicate that the remnant barrier would have
failed even if the bottom coal had not been mined (Figure 65). Element stability factors below
1.0 in Figure 65 indicate that the peak strength of elements was exceeded across the entire width
of the barrier even though the modeled mining height was 8 feet. The primary effect of bottom
mining inby the pillar line was to weaken an already undersized remnant barrier. Bottom mining
in the barrier cuts between crosscuts 139 and 142 weakened the barrier near the last known
location of the miners and, consequently, contributed to increased stress levels.
Variation in Barrier Width from Design to Implementation. The South Barrier section was
developed with four entries on 80-foot centers and crosscuts on 130-foot centers. AAI had
evaluated this pillar system using both ARMPS and LaModel. However, their analyses
considered system stability with a 55-foot wide barrier north of the section and a 135-foot wide
barrier to the south. When the South Barrier section was developed, barrier widths were actually
75 feet (55 feet minimum from the Main West notches) and 121 feet, respectively. Dr. Heasley’s
calibrated Crandall Canyon Mine model was modified and rerun to consider the effects of
varying barrier widths. Since the model uses 10-foot wide elements, the “as designed” barriers
were represented as being 60 and 140 feet wide to the north and south, respectively. The “as
mined” model used 80 and 120-foot wide barriers to the north and south, respectively. With the
exception of these grid modifications, the two models were identical to one another.
103
2.0
1.8
without bottom mining
1.6
1.4
1.2
1.0
0.8
0.6
0.4
0.2
0
Element
Safety
Factor
with bottom mining
Figure 65 - Element Safety Factors
Figure 66 illustrates pillar safety factors calculated for the Main West region as it was actually
developed and recovered prior to the August 6 accident. These model results are consistent with
Dr. Heasley’s results that show some pillar failure in the sealed portion of Main West but stable
pillars in the section after development and after the pillar recovery prior to the August 6
accident. Although broad pillar failure can be triggered by one of several mechanisms, the
model demonstrates a general reluctance for the Main West failure to propagate south past the
104
75-foot wide barrier pillar (modeled as 80 feet wide) and into the South Barrier Section. In
contrast, when the north side barrier width is reduced to 55 feet (modeled as 60 feet), Main West
pillar failure propagates southward into the section during development mining.
2.0
1.8
1.6
1.4
1.2
1.0
0.8
0.6
0.4
0.2
0
Pillar
Safety
Factor
Figure 66 – Pillar Safety Factors Modeled with a 120-foot Southern Barrier
Figure 67 illustrates pillar safety factors for three model steps that represent development mining
in the South Barrier section modeled with a 60-foot north side and a 140-foot south side barrier.
In Figure 67A, pillars in the South Barrier section are stable as indicated by the blue colors. In
Figure 67B, one additional crosscut has been developed. The South Barrier section remains
stable but several additional pillar failures are noted in the Main West. In Figure 67C, another
crosscut has been developed and failure is widespread throughout the South Barrier section as
noted by the yellow and orange colors. A wider barrier south of the section (137-foot versus the
121-foot actually mined) may have decreased the likelihood of failure from Panel 13 longwall
extraction abutment stress. However, model results suggest that pillar failure may have occurred
in the section during development as a result of the corresponding reduction of barrier width to
the north (55 feet initially planned versus 75 feet as mined measured outside the Main West
notches).
105
A
2.0
1.8
1.6
1.4
1.2
B
1.0
0.8
0.6
0.4
0.2
0
Pillar
Safety
Factor
C
Figure 67 – Pillar Safety Factors Modeled with a 140-foot Southern Barrier for Development Mining
Skipping Pillars during South Barrier Retreat. After the March 10 non-injury coal outburst
accident in the North Barrier section, AAI and the mine operator concluded that the method of
mining in that area had contributed to the event. Pillar recovery had been discontinued at
crosscut 137 and resumed outby between crosscuts 134 and 135 (i.e., pillars were “skipped”).
When the March 10 accident occurred, several pillars had been removed outby crosscut 135 but
good caving conditions had not been established. Hanging, cantilevered strata inby the new
pillar line were thought to have caused additional loading on the surrounding pillars. Thus, AAI
and GRI attributed the event in part to the operator’s decision to reestablish the pillar line under
deep cover and in the abutment zone of the original pillar line and, to a lesser extent, the
abutment load from the Panel 12 longwall gob to the north. As a result, AAI cautioned against
skipping pillars in the South Barrier.
Although the mine operator skipped pillars between crosscuts 139 and 142 in the South Barrier
section, this decision did not contribute to the August 6 accident. The North Barrier section burst
experience raised concerns with abutment stress as a pillar line was reestablished. However, the
South Barrier section scenario is distinctly different and similar stress conditions were not
present for several reasons:
•
First, on August 6, a new pillar line had not yet been created. Mining was limited to the
barrier pillar south of the No.1 entry; no pillars had been recovered. Thus, the amount of
potentially cantilevered strata created by the barrier cuts and available to generate
additional abutment load was minimal.
106
•
Second, the August 6 mining location was about 400 feet outby the last South Barrier
pillar line. At this distance, abutment stress from the active gob would also be minimal.
•
Finally, overburden was 1,760 feet versus more than 2,000 feet in the area affected by the
North Barrier outburst accident. AAI recommended against skipping pillars “particularly
under the deepest cover.” In February 2008, AAI indicated that “the deepest cover”
could apply to the ridge crest over the area (2,000 to 2,200 feet) or may be interpreted
more broadly (e.g., 1,800 to 1,900 ft). AAI stated that GRI did not seek clarification of
this term.
The skipped pillars between crosscuts 139 and 142 in the South Barrier section did not cause or
compound the pillar collapse that occurred on August 6. Conversely, these pillars likely reduced
the severity of the event in the vicinity of the working section.
Summary - Analyses of Collapse
Three types of analyses were conducted to evaluate ground behavior at Crandall Canyon Mine.
Although the approaches are substantially different, the results and conclusions are similar.
•
ARMPS stability factors below NIOSH’s recommended minimums do not necessarily
ensure failure. However, stability factors for the North Barrier section were below
recommended values and lower than any previous experience at the mine. GRI
abandoned the North Barrier section due to difficult ground conditions and bursts, yet
they employed a design with still lower stability factors in the South Barrier section.
•
ARMPS is not directly capable of evaluating the exact geometry of the entire area
affected by the August 6 collapse. However, if the effects of longwall mining are
neglected entirely, ARMPS provides insight to overall Main West stability. This
approach demonstrates that the Main West pillar stability is below NIOSH
recommendations even without the additional influence of longwall abutment stress.
•
Despite the use of optimistic input values (e.g., consideration of development mining
only), FEM model results indicate the strong potential for a rapid catastrophic failure of
the North and South Barrier sections and the Main West pillars between them.
•
BEM analyses confirm that the Main West was vulnerable to wide-spread failure because
a large area of pillars was developed with marginal safety factors and similar strength
barrier pillars. Analyses indicate that one or more events or conditions may have been
the trigger which actually initiated the pillar failure. However, model results are more
consistent with known conditions at the accident site when coal properties and applied
load (adjusted through changes in gob property) are not uniform in the model.
All of the analyses conducted as part of this accident investigation indicate that the mining plan
employed to extract barriers on either side of the Main West was inadequate to maintain stability
during pillar recovery. The design created a large area of similar sized and marginally stable
pillars. When one pillar or group of pillars failed, the rest were destined to fail in domino
fashion.
Seismic analyses and subsidence information developed in the accident investigation indicate
that the collapse initiated near the South Barrier section pillar line and the greatest surface
displacements were located 500 feet outby the last known location of the miners. These
observations suggest that loading conditions were more extreme near the working face and
provide further clarification that the collapse was most likely initiated by the mining activity.
107
Critique of Mine Design
The engineering analyses discussed in the previous sections demonstrate that the August 6, 2007,
accident was caused by the rapid collapse of a large area of pillars. Overburden in excess of
2,000 feet and abutment stresses from adjacent mined-out longwall panels and active pillar
recovery combined to create a high stress environment that the pillar system was incapable of
supporting. Initially both GRI and MSHA recognized the potential for high stress. Although
recent pillar recovery operations had been conducted in the South Mains without the assistance
of a ground control consultant, GRI retained these services for the design of the North and South
Barrier sections. Similarly, previous pillar recovery operations had been conducted at the mine
under the existing roof control plan without the benefit of site-specific provisions. For the North
and South Barrier sections, MSHA required such site-specific plans for both development and
pillar recovery.
GRI implemented and MSHA approved a mine design based largely on the results of engineering
analyses performed by AAI. These analyses used two of the approaches discussed in the
previous section of this report, ARMPS and LaModel. AAI generated an overburden map for
these analyses, which was determined to be accurate by comparing it to the overburden map
independently generated by the MSHA accident investigation team. AAI’s analyses concluded
that proposed pillars should function adequately for short-term mining in the North Barrier.
After this design failed, AAI modified the design. Their further analyses indicated that pillar
dimensions proposed for South Barrier mining would “provide a reliable level of protection
against problematic bumping for retreat mining under cover reaching 2,200 feet.” However,
pillar recovery operations had retreated beneath overburden of only about 1,640 feet at crosscut
142 (barrier slabbing to 1,760 feet at crosscut 139) when the August 6 collapse occurred.
While mining in the South Barrier section, GRI deviated from the design analyzed by AAI and
the approved roof control plan (e.g., GRI mined bottom coal, varied the barrier pillar dimensions,
and mined the barrier between crosscuts 139 and 142). These actions affected barrier pillar
strength and pillar stress levels in the vicinity of the last known location of the miners. They
were also part of the active pillar recovery operations the cumulative effect of which was the
August 6 collapse. However, the Main West and adjacent North and South Barrier sections were
primed for a catastrophic pillar failure independent of these activities because the mine design
created a large area of equal size and marginally stable (near unity safety factors) pillars. This
failure mechanism was not apparent in the results of some of the AAI analyses conducted prior
to the accident because overly optimistic design assumptions and/or inappropriate input
parameters or procedures were used. Other analyses were done properly but results indicative of
failure were either misinterpreted or were not acted upon.
Previous Ground Control Studies at Crandall Canyon Mine
Prior to mining in the North and South Barrier sections, GRI contracted AAI to evaluate ground
conditions and entry stability associated with GRI’s plan for room and pillar mining in the
barriers. AAI’s proposal for this work indicated that “Concern exists for potentially high stress
conditions caused by a combination of deep cover and side-abutment loads from the adjacent
longwall gobs, and, to a lesser extent, load transferred onto the barriers by time dependent pillar
convergence in Main West.” To evaluate these concerns, AAI elected to use a numerical model
to assess vertical stress, convergence, and pillar yielding (see Appendix F).
GRI had used AAI’s services on several occasions prior to the analysis of Main West. AAI had
developed numerical models of ground behavior at Crandall Canyon Mine prior to 1996. These
108
models were used to make preliminary evaluations of pillar design configurations, even though
at that time model accuracy could not be verified.
Between June 1995 and January 1996, Neil & Associates (NAA) conducted field studies in the
6th Right yield-abutment longwall pillars at the mine. Subsequently, GRI contracted AAI to
refine the model for Crandall Canyon Mine using the now available field data. AAI’s calibration
to the 6th Right data in 1997 improved their confidence in accurately representing ground
behavior at the mine.
AAI developed the calibrated model of Crandall Canyon Mine ground behavior using a
boundary element computer code called EXPAREA (see Appendix R). This software and the
calibrated model were used in 2000 to evaluate the effect of barrier pillar width on future bleeder
entry stability. The mine location modeled in this study (bleeder entries west of Panel 15) was
less than 2,500 feet from the Main West South Barrier and several aspects of the study (e.g.
evaluations of abutment load distribution) were relevant to the subsequent Main West South
Barrier study (see Appendix E).
Barrier Pillar Design
In coal mining, the term barrier pillar refers to a block of coal left in place to isolate or protect
mine structures from potentially harmful interactions. For example, barriers could be required to
isolate workings in adjacent properties from one another or to separate active and abandoned
workings within the same mine. In these contexts, barriers function primarily to prevent an
influx of impounded water or gasses. However, in retreat mining applications (both pillar
recovery and longwall), barrier pillars typically are used to protect mine workings from high
vertical stress concentrations near the boundaries of extracted areas often referred to as gobs.
A variety of rules of thumb, mathematical formulas, and design methods have been developed to
establish minimum widths of barrier pillars. A USBM publication 8 summarizes nine of these
approaches and provides an overview of performance evaluation techniques that can be used to
optimize barriers. Each of the nine formulas is included in Table 9 even though some of them
were developed especially for water impoundment. The formula names indicated by bold font
are applicable to barriers used in longwall and pillar recovery operations.
Table 9 also includes a minimum barrier width corresponding to each barrier design equation.
Input parameters used to generate these results are pertinent to the Crandall Canyon Mine
accident site. For example, an 8-foot mining height, 2,160 feet maximum overburden, and
800-foot panel width were used. A maximum convergence value of 3.7 inches was used in the
Holland Convergence Method. Using the six bolded equations in Table 9, these parameters
generate minimum barrier pillar widths ranging from 202 to 384 feet.
AAI had considered four of these equations in a 2000 project which evaluated the effects of
barrier pillar widths on future bleeder entry stability for Panel 15, south of Main West (see
Appendix E). Results of AAI’s analyses in that study are illustrated in Figure 68 ‡. AAI stated
that this figure “gives a summary of recommended barrier pillar widths by various empirical
‡
Calculated values in Table 9 and Figure 68 are dissimilar because input values (e.g. mined
height and overburden depth) vary between the two scenarios.
109
methods. The design widths shown here might be helpful as an additional source on which to
base decisions. For a depth of 1000 ft, all the methods support a barrier pillar of 260 ft or less.
At 1500 ft of cover, three of four methods suggest a barrier pillar of less than 260 ft.” AAI
refers to this work as an “additional source” since it was presented as confirmation of the
conclusions drawn from numerical models.
Table 9 - Barrier Pillar Design Formulas
Name
Formula
Barrier Width (ft)
under 2,160 ft
overburden
1
Dunn’s Rule
W =
( D − 180)
+ 15
20
114
2
Old English Barrier Pillar
Law
W=
(H × T )
+ 5T
100
212
3
Pennsylvania Mine
Inspector’s Formula
W = 20 + 4T + 0.1D
268
4
Ash and Eaton Impoundment
Formula
W = 50 + 0.426 D
970
5
Pressure Arch Method
6
British Coal Rule of
Thumb
7
North American Method
8
Holland Rule of Thumb
9
⎛D
⎞
W 〉 A = 3 ⎜ + 20 ⎟
⎝ 20
⎠
⎛D⎞
W = ⎜ ⎟ + 45
⎝ 10 ⎠
W=
( D × P)
7000 − D
D
+ 105
22.2
5 (log 50.8C )
W =
+ 15
( E log e)
W=
384
261
357
202
Holland Convergence
Method
290
where:
W = barrier pillar width, ft
D = depth of mining (or height of hydrostatic head in #3 above), ft
H = hydrostatic head or depth below drainage (ft)
T = coal seam thickness (ft)
A = minimum width of the maximum pressure arch, ft
P = width of adjacent panel, ft
C = estimated convergence on high-stress side of barrier pillar, in
E = coefficient of extraction adjacent to barrier (E = 0.09 for complete caving)
AAI used numerical models in their 2006 studies of Main West barrier development and pillar
recovery. Despite the relatively close proximity and similar study objectives, results of the 2000
and 2006 model studies differ substantially. These numerical analyses will be discussed in detail
in a later section of this report. The 2006 results also conflict with output from the empirical
formulas in Table 9. Unlike, the 2000 study, AAI did not use barrier pillar formulas to confirm
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the 2006 model results. One of a series of written questions posed to AAI during the accident
investigation addressed the use of barrier pillar equations:
AAI designed barriers for longwall panels at Crandall Canyon and it appears that
several methods were used to estimate barrier widths (North American method,
Holland Rule of Thumb, Holland Convergence method, PA Mine Inspectors
formula). How were these formulas considered when evaluating mining in the
existing barriers or why were they not considered?
AAI responded, “These methods are limited to cover less than 2,000 ft.”
Figure 68 - Barrier Pillar Sizes from Empirical Methods
Figure 4 in AAI’s May 5, 2000, Report
As indicated in Figure 68, AAI had previously used the North American method to determine
barrier width in overburden depths up to 2,500 feet. This method is the only one of the four that
accounts for the width of the adjacent panel in determining the barrier width. AAI’s results in
Figure 68 were based on using two longwall panel widths (~1,560 feet) and, even at lower depths
of cover, this method recommends wider barrier widths than the other three methods. This is a
reasonable assumption, given the caving characteristics of strata in the Wasatch Plateau (i.e.,
maximum subsidence may not be achieved with the extraction of a single panel – see Appendix
L). However, if one panel width is used (~800 feet), the calculated barrier widths are much more
consistent with the other methods (i.e., 130 feet wide at 1,000 feet of overburden, 210 feet wide
at 1,500 feet of overburden, 310 feet wide at 2,000 feet of overburden, and 430 feet wide at
2,500 feet of overburden). As indicated in Table 9, the recommended barrier width using this
approach is 357 feet for 2,160 feet of overburden (the depth at which pillar recovery was
abandoned in the North Barrier section). Although this approach generates a narrower barrier
width than what AAI had calculated in 2000, the recommended width is still nearly three times
larger than the 130-foot width determined through numerical modeling in AAI’s 2006 studies.
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Also, the 130-foot dimension is approximately half the width that the barrier design equations
would recommend for a depth of 2,000 feet. This is significant since about 25% of the Main
West North and South Barriers have overburden exceeding 2,000 feet. Whereas the numerical
model results for barrier design in the May 2000 study were consistent with empirical design
equations, the 2006 results were not.
AAI did not consider the empirical equations in 2006 because they considered them less relevant
to the North and South Barrier mining scenarios. Similarly, they discounted the relevance of the
May 2000 study since it addressed barriers to protect a two-entry bleeder system (i.e., to limit the
effects of longwall mining-induced stresses) rather than a pillar recovery section. However, a
comparison to either of these results would have indicated that AAI’s 2006 model results were
flawed. AAI’s report on the 2000 barrier design project concludes that “To minimize any
potential for stress overloading resulting from panel mining, or to minimize maintenance and to
provide long term stability (greater than three years), a barrier pillar of 400 ft would be
required.” Regardless of the relevance of the scenario, this conclusion contradicts the 2006
conclusion that “For the current geometry, stress levels taper to near pre-mining (in situ) stress
levels approximately 100 ft into the barrier, indicating that the proposed 130-ft-wide barrier will
limit exposure of the planned entries and pillars to most of the abutment.”
Abutment stresses are transferred from extracted areas to adjacent workings (see Figure 35). The
stresses are highest near pillared areas (referred to as “gob”) and diminish with distance. Rules
of thumb used to estimate abutment stress transfer distance are discussed in Appendix T.
However, longer transfer distances have been observed in some mines in the Wasatch Plateau.
In a paper titled “Long load transfer distances at the Deer Creek Mine,” Goodrich et al. 9 wrote:
Load transfer distances at the Deer Creek mine (including other mines in the
Wasatch and Book Cliff Coal Fields) have been generally greater than predicted
using empirical design methods (Koehler & Tadolini 19958, Abel 1988 10,
Barrientos & Parker 1974 11). The long load transfer distances observed in the
case of the 5th and 4th West panels is believed to be due to the strong and stiff
sandstone/siltstone strata in the overburden, including the Upper Blackhawk
strata and the Castlegate Sandstone.”
Similar long abutment stress transfer distances are implicit in a discussion of barrier sizing in a
paper titled “Interpanel Barriers for Deep Western U.S. Longwall Mining 12.” Although
numerical models described in the paper address a longwall mining scenario, they demonstrate
that wide barriers (e.g., 390 feet wide at depths of 2,600 feet) are required between panels to
minimize abutment stress override. Cantilevered or overhanging strata are typically associated
with high abutment stresses. The authors state that “Overhanging is likely in the Wasatch
Plateau-Book Cliffs coal fields given the abundance of massive overburden strata, such as the
Castlegate Sandstone.”
The authors or coauthors of each of the aforementioned papers were employees of AAI when the
papers were written. Since the Upper Blackhawk and Castlegate sandstone units (see Figure 23)
discussed in these papers are present at Crandall Canyon Mine, AAI’s institutional knowledge
should have indicated that the short abutment load transfer distance from the model results was
not accurate. Similarly, since interpanel barriers are used at another UEI mine in the area, GRI
also had pertinent institutional knowledge.
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Agapito Associates, Inc. Analyses
AAI used LaModel to analyze room and pillar workings in the North Barrier section. The initial
analyses focused on development mining in the area and calibration of the model to historical
conditions in the 1st North pillar panels, which were developed in a herringbone pattern and
retreated using a continuous haulage system. Results of this work were reported in a
July 20, 2006, draft letter report to Laine Adair (see Appendix F). AAI concluded that the
section design should function adequately for short-term mining in the barriers. Model results
indicated that side-abutment stress from the adjacent longwall would be limited in extent (about
130 feet) and, thus, stress conditions would be controlled by the depth of cover and not by
abutment loads.
AAI subsequently was contracted to do additional LaModel analyses to evaluate pillar recovery
in the North Barrier section. These results were reported in an email dated August 9, 2006, from
Leo Gilbride to Laine Adair (see Appendix G). In this instance, ARMPS was used to
supplement the LaModel analysis. AAI reported that “Conclusions from LAMODEL
corroborate the ARMPS results, principally that convergence can be adequately controlled with
the proposed mine plan and that ground conditions should be generally good on retreat in the
barriers, even under the deepest cover (2,200 ft ).”
AAI concluded that the ground conditions they observed on December 1, 2006, agreed with their
analytical predictions (i.e., LaModel results). However, the predictions themselves were
inaccurate and misleading. Both the LaModel and ARMPS analyses used either inappropriate
input values or an overly optimistic design approach that negatively affected the reliability of the
results, as discussed below.
Boundary Element Modeling. The July 20, 2006, report prepared by AAI describes the
procedures used to develop a numerical model for mining in the North Barrier section. The
report also includes two tables that list input parameters that were used in the final, “calibrated”
model. The first table lists coal material properties developed using equations included in the
report. The second table lists additional parameters that reportedly were “based principally on
previous modeling studies for the Crandall Canyon Mine.” However, examination of the actual
LaModel input files demonstrates that many of the input parameters were much different than
those shown in the report and were not consistent with those used in previous Crandall Canyon
Mine models.
Coal Properties. AAI used both strain softening and elastic coal properties in their Crandall
Canyon Mine models. Strain softening implies that an element of coal will carry increasing
loads up to a peak value before it then fails. At failure, the element loses strength and,
subsequently, it is only able to carry a lesser, “residual,” load. The methodology for using strain
softening properties described in AAI’s July 20 report is very similar to that used by MSHA
Technical Support (see Appendix U). The methodology assumes that elements farther away
from an entry will fail at progressively higher peak loads and also maintain higher residual loads.
This approach is based largely on the premise that coal strength increases with lateral
confinement and lateral confinement increases with distance from the pillar edge.
Traditionally, the effect of confinement on pillar strength has been incorporated into BEM
models by representing an individual pillar as a series of concentric rings (Figure 69A). Letter
codes are used to represent various material properties and the codes are deployed such that
material strength increases toward the pillar center. In reality, pillar corners experience less
confinement and, consequently, have lower peak strengths. The LaModel preprocessing
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program, LamPre, offers a utility to calculate coal properties to account for the weakening at
pillar corners and another to deploy them (automatic yield zone application) as illustrated in
Figure 69B. The preprocessor provides a user-friendly interface to facilitate the construction of
model grids; letter codes (material properties) can be arranged manually in any configuration.
The automatic yield zone application available in LamPre provides a convenient means of
distributing codes as illustrated in Figure 69B. However, the material properties assigned to the
letter codes must be determined specifically for this configuration (i.e., they must be calculated
to represent side and corner elements).
AAI correctly calculated coal properties as indicated in their report using the methodology
described in Appendix F. The results of these calculations are listed in Table 10. Each of the
eight sets of values listed in Table 10 corresponds to coal strengths at successively deeper
distances into the pillar on 5-foot intervals. The values were then entered manually into the
LaModel preprocessor program, LamPre. These values are consistent with a model constructed
as shown in Figure 69A. AAI entered the material properties manually and then used the
automatic yield zone application to deploy them as shown in Figure 69B. As a result, the
distribution of lettered elements used to represent the material properties was incorrect.
Table 10 - Coal Properties Calculated by AAI
A
B
Figure 69 – Plan View of Pillars showing Coal Property Elements
as Indicated in AAI Report vs. Those Actually Deployed in AAI Modeling
114
The significance of this error was that modeled pillars up to 40 feet wide appear to be much
stronger than they actually are (approximately 60% greater peak strength and 160% greater
residual strength). Furthermore, pillars over 40 feet wide contain elastic elements with no limit
on their load carrying capability. Elastic elements are infinitely strong.
Elastic elements are used routinely in boundary element models. However, Karabin and Evanto
pointed out in a 1999 publication 13, “Known or potentially yielding pillars should not contain
linear-elastic elements which could erroneously affect the stress transfer to adjacent areas.”
The implication of using elastic elements in the Crandall Canyon Mine model was that the cores
of modeled pillars in the North and South Barrier sections and in the sealed portion of the Main
West entries would never fail regardless of the applied load. Elastic conditions (unlimited
strength) is inconsistent with the known conditions discussed in AAI’s May 3, 2006, project
proposal for the Main West Barrier mining study, which stated that “time-dependent pillar
convergence existed in the sealed portion of the Main West.” The model, as constructed with the
associated rock mass and gob properties, was incapable of demonstrating pillar failure,
subsequent yielding, and stress transfer (domino failure) over a broad area.
Rock Mass Properties. One significant difference between EXPAREA, the program
originally used to develop a calibrated Crandall Canyon Mine model, (see Appendix R) and
LaModel relates to the representation of the rock above and below the seam (rock mass). In
EXPAREA and most other boundary element models, the rock mass is comprised of a single
(homogeneous elastic) unit of material. In LaModel, the rock mass is represented as a stack of
layers piled atop one another. The layered formulation used in LaModel provides an additional
parameter that can be adjusted to allow more flexible and realistic strata behavior. Rock mass
behavior in this model is controlled by both the assigned material properties and layer thickness.
In selecting parameters for the laminated rock mass in LaModel, AAI evaluated two lamination
thicknesses (25 and 50 feet). AAI concluded there was no difference between the two values and
the smaller value was selected.
In his doctoral thesis, Dr. Heasley included equations that could be used to estimate properties
that would equate the laminated strata behavior with the homogeneous rock mass used in other
boundary element programs (see Appendix V). Equating the parameters used in the calibrated
EXPAREA model to LaModel suggests that a 115-foot thickness would have been more
appropriate than the 25-foot value that AAI used. The implication of using thin laminations is
that the roof tends to sag readily into the mine openings and load the edges of the pillars.
Conversely, the rock mass is less apt to span across openings or failing pillars and transfer loads
over a longer distance.
Gob Properties. The last of the three critical components of a boundary element model is the
gob. Gob properties are extremely important in these models because they influence the amount
of abutment load transferred from a gob area to adjacent structures. However, there are few
established guidelines for selecting them. In the absence of field data, modelers often rely on a
fundamental understanding of the influence of gob parameters and various rules of thumb based
on personal experience.
With regard to gob modulus (an input parameter), Michael Hardy (AAI Principal) stated in an
interview with the investigation team that “it's very important because it controls the load
transfer through the gob…we tweak that a lot to try and get the right load transfer through the
gob. And this is a very important parameter. It's a very difficult parameter because we have
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very little feedback from the field that says this is the stress on the gob. It's the biggest --- quite
possibly the biggest parameter that's used in interpreting load transfer from a gob into the
barrier pillars and surrounding area.” The EXPAREA model that AAI had previously
calibrated to Crandall Canyon Mine conditions used a bilinear gob model. Although a bilinear
gob model is available for use in LaModel, AAI elected to use the default material, strainhardening gob, instead.
The LaModel preprocessor, LamPre, includes a utility to assist users in selecting a final gob
modulus for the strain-hardening gob element. As written in the program Help file, this utility
“is intended to simplify the task of determining gob material properties and to allow the user to
obtain fairly accurate gob properties in the initial model run.” Typically, the user inputs the
width of the gob area and the estimated peak stress on the gob, and the utility returns a final gob
modulus which provides a starting point for calibration.
The parameters that AAI used in the LamPre gob property utility are not available since these
data are not retained in the LaModel input files. Furthermore, given the number of variables that
can affect the utility’s output, it is impossible to replicate the process. However, it appears that
the effects of thin lamination thickness and perhaps a very wide gob resulted in a very low final
gob modulus value.
The effects of a very low gob modulus are readily apparent in the LaModel convergence results.
In models of the North and South Barrier sections that used this value, LaModel convergence
results actually exceeded the height of the mined openings over broad areas of the model. The
modeled entry height was 8 feet but maximum convergence in some of the models exceeded 20
feet, which is physically impossible. Although the excessive convergence values are evident in
the LaModel postprocessor, LamPost, they are not evident in illustrations provided in AAI’s
reports due to the manner in which the output data were scaled.
Scale Selection for Illustration. Each of the reports that AAI prepared for GRI included
numerous illustrations. Typically, color figures were provided to illustrate the distribution of
vertical stress, convergence, and yield condition in plan view. The July 20, 2006, report
(Appendix F), for example, included 21 colored plan view figures, two cross-section views, and
one mine map. All of the vertical stress figures included a key that ranged from 0 to 10,000 psi.
However, one of the cross-section figures shows that peak stresses in excess of 30,000 psi occur
near the barrier rib adjacent to the longwall gob. Thus, a more appropriate label for the key in
the plan view figure would indicate that the highest color range includes all vertical stress levels
greater than 9,000 psi.
It is common practice to scale numerical model results to highlight particular points or ranges of
interest. For example, even though safety factors may range from near 0 to 6 in a given
(hypothetical) model, it may be beneficial to illustrate the range between 0 and 2. Since safety
factors below one indicate failure, this range would show the most critical areas. Similarly, AAI
focused on a range of convergence from 0 to 2 inches because they associated 2 inches of
convergence with difficult roof conditions. Although this scale highlighted a range of interest,
another implication was that the scale masked unreasonably high levels of convergence that were
present elsewhere in the model. The range used in the vertical stress plan views had a similar
effect. Vertical stress levels in these plots appeared to be reasonable even though peak values in
some of the models actually exceeded 90,000 psi.
116
Model Calibration. In the initial proposal to model Main West Barrier mining, AAI
indicated that two previous pillar recovery areas would be used for calibration purposes. One
area was South Mains, which was recovered between August 2005 and October 2006. The
second was the 1st North panels that were recovered between February 1992 and August 1994.
Ultimately, however, AAI opted to calibrate the model based only on the 1st North Left Panels.
In a paper titled “Experience with the Boundary Element Method of Numerical Modeling as a
Tool to Resolve Complex Ground Control Problems” Karabin and Evanto 14 outlined a procedure
for creating and using effective boundary element models. Their recommended simulation
process flow chart is illustrated in Figure 70. The first four steps of the flow chart in Figure 70
represent the model calibration portion of the simulation process. The authors emphasize that
underground observations are an essential first step in any modeling effort. They recommend
that several areas be evaluated and they describe a system of mapping that can be used to
quantify various observed ground conditions for later use in model validation. The authors stress
that verifying model accuracy (i.e., validation) is the most critical step in the entire simulation
process. If model results do not correlate reasonably well with observed conditions, the
calibration process must continue (i.e., material properties must be adjusted).
Figure 70 - Simulation Process Flow Chart
117
AAI’s LaModel model was calibrated to Crandall Canyon Mine ground conditions by adjusting
input parameters until model results were consistent with mining conditions reported to have
existed in the 1st North Left panels. AAI personnel could not make underground observations in
these inaccessible panels, but relied instead on descriptions of the ground conditions provided by
GRI.
AAI claimed that they calibrated the LaModel program using three criteria: vertical stress,
convergence, and yielding condition. Lamination thicknesses and coal strength were varied to
gauge the sensitivity of model results, reportedly to calibrate to all three input criteria. In their
written response to the accident investigation team, AAI indicated that this activity resulted in a
calibrated model that simultaneously fit all three criteria. However, interview statements of the
AAI engineer that did the modeling reveal that the calibration process relied exclusively on an
evaluation of pillar yield condition. Coal strength was adjusted until pillars in the first pillar row
of the 1st North, 9th Left Panel (immediately north of Main West crosscut 99) yielded during
panel retreat while the outby rows did not (Figure 71).
Figure 71 - Modeled Yield Condition - Partial Retreat in 9th Left Panel
While mining the 9th Left panel, difficult roof conditions were encountered (i.e., “peeling top
coal”) on the pillar line. AAI noted that 2.0 inches or more of convergence was associated with
the yielded pillar row in their “calibrated” model. Thus, 2.0 inches of convergence was
considered a site-specific indicator of potential roof and rib instability for subsequent predictive
models.
118
AAI also interpreted abutment stress transfer from their model of the completed 9th Left Panel.
As illustrated in Figure 72, AAI’s model included mining that was done north of the Main West
entries. This northward extension of Main West (labeled “Area A” in Figure 72) was developed
intermittently between 2003 and 2005 and approached to within about 145 feet of the 9th Left
Panel. AAI interpreted model results to show “no significant side abutment stress override
across the barrier on the main pillars, consistent with actual conditions.” Since this
interpretation appears in a report section titled “1st North Left Panels Back-Analysis,” it appears
to be intended to support the validity of AAI’s model. However, the interpretation actually does
little to verify that abutment stress transfer in AAI’s model is reasonable.
Underground observations made by the accident investigation team (in Area A, Figure 72)
confirmed that there were no significant effects of abutment stress transfer from the adjacent
9th Left Panel. However, this observation does not validate AAI’s model results. Given the
geometry, substantial abutment stress effects would not be anticipated to occur in Area A. The
center of this area is bounded by unrecovered pillars in the 9th Left Panel. One end of the area is
bounded by solid coal and the other by a barrier and unmined pillars of the 1st Right Mains. A
more appropriate method of validating model behavior is to correlate model results with stress
damage (e.g., roof or rib deterioration) rather than a lack of damage.
Area A
Figure 72 - Modeled Vertical Stress – Retreat Completed in 9th Left Panel
119
After the initial calibration process based on 1st North Panels, AAI had two opportunities to
verify that model results were consistent with actual observed conditions at the mine. The first
opportunity was in December 2006 when AAI personnel visited the site specifically to view
ground conditions under deep cover. At that time, AAI viewed conditions as being “consistent
with analytical predictions.” Mining had not advanced into the deepest overburden at the time of
the site visit. No modifications were made to the Crandall Canyon Mine model as a result of
AAI’s December 1, 2006, visit.
The second opportunity was after the March 10 pillar burst. AAI was notified by GRI of the
event and Hardy and Gilbride traveled to the site on March 16. When asked “What conclusions
did AAI personnel draw from the conditions observed on the North Barrier section regarding the
adequacy of the design process (e.g,. models) that had been used?,” AAI responded that “The
bump occurrence in the North Barrier was limited to six or seven pillars and did not extend
outby. The observation of this condition seemed to be consistent with the modeling results, i.e.
bump occurred only around the edges of the pillars. Based on the observations in the North
Barrier, further analysis was completed using the established models and a change in the plan
for mining the South Barrier was recommended to reduce bump risk.”
Photographs, sketches, and interview statements of others indicate that the area affected by the
burst was not limited to six or seven pillars and did extend outby. BLM’s Falk noted, for
example, that “Entry ways outby two breaks from the face had extensive rib coal thrown into the
entry way. Stress overrides outby the face were very concerning.” AAI’s field notes also
suggest that the damage was more widespread (see Figure 73). The remnants of damaged pillars
are sketched inside the original pillar boundaries as indicated by the orange lines in the figure.
Photographs taken in this area during AAI’s March 16 visit are included in Appendix O.
Figure 73 - Notes Made by AAI on March 16, 2007
(orange lines added for emphasis)
120
AAI attributed the March burst to a lagging cave inby crosscut 138 and the start-up cave between
crosscuts 134 and 135 based on their onsite observations. The model grid was changed to reflect
this condition. Open entries (as opposed to gob material) were used to represent the areas
between crosscuts 134 to 135 and 138 to 139. However, this change had a negligible effect on
the model results. Since the gob modulus used in both models was very low, the amount of load
transmitted to the gob (rather than transferred to adjacent pillars) was small in either case.
Models run by the accident investigation team indicated that peak stress in the gob only
increased by approximately 7 psi when the lagging cave was replaced with AAI’s low gob
modulus.
Models that AAI developed after the March bursts indicated that high stresses were concentrated
in the area between these two partially caved or un-caved gobs (see Figure 74). A comparison of
Figure 73 and Figure 74 indicates that, even with the lagging cave incorporated into the model,
high vertical stresses do not coincide with the extent of damage observed in the mine. Modeled
vertical stresses in pillars between crosscuts 136 and 137 appear to be quite similar to stress
levels in pillars outby crosscut 133. Furthermore, the pillars outby 133 appear to be largely
unaffected by stress transfer from either the longwall gob to the north or the un-caved pillared
area between crosscuts 135 and 134. AAI postulated that a dynamic failure (a localized burst) of
these pillars could have propagated to pillars over a much wider area.
Figure 74 - AAI Model Results of Vertical Stress in March 2007 Burst Area
The changes that AAI made to their numerical model after the March bursts did not constitute a
recalibration of the model to the observed ground conditions. Had the disparity between field
conditions and model results prompted a careful examination of model input and model
recalibration, a properly constructed model would have shown that the South Barrier section
mine design was destined to fail. The following section illustrates the output that can be derived
by a properly constructed model using AAI’s reported parameters.
BEM Using AAI Model Constructed as Reported. LaModel analyses were conducted with
coal properties distributed as outlined in the text of AAI’s July 20 report (Appendix F). Results
indicate that pillars in the North and South Barrier sections would have failed over a relatively
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broad area (Figure 75). In this figure, red and yellow represent elements with a safety factor less
than 1 (i.e., the element is considered to have failed).
Figure 75 - Element Safety Factors with Coal Properties Distributed as Indicated in AAI Report
Figure 76 illustrates element safety factors from a simulation in which AAI’s model was further
modified to reflect gob properties and lamination thicknesses more consistent with their
calibrated EXPAREA model. In this case, a bilinear gob model was used rather than strain
hardening and lamination thickness was increased to 115 feet rather than 25 feet. The greater
thickness was established using an equation provided by Heasley5. Also, rather than modeling a
single scenario as AAI had, mining in the North and South Barriers was modeled as three steps:
(A) North Barrier pillar recovery to crosscut 133, (B) South Barrier development and (C) South
Barrier pillar recovery to about crosscut 131. Results of these model steps are illustrated in
Figure 76. Both models (Figure 75 and Figure 76) show widespread pillar failure.
Element safety factors based on the modified model show pillar failure near the site of the March
10 outburst accident (Figure 76 A). Pillar rib elements fail under the deepest cover but pillars
remain stable as the South Barrier is developed (Figure 76 B). However, as pillars are recovered
in the South Barrier, failure propagates outby the face and extends into the Main West and North
Barrier section workings. Although the model does not match the observed damage as well as
Dr. Heasley’s model, it is generally consistent with the failures that occurred in March and
August 2007 at Crandall Canyon Mine. The modeling results illustrate that a properly
constructed and calibrated model will depict that the South Barrier section pillar design is
unstable and destined to wide spread failure.
122
Figure 76 - Element Safety Factors using Modified Coal Strength Property
Distribution, Gob Properties, and Lamination Thickness
123
South Barrier Design. After the March burst, AAI changed their model to reflect a lagging
cave but this change had very little impact on model results. The model used to evaluate designs
for the South Barrier section was essentially the same as the model used to design the North
Barrier section. Proposed design changes including longer crosscut spacing were evaluated.
AAI had modeled the effects of longer crosscut spacing early in the Main West Barrier Mining
project. Their earlier conclusion was that “increasing crosscut spacing does not significantly
improve conditions.” Increased pillar length (reported as a 20-foot increase, but modeled as a
10-foot increase from 70 to 80 feet) “only incrementally reduces rib yielding, corresponding to a
modest decrease in entry convergence.” In the South Barrier section models, however, pillar
length was increased by 37 feet (72 to 109 feet). AAI noted that modeled stresses in the
projected South Barrier workings were similar to those experienced at the March burst site when
crosscuts of similar length were used (see handwritten notes, Figure 77). However, AAI
concluded that the longer crosscut spacing “increases the size and strength of the pillars’
confined cores, which helps to isolate bumps to the face and reduce the risk of larger bumps
overrunning crews in outby locations.”
Figure 77 - AAI Notation on Plot of Model Results
Text boxes reflect handwritten notes and were added for clarity.
AAI’s model results with two different crosscut spacing distances are shown in Figure 78. The
images are similar in the sense that high stresses are concentrated in pillar ribs adjacent to the
expanding gob area. With longer pillars, the concentration appears to be reduced in the vicinity
of the outby intersection. It is important to note, however, that the models did not evaluate pillar
recovery on a cut-by-cut basis. When pillar cuts remove coal from the inby ends, the pillars in
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the active mining area are reduced in size. Consequently, some of the benefit of longer pillars in
the active mining area is diminished as pillar recovery proceeds. The stress concentration will
migrate towards the outby intersection as the pillar in the active mining area is reduced.
Although the larger (i.e., longer) pillars used in the South Barrier were stronger than those used
in the North Barrier, they were not sufficient to ensure the stability of these workings during
pillar recovery. Given the aforementioned deficiencies, the models provided no insight into the
“risk of larger bumps overrunning crews in outby locations.”
Figure 78 – AAI Modeled Vertical Stress Results Comparing Effects of Crosscut Spacing
ARMPS Analyses. As part of their evaluation of proposed mining in the North Barrier section,
AAI performed calculations using NIOSH’s Analysis of Retreat Mining Pillar Stability
(ARMPS) software. Model procedures and results described in an August 9, 2006, email from
Leo Gilbride to Laine Adair provide insight to these analyses. The available information
demonstrates that much of AAI’s ARMPS analysis was consistent with NIOSH’s recommended
use of the program. However, several assumptions led to overstated estimates of stability. In
addition, calculations indicating extremely low pillar stability factors for the South Barrier
analysis were either misinterpreted or not acted upon.
ARMPS Input. AAI calculated stability factors (StF’s) for the 1st North Panels and for the
North Barrier section. The calculations were performed using default values available in
ARMPS. For example, the analyses relied on default values for in situ coal strength (900 psi),
unit weight of overburden (162 lb/ft3), abutment angle of gob (21º) and extent of the active
mining zone (AMZ). Using these values and the geometries illustrated in Figure 79, AAI
determined that the minimum pillar stability factor (PStF) in the 1st North Panels was 0.37.
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Minimum PStF in the North Barrier section was 0.53 at 2,000 feet of overburden. These values
(0.37 and 0.53) are generally consistent with the PStF values discussed earlier in Table 5 and
Table 7 (Method 1 – 215-foot barrier). However, it is important to note that Method 1 overstates
the benefit of leaving a row of bleeder pillars. More conservative estimates of PStF at 2,000 feet
of overburden, obtained using Methods 2 and 3, are 0.29 and 0.27, respectively.
Figure 79 - ARMPS Analysis Geometries used by AAI
Back-Analysis. NIOSH provides the following guidance for developing site-specific criteria
in one of the resource files 15 provided in the ARMPS Help file:
“ARMPS appears to provide good first approximations of the pillar sizes
required to prevent pillar failure during retreat mining. In an operating mine,
past experience can be incorporated directly into ARMPS. ARMPS stability
factors can be back-calculated for both successful and unsuccessful areas. Once
a minimum ARMPS stability factor has been shown to provide adequate ground
conditions, that minimum should be maintained in subsequent areas as changes
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occur in the depth of cover, coal thickness, or pillar layout. In this manner,
ARMPS can be calibrated using site-specific experience.”
Back-analysis is considered an acceptable practice for mines with a proven track record of retreat
mining experience. However, site-specific criteria used in lieu of NIOSH’s recommendations
should be developed cautiously using multiple case histories with known conditions at a given
mine. In these cases, proper examinations of individual mine data may demonstrate that stability
factors above or below NIOSH’s recommended values are warranted. Proper examination must
entail an analysis of the broad experience at a mine site rather than a focus on isolated case(s)
that represent the extreme.
AAI used default input parameters (including 900 psi coal strength) in their ARMPS analyses.
Therefore, the resulting stability factors could be compared directly to those comprising the
NIOSH database. AAI considered the database and observed that:
“The ARMPS database shows that industry experience is mixed for mines
reporting similar SFs (0.16 to 1.05) at comparable depths (1,500 to 2,000 ft). Of
these cases, slightly more than half were successful, while the remainder
encountered ground control problems.”
This observation is accurate. Eleven of 21 cases at depths greater than 1500 feet were deemed to
be satisfactory designs. Difficult ground conditions were attributed to the remaining ten.
Similarly, five of ten cases with PStF’s less than 0.53 (i.e., the PStF value they determined for
the proposed North Barrier section) were satisfactory and the other five experienced difficulties
(see Figure 80). It is noteworthy that in all of the “failed” cases, NIOSH indicated some degree
of pillar “bumping” was involved.
Figure 80 - Pillar Stability Factors from NIOSH ARMPS Database for Depths Over 1,500’
NOTE: NIOSH ARMPS Database only contains case histories at or below 2,000’ overburden.
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AAI recognized that the North Barrier section pillar stability factors they had calculated were
below the NIOSH recommended minimum. AAI reasoned that since the 1st North Left block
panels had been mined successfully with a PStF of 0.37, the North Barrier section with a PStF of
0.53 should be acceptable:
“At GENWAL [Crandall Canyon Mine] good success has been achieved at SFs
below 0.90. Retreat conditions in the 1st North Left block were generally
successful with a SF of 0.37, suggesting that a SF of about 0.40 is a reasonable
lower limit for retreat mining at GENWAL…The lowest SF for the proposed
retreat sequence in Main West barriers is 0.53 under the deepest cover, which is
approximately 43% higher than the "satisfactory" SF of 0.37 for the 1st North
Left block. Implications are that the proposed retreat sequence in Main West will
be successful in terms of ground control, even under the deepest cover (2,200 ft).”
However, AAI’s back-analysis was flawed in several ways. First, the panels in 1st North Panels
were considered to be satisfactory designs despite the fact that pillar rows were skipped in each
of the last four panels near the deepest cover. This assumption was made even though AAI, and
GRI personnel who provided information to AAI, did not have personal experience with mining
in these areas. Mine personnel related problems associated with roof coal and AAI considered
this from the standpoint that similar problems would not be anticipated in the North and South
Barrier sections:
“…occasional problems with peeling top coal were encountered in the 1st North
Left block. This required skipping pillars on retreat in some locations. Top coal
is currently mined to minimize this risk and is not expected to be a problem in
Main West.”
It is highly speculative to conclude that additional problems would not have been encountered
had the top coal been mined in these areas. Furthermore, reports indicate that ground control
problems were not limited to spalling top coal. Two injuries caused by ground failures (a burst
and a rib roll associated with a bounce) were reported during pillar recovery in the 1st North
7 Left panel.
Second, AAI’s analysis considered GRI’s pillar recovery experience in the 1st North Left Block
panels but did not consider recovery work in the South Mains. GRI had much more recent
experience and first hand knowledge of ground conditions during pillar recovery in this area
since mining was not completed until October 2006. Although the South Mains pillars and
barriers were recovered in a different manner than the Main West Barriers, back-analysis would
have demonstrated that PStF’s in the North and South Barrier sections were far lower than those
associated with difficult conditions in the South Mains. Rather than anticipating ground
conditions better than those encountered in the 1st North Left Block panels, GRI and AAI should
have expected conditions worse than those encountered in the deepest cover in the South Mains.
Third, AAI’s analysis did not consider barrier pillar stability factors. In formulating their
recommendations for stability factors in deep cover mining operations, NIOSH noted that the use
of large barrier pillars in conjunction with reasonably sized pillars substantially increased the
likelihood of successful pillar recovery in overburden greater than 1,000 feet. Minimum
BPStF’s for panels in 1st North and for recovery in the South Mains were 1.52 and 1.59,
respectively. The back-analysis showed that pillar recovery at Crandall Canyon Mine
historically had been conducted with barrier pillar stability factors (BPStF) exceeding 1.5, as
shown in Figure 81. The minimum BPStF calculated for the North Barrier section varies from
0.98 to 1.54. Method 1, representing the effect of combining the bleeder pillar and barrier pillar
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in ARMPS (i.e., assume the pillar is not developed) yielded the 1.54 BPStF value that is
consistent with BPStF’s in the historical previously mined areas. However, Method 1 overstates
the benefit of leaving bleeder pillars. Methods 2 and 3, which offer more realistic approaches,
both show that BPStF in the North Barrier design is well below those calculated for past Crandall
Canyon Mine pillar recovery areas.
Finally, after the March 10 outburst accident, AAI again used ARMPS to evaluate several
potential pillar designs for use in the South Barrier section. The analyses included a design
similar to the one that was actually implemented. The ARMPS pillar stability factor for this
design is 0.26 and the barrier pillar stability factor is 0.87 (yellow square in Figure 81). There
are no indications that these values were included in any written report or email to GRI. AAI’s
StF’s were based on a barrier width of 137 feet between the section and the worked out longwall
Panel 13. When it was actually developed, the barrier width was reduced to 121 feet. For this
scenario, the pillar and barrier pillar stability factors are 0.23 and 0.76, respectively. The South
Barrier section PStF’s are below AAI’s mine-specific stability threshold of 0.4 and below the
values associated with the March 10 outburst accident. Also, Figure 80 illustrates that the PStF
values for the implemented South Barrier section pillar design at 2,000 feet of overburden are
below all successful cases in the data base and equivalent to two failed cases. None of these
ARMPS results were presented in the April 2007 AAI report for the South Barrier section design
that MSHA considered in the plan approval process (see Appendix I).
Barrier Stability Factor (BPStF)
2.5
NIOSH Minimum PStF
1st North Panels 6 to
9 Pillar Recovery
NIOSH Minimum BPStF
2
NB Recovery Burst
OB using Different
Calculation Methods
South Mains Pillar
Recovery
1.5
1
0.5
AAI South Barrier Pillar
Recovery Calculation
0
0
0.5
1
1.5
2
Pillar Stability Factor (PstF)
Note: NB = North Barrier, SB = South Barrier, OB = Overburden
1st North Panels 6 to 9 Recovery
South Mains Pillar Recovery
NB Burst OB Method 1 - 2160 OB
NB Burst OB Method 2 - 2160 OB
NB Burst OB Method 3 - 2160 OB
AAI SB Recovery Calc - 2000 OB
Figure 81 – Crandall Canyon Mine ARMPS Stability Factors showing AAI South Barrier Calculations
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Roof Control Plan
Section 30 CFR 75.220(a)(1) requires each mine operator to develop and follow a roof control
plan, approved by the district manager, that is suitable to the prevailing geological conditions and
the mining system to be used at the mine. After reviewing the plan, the mine operator is notified
in writing of the approval or denial of the proposed roof control plan or proposed revision. At
the time of the August 2007 accidents, the relevant portions of the approved roof control plan
consisted of the following:
•
A base plan approved July 3, 2002.
•
Added pages 21 through 94 concerning pillar recovery, approved September 5, 2003.
•
A site-specific plan for extraction of pillars in South Barrier section, dated May 16, 2007,
and approved June 15, 2007.
Several previous site specific roof control plans had been approved for mining the North and
South Barrier sections. At the time of the August accidents, these plans had been terminated
because mining had been completed in the affected areas:
•
A site-specific plan for development of North Barrier section, dated November 11, 2006,
and approved November 21, 2006.
•
A site-specific plan for leaving roof coal during development of North Barrier section,
dated January 10, 2007, and approved January 18, 2007.
•
A site specific plan for pillar recovery in North Barrier section, dated December 20,
2006, and approved February 2, 2007.
•
A site-specific plan for development of South Barrier section, dated February 20, 2007,
and approved March 8, 2007.
On July 20, 2006, a draft report of a geotechnical analysis for developing the North and South
Barrier sections was sent from Gilbride to Adair (see Appendix F). The report concluded “that
the proposed Main West 4-entry layout with 60-ft by 72-ft (rib-to-rib) pillars should function
adequately for short-term mining in the barriers (i.e., less than 1 year duty)”. AAI conducted
another geotechnical analysis, dated August 9, 2006, for recovering the pillars in the North and
South Barrier sections. The report for this analysis stated that “ground conditions should be
generally good on retreat in the barriers, even under the deepest cover (2,200 feet)”. On
September 8, 2006, GRI provided these reports to MSHA District 9 to justify approval of their
proposed plans to mine the North and South Barrier sections. As part of the plan review of the
AAI ARMPS analysis, MSHA District 9 conducted a back-analysis of the 1st North 9th Left
Panel. The MSHA analysis determined that the pillar stability factor (PStF) should exceed 0.42
for the proposed North and South Barrier recovery plans. No assessment was made for the
required barrier pillar stability factor (BPStF). The MSHA ARMPS analysis is described in
Appendix W.
MSHA’s review of the August 9, 2006, AAI analysis for pillar recovery in the North and South
Barrier sections raised several questions. On November 21, 2006, MSHA sent a letter to GRI
stating that the pillar recovery plan could not be approved and listed the following deficiencies:
1. In situ coal strength was estimated at 1640 psi. An explanation of how this strength was
determined should be included. Typical coal strength values are much lower.
2. The elastic modulus of coal was estimated at 500 ksi. An explanation of how this
modulus was determined should be included. If experimental analysis of test samples
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was conducted, an explanation of the number of samples, the size of samples, and the
testing method employed should be included in the submittal.
3. The mine geometry employed in the computer model differs from the physical map
geometry. This observation applies to the ARMPS model geometry employed in the
analysis of the historical section and the projected sections.
4. The LAMODEL analysis shows, that during pillaring, surrounding pillars exhibit
yielding zones. This could indicate a violent outburst since the in-situ coal strength is
stated as 1640 psi.
5. A stability factor of 0.37 was determined by analyzing the pillars of 1st North 9th Left
Panel. The analysis of this area was employed to determine the minimum stability factor
for favorable retreat mining. This stability factor appears to be determined from where
mining ceased due to poor ground control conditions. Therefore, a higher stability factor
should be employed that ensures an adequate factor of safety.
There was no written response from GRI to MSHA’s letter. However, Billy Owens discussed
these inconsistencies with GRI in December 2006. Owens recalled that GRI provided the
following explanations to address the deficiencies:
1. Studies indicate that coal strengths for the Hiawatha seam range from 1,800 to
4,000 psi and, therefore, the operator felt that the 1,640 psi coal strength was
appropriate.
2. AAI had instrumented the coal Hiawatha coal seam and determined that the elastic
modulus of 500 ksi was typical.
3. The ARMPS program is not designed to simulate a section that is recovering pillars but
leaving an unmined pillar to establish a bleeder. AAI’s model incorporated the bleeder
pillar as part of the barrier pillar. Also, the geometry that AAI used was from actual
survey data provided by the operator.
4. As long as the core was not overstressed, there was no bounce potential.
5. The minimum stability factor of 0.40 was used, which was above the 0.37 threshold
determined by back-analysis in 1st North.
Based on this information, Owens agreed with AAI’s analysis. However, approval of the North
and South Barrier section recovery plans would only be granted if favorable conditions were
observed during development.
North Barrier Section - Development Plan. GRI submitted a roof control plan for developing
through the North Barrier section, dated November 11, 2006, which was approved by MSHA on
November 21, 2006. The plan showed development of four entries through the barrier. The plan
specified a minimum of 80 x 90-foot centers, which could vary depending upon conditions
encountered. The plan required a minimum 130-foot barrier to the north. The width was not
specified for the barrier to the south.
Density of the primary roof support during development of the North Barrier section was six
bolts per row with a maximum distance of five feet between rows. This bolting pattern had been
used routinely for many years even though it had not been specified previously in the roof
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control plan. The entries and crosscuts were to be mined a maximum of 20 feet wide. No roof
coal was to be left in this area.
Owens and Peter Del Duca visited the developing North Barrier section on January 9, 2007, to
assess and investigate the conditions for the pillar recovery plan, dated December 20, 2006. At
that time, the section had advanced past the deepest overburden to about crosscut 141 which was
beneath approximately 2,000 feet of overburden. This inspection was purposely scheduled so
that conditions could be observed under the deepest cover prior to approval of the pillar recovery
plan. Owens considered pillar yielding that he observed to be acceptable. However, weak roof
rock was falling out during mining. He discussed with GRI the possibility of leaving roof coal to
prevent this. Prior experience had shown that roof coal would help support the weak rock. The
plan was revised on January 18, 2007, to permit leaving roof coal. Where roof coal was left, the
minimum length of bolt was required to be six feet.
Owens also observed that there was a need for roof-to-floor support in the crosscut between the
Nos. 3 and 4 entries. Since the No. 4 entry was the future bleeder entry after pillar recovery
started, he informed GRI that additional roof support would be needed in this crosscut for
approval of the submitted pillar recovery plan. GRI submitted a revised pillar recovery plan that
required a double row of timbers in the crosscuts adjacent to the bleeder entry.
North Barrier Section - Pillar Recovery Plan. Based on information furnished by GRI, AAI’s
ground control analysis, and visual observations during development, the pillar recovery plan for
the North Barrier section (dated December 20, 2006) was approved on February 2, 2007. The
plan showed the sequence of removing pillars from west to east and specified where coal was not
permitted to be mined. The rows of pillars were to be extracted from south to north. Pillars
between the Nos. 3 and 4 entries were not mined to establish a bleeder entry. Barrier mining was
not permitted. A double row of roof-to-floor support, on four-foot maximum centers, was
required to be installed outby the pillar line at the entrance to the crosscuts in the No. 4 entry.
MSHA personnel did not visit the North Barrier section during pillar recovery. Coal outburst
accidents occurred on this section on March 7 and 10. GRI did not immediately contact MSHA
at once without delay and within 15 minutes at the toll-free number, 1-800-746-1553, following
both of these accidents as required by 30 CFR 50.10. On March 12, 2007, GRI contacted MSHA
District 9 personnel by telephone to request approval to move the bleeder measurement point
location outby. The proposed location was in the No. 4 entry, adjacent to the pillar line, because
the bleeder entry had been damaged by the coal outburst accident. An MSHA inspection was not
conducted in the area affected by the accident. MSHA denied the request because the bleeder
could not be properly evaluated at the proposed measurement point location. The section was
abandoned and sealed.
South Barrier Section - Development Plan. On March 8, 2007, prior to the accident that stopped
pillar recovery in the North Barrier section, a plan for developing the South Barrier section
(dated February 20, 2007) was approved. The plan allowed development of four entries through
the barrier. The plan specified a minimum of 80-foot entry centers and 90-foot crosscut centers,
which could vary depending upon conditions. A 55-foot barrier was required to the north. No
width was specified for the barrier to the south.
Density of the primary roof support during development of the South Barrier section was six
bolts per row with a maximum distance of five feet between rows. The entries and crosscuts
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would be mined a maximum of 20 feet wide. Roof coal could be left in areas where weak
immediate roof was encountered.
At the end of March 2007, development mining began in the South Barrier section under the
approved roof control plan. The North Barrier coal outburst accidents had prompted the operator
to have AAI reevaluate mining of the South Barrier section. While AAI was performing their
analysis, mining was conducted in relatively shallow overburden in the vicinity of crosscuts 108
to 115. Although AAI considered designs based on 35 feet (measured from the Main West
notches) and 137 feet wide barriers, mining in this area established the barrier widths at 55 and
121 feet. AAI completed their analysis as mining progressed to crosscut 118. AAI’s
recommendations for pillar recovery were: to increase pillar centers from 80 x 92 feet to
80 x 129 feet, to recover the pillars as completely as is safe, to slab the south side barrier, and to
avoid skipping pillars under the deepest cover (refer to Appendix I). Based on these
recommendations, development mining to the west of crosscut 118 was established on 80 x 130foot centers.
South Barrier Section - Pillar Recovery Plan. On May 16, 2007, GRI submitted site-specific
amendments to the roof control and ventilation plans to permit pillar recovery of the South
Barrier section. They also provided MSHA with a copy of the AAI report for pillar recovery in
the South Barrier section. Maps included with both proposed plans were consistent in showing
that no pillars would be recovered immediately adjacent to the bleeder entry. In the three-entry
portion of the section between crosscuts 139 and 142, both proposed plans showed slab cuts from
the barrier pillar south of the No. 1 entry, as well as recovery from those pillars between the
No. 1 and No. 2 entries.
On May 22, 2007, Owens and Gary Jensen visited the South Barrier section to observe
conditions and evaluate the adequacy of the proposed roof control plan amendment. Owens
determined that pillars were yielding closer to the face and that pillars outby appeared to be more
stable than he had observed during his visit to the North Barrier section. He interpreted these
observations to be favorable. However, he expressed concern that any pillar recovery in the area
between crosscuts 139 to 142 could jeopardize bleeder stability and suggested that no pillar
recovery be conducted in this area. The following day, GRI submitted a revised roof control
plan for recovering the South Barrier section. The revised plan showed that no pillars would be
recovered between crosscuts 139 and 142, and no slab cuts would be mined from the barrier
pillar south of the No. 1 entry. The proposed ventilation plan for recovering the South Barrier
section was not revised, resulting in differences between the maps in the proposed plans (see
Figure 82). However, the ventilation plan addendum did contain a provision stating: “This plan
is for the ventilation for the pillar recovery of the developed area of the south barrier block…The
pillar recovery proposed by this plan will be done in accordance with the approved Roof Control
Plan.” Accordingly, the pillar recovery sequence was not shown on the map included with the
site-specific ventilation plan, giving preference to relevant portions of the roof control plan. The
ventilation plan for South Barrier pillar recovery was approved on June 1, 2007.
The revised roof control plan for pillar recovery of the South Barrier section was approved on
June 15, 2007 (see Appendix J). Measurements from the scaled map included with this roof
control plan addendum indicated that the pillars were to be mined on 80 x 130-foot centers. The
plan also showed the sequence of removing pillars from west to east and specified where coal
was to be left unmined. The rows of pillars were to be extracted from south to north. To protect
the No. 4 bleeder entry, the northern-most pillars were not recovered.
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A 55-foot barrier between the South Barrier section No. 4 entry and the sealed Main West
notches was also required to be left unmined. The roof control plan permitted a maximum
40-foot cut from the last row of roof bolts into the barrier south of the No. 1 entry. A double row
of roof-to-floor support (timbers) was also required to be installed at the entrance to crosscuts in
the No. 4 entry for additional bleeder protection. These timbers were required to be set a
maximum of four feet apart with a minimum of four per row.
Figure 82 - Comparison of South Barrier Roof Control and Ventilation Plans
Mine management was made aware of the approved roof control plan requirements by the UEI
engineering staff, who routinely provided the mine with 1":100' scaled section maps of projected
mining. This map (referred to as a “mark up map”) was posted in the records room and
additional copies were provided to section foremen. Section foremen placed temporary notations
on the posted mark up map showing mining progress at the end of each shift. Periodically,
engineers would exchange new mark up maps for older copies, from which they would
incorporate the temporary notations into the up-to-date map of the entire mine.
The initial South Barrier section mark up map showed the pillar recovery sequence from crosscut
149 to crosscut 142. On July 31, 2007, as pillar recovery approached crosscut 143, Gary
Peacock emailed David Hibbs (manager of engineering), “We need an updated mark up map at
Crandall showing the pillars that will be left in the area were there is only 3 entries.” Hibbs
replied, “Gary, I feel we need to leave all rows in the area of 3 entries and also delete the
barrier. Do you have any thoughts?” Peacock answered, “I think we should take the barrier.”
Hibbs responded to Peacock: “Gary, This is the drawing in approved Roof Control Plan for that
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area.” Hibbs attached a copy of the pillar extraction map from the approved roof control plan
and included Shane Vasten (surveyor) in his email response to Peacock. Later that evening,
Vasten emailed Peacock and Hibbs: “Gary, Here is a mark up map for you to look at based on
the latest approvals forwarded to me from Dave. If you have any questions/concerns, get with
Mr. Hibbs. Ace and I will be there tomorrow doing month end. I will check with you then to see
if any changes need to be made. I will also plot more maps for you then. I just wanted to send
you this one so you can be looking it over.” Between crosscuts 142 and 139, the attached mark
up map (see Figure 83) correctly showed that no pillars were to be recovered and the barrier was
to remain unmined south of the No. 1 entry (as indicated by the standard symbol X in the pillars)
in accordance with the approved roof control plan. Interview statements, belt scale records, shift
foremen’s reports, and production records revealed that the barrier south of the No. 1 entry
between crosscuts 139 and 142 was, nonetheless, mined.
Figure 83 - Mark Up Map Provided to Mine Management on July 31, 2007
Roof control plans as required by 30 CFR 220(a) (1) must be developed and followed by the
mine operator and be suitable for the prevailing geologic conditions and the mining system to be
used at the mine. MSHA approved site specific roof control plans for pillar recovery in the
North and South Barrier sections by considering observed mining conditions and AAI’s analyses
of mine stability provided to MSHA by GRI. Although no adverse conditions were observed
when MSHA roof control specialists visited the sections during development mining, adverse
conditions were encountered during pillar recovery on both sections, including coal burst
accidents on at least three occasions: March 7, March 10, and August 3. Prior to the March 10
and August 6 accidents, miners were struck by coal, ventilation was impaired, regular mining
was disrupted, and equipment was damaged, indicating that the roof control plan was not suitable
for controlling the roof, face, ribs, or coal bursts. While recovering pillars in the South Barrier
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section, miners recognized that ground conditions were similar to those that forced abandonment
of the North Barrier section. Although these similar conditions indicated that the roof control
plan was inadequate, revisions to the plan were not proposed by GRI and mining was allowed to
continue until the August 6 accident.
Summary – Critique of Mine Design
ARMPS and LaModel analyses were conducted by AAI to evaluate the stability of mine designs
proposed for development and recovery of pillars in the North and South Barrier sections.
Although AAI concluded that the designs should function adequately, mining in each area ended
in failure. A review of input files, model results, notes, and various types of correspondence
indicates that the analyses were flawed and relied on overly optimistic assumptions.
Furthermore, the South Barrier section was evaluated using essentially the same models that had
proved to be unreliable in the North Barrier section analyses. An AAI ARMPS analysis that
showed the design was inadequate was not included in the report that GRI furnished to MSHA.
The roof control plan, developed by GRI using AAI’s mine design, was not suitable to the
prevailing burst prone ground conditions and the pillar recovery system used in the North and
South Barrier sections. Accident experience at the mine included at least three coal outburst
accidents in the North and South Barrier sections prior to August 6. The accident on August 3,
2007, showed that conditions on the South Barrier section were similar to those preceding the
March 10 accident. Following the August 3 accident, GRI did not propose revisions to the roof
control plan when conditions and accident experience indicated the plan was inadequate and not
suitable for controlling coal bursts on the South Barrier section. Instead, GRI resumed mining in
a manner that did not comply with the approved roof control plan. Continued pillar recovery
prior to taking corrective actions following the August 3 accident exposed miners to hazards
related to coal bursts.
An analysis of MSHA’s roof control plan review process is beyond the scope of this report.
MSHA’s procedures for determining if mine operators are complying with relevant requirements
of 30 CFR and the Mine Act will be addressed in the findings of an independent review team.
Mine Ventilation
Mine Ventilation System
Figure 84 depicts a simplified schematic of the mine ventilation system based on air
measurements recorded during the week prior to the accident. The mine was ventilated by
exhausting fans. Mine openings consisted of five drift openings. From left to right, the first drift
served as the entrance to an underground bath house and provided a small amount of intake air.
The second drift served as the main intake and travelway. The third drift contained the belt
conveyor. Return air exited the mine through the fourth drift. A stopping was erected in the fifth
drift to separate the return air course from the surface.
According to the weekly examination record book, in the week preceding the August 6, 2007,
accident, 220,806 cfm of air was entering the mine through the main intake. An air quantity of
252,216 cfm was exiting the mine through the return drift and main fans. The quantity entering
the belt haulage entry and the bath house entrance were not recorded in the weekly examination
book. A revised ventilation map received on July 2, 2007, indicated that 31,036 cfm of air
entered the mine through the belt drift and 5,200 cfm entered through the bathhouse.
136
Figure 84 - Ventilation System before August 6 Accident
137
The main fan installation consisted of four main fans. Two parallel sets of two fans in series
were utilized. Documents provided by the operator indicate that an original installation of two
fans in parallel had been upgraded by installing additional fans in series resulting in the four fan
system. The fan system capacity was stated in the ventilation plan as 300,000 cfm, with 150,000
cfm being provided by each set of fans. The actual operating point of the fan system prior to the
accident was 252,216 cfm at a pressure of 6.5 inches of water gauge.
At the time of the accident, the ventilation system consisted of three main air splits: the 3rd North
section, the completed South Mains pillar recovery section, and the South Barrier section. Only
the South Barrier section was active. A minimum of 15,000 cfm of air was required by the mine
ventilation plan at the intake end of the pillar line. Records indicate that 51,340 cfm was
provided. A discussion of the ventilation plan is included in Appendix X.
Post-Accident Mine Ventilation
The effect of the August 6, 2007, accident on the mine ventilation system was significant. The
initial air blast and burst coal pillars destroyed or damaged stoppings from the accident site outby
to crosscut 93 and the overcasts at crosscut 90 and 91. The damage short-circuited ventilation
inby that point.
The short circuiting of air affected the main fan pressure. Figure 85 shows the fan pressure
recorded by the mine monitoring system for the time period immediately before and after the
accident. Also, the daily fan examination record book indicated 6.5 inches of water gauge (w.g.)
for fans 1 and 2 and 6.25 inches w.g. for fans 3 and 4 on the previous day. A pressure of
5.25 inches w.g. for fans 1 and 2 and 5.5 inches w.g. for fans 3 and 4 was recorded after the
accident. This was an average decrease of 1.0 inches w.g. after the accident.
Figure 85 - Fan Pressure at the Time of the August 6 Accident
Curtains were installed in place of the damaged permanent ventilation controls up to the rescue
work site in the hours following the August 6 accident. The subsequent burst at 1:13 a.m. on
138
August 7 damaged many of these temporary ventilation controls. The temporary controls were
then replaced with permanent stoppings. These permanent stoppings were completed prior to
resuming rescue efforts. Figure 86 shows the locations of stoppings damaged in the August 6
accident and the stopping configuration after the August 16 accident.
Figure 86 - Ventilation Controls after Accidents
139
Originally, the South Barrier section No. 3 entry was in common with the belt entry. As
ventilation controls were reestablished, the No. 3 entry was utilized as a return air course.
Stoppings were erected between the No. 2 and 3 entries. A feeder was set in the No. 2 entry
between crosscuts 119 and 120. The stoppings between the intake and belt entries (No. 1 and
No. 2) were reestablished up to crosscut 120. Crosscut 120 was left open to serve as the haul
road to the feeder. A stopping was built across the No. 2 entry inby crosscut 120. Inby that
point, the No. 1 entry served as the intake and the Nos. 2, 3, and 4 entries served as returns.
As material was loaded and the rescue operation advanced, ventilation controls were erected in
the crosscuts between the No. 1 and No. 2 entries. The last crosscut outby the clean-up area was
left open to serve as a connection to the return air course. Line curtain was used to ventilate to
the clean-up area during the rescue operation.
Ventilation in Area of Entrapment
It was unlikely that any ventilation was reaching the working area of the South Barrier section
immediately after the August 6 accident. When boreholes were drilled into the South Barrier
section, outside air entered the holes due to the negative pressure of the exhausting ventilation
system. This indicated that some borehole air could be drawn through the collapse area. Later,
air was injected into some holes to provide breathable air to potential survivors. Initially the
other holes continued to intake. However, when the injected air volume was increased, air exited
from the other boreholes. The air being injected (2,000 to 3,000 cfm) exceeded the air quantity
returning to the mine ventilation system. This observation shows that the rubble from the
collapse severely restricted air flow to the South Barrier section.
On the morning of August 6, rescuers attempted to pump breathable air to the section from
underground. A compressor was used to force air through the fresh water pipeline running along
the South Barrier section belt. Since the pipeline was likely damaged by burst material between
crosscut 120 and the working section, the air may not have reached the work area.
Air Quality in South Barrier Section Pillar Recovery Area
Before the accident, preshift examination records for the South Barrier section indicated air
quality of 20.9% oxygen (O2), 0% methane (CH4), and 0 ppm carbon monoxide (CO). After the
accident, oxygen deficiency as low as 16% was encountered. Samples from Borehole No. 1
taken at 9:57 p.m. on August 10, 2007, indicated 7.46% O2, no detectable amount of CH4, 141
ppm CO, and 0.58% CO2. Exposure to this atmosphere will result in vomiting, unconsciousness,
and death. Higher oxygen concentrations were detected in Borehole Nos. 3 and 4. However, no
evidence of the miners was observed in these boreholes. It is likely the entrapped miners were
exposed to an atmosphere similar to that observed in Borehole No. 1.
Had the miners survived the initial catastrophic ground failure, oxygen deficiency would have
contributed to their deaths. Table 1116 lists effects of exposure to reduced oxygen. These effects
would occur at increased oxygen concentrations at higher altitudes. Figure 87 16 shows the time
of useful consciousness versus oxygen concentration. At 7.5% O2, the time of useful
consciousness is just over one minute. The time of useful consciousness is the time after
exposure to oxygen deficiency during which a person can effectively take corrective action such
as donning an SCSR before impairment or unconsciousness occurs.
140
Table 11 - Effect Thresholds for Exposure to Reduced Oxygen
% O2
by
Volume
Effect
17
Night Vision Reduced, Increased Breathing Volume, Accelerated Heartbeat
16
Dizziness
15
Impaired Attention, Impaired Judgment, Impaired Coordination, Intermittent
Breathing, Rapid Fatigue, Loss of Muscle Control
12
Very Faulty Judgment, Very Poor Muscular Coordination, Loss of
Consciousness, Permanent Brain Damage
10
Inability to Move, Nausea, Vomiting
6
Spasmatic Breathing, Convulsive Movements, Death in 5-8 Minutes
Figure 87 – Approx. Time of Useful Consciousness vs. Oxygen Concentration
For Seated Subjects at Sea Level. Adapted from Miller and Mazur16
141
Three sources of the oxygen deficiency detected in the South Barrier section after the accident
were considered:
•
•
•
Release of in situ gasses from the coal seam,
Oxidation of the coal during the initial catastrophic pillar failure, and
Breaching of one or both of the barrier pillars to the north and south of the
section.
At other mines, low oxygen concentration has been reported to have occurred after coal bursts.
However, reports of these accidents also indicated that the oxygen was displaced by a release of
methane gas. Several samples taken from boreholes after the August 6 accident contained
methane concentrations below 0.1%. The remaining samples contained no detectable amount.
No report of oxygen deficiency was recorded for the preshift examination conducted after the
March 10, 2007, outburst accident, nor was there any indication of oxygen deficiency from
interview statements.
During development of Main West, approximately between crosscuts 73 and 78 and at the mouth
of 1st North, gasses were liberated during mining that created a detectable amount of oxygen
deficiency. The gasses present were unknown and appeared to be related to a change in the
immediate roof confined to that area. The oxygen deficiency was detectable only by placing a
detector directly against a freshly exposed coal rib and it did not affect normal mining. This
phenomenon was not reported to have been observed in any other part of the mine. The accident
site was located approximately one mile west of this area. It is unlikely that the oxygen
deficiency resulted from gasses released from the coal at the August 6 accident site. No
incidents of oxygen deficiency were reported during the development or pillar recovery of that
area or immediately after the March 10, 2007, outburst accident in the North Barrier section.
It is also unlikely the oxygen deficiency was caused by oxidation of coal during the initial
catastrophic pillar failure. The oxygen level dropped from 20.9% to approximately 7.5%. Any
rapid oxidation would have generated high levels of carbon monoxide (CO) and carbon dioxide
(CO2). Gas analysis of samples collected from boreholes indicated concentrations of
approximately 140 ppm CO and 0.6% CO2. While these concentrations are above normal levels,
they cannot account for a 13% drop in oxygen levels. Also, no reports were made of any other
products of oxidation or combustion detected by instruments or smell during rescue efforts.
The areas to the north and south of the South Barrier section were both sealed at the time of the
accident. Mining had been completed and the areas were sealed for several years. Oxygen
deficiency was known to exist behind the seals in these areas, based on samples collected during
previous examinations.
During the rescue attempt, the Main West No. 1 seal was breached. Air samples were collected
of the atmosphere in the sealed area. Air samples were also collected from the Panel 13 sealed
area atmosphere at crosscut 107, the South Barrier section during the rescue attempt, and from
boreholes drilled into the inby end of the section. Table 12 shows selected results from gas
chromatograph analysis of the air samples.
142
Table 12 - Results of Air Sample Analysis
Location
Main West
Seal 1
Main West
Seal 1
Main West
Inby Seal 1
Panel 13 xc
107 seal
Panel 13 xc
107 seal
126 xc#4
Entry
126 xc#4
Entry
No 2 Entry
50 feet inby
xc 123
65 feet inby
xc 119
Borehole
No. 1
Borehole
No. 1
Borehole
No. 1
Borehole
No.3
Borehole
No.4
Date &
Time
08/12/07
20:30
08/14/07
15:00
08/16/07
14:40
01/00/00
00:00
01/00/00
00:00
08/10/07
14:00
08/10/07
15:58
08/10/07
19:15
08/10/07
19:20
08/10/07
19:25
08/10/07
16:04
08/10/07
16:07
08/10/07
21:57
08/16/07
06:00
08/18/07
19:15
H2
ppm
O2
%
N2
%
CH4
%
CO
ppm
CO2
%
C 2H 2
ppm
C 2H 4
ppm
C2H6
ppm
Ar
%
4
7.78
89.46
NDA
152
1.81
NDA
NDA
NDA
0.93
5
6.14
90.94
0.01
186
1.96
NDA
NDA
NDA
0.93
5
4.27
92.57
0.01
204
2.19
NDA
NDA
NDA
0.93
NDA
19.45
79.02
NDA
4
0.6
NDA
NDA
NDA
0.93
NDA
19.39
79.07
NDA
5
0.61
NDA
NDA
NDA
0.93
2
20.95
78.02
NDA
7
0.1
NDA
NDA
NDA
0.93
2
20.95
78.02
NDA
8
0.1
NDA
NDA
NDA
0.93
1
20.95
78.04
NDA
6
0.08
NDA
NDA
NDA
0.93
2
20.95
78.03
NDA
10
0.09
NDA
NDA
NDA
0.93
2
20.95
78.04
NDA
8
0.08
NDA
NDA
NDA
0.93
88
7.61
90.86
NDA
146
0.56
NDA
NDA
NDA
0.93
78
7.58
90.90
NDA
140
0.56
NDA
NDA
NDA
0.93
79
7.46
91.00
NDA
141
0.58
NDA
NDA
NDA
0.93
2
16.88
81.86
0.02
21
0.3
NDA
NDA
40
0.93
3
11.97
86.52
0.04
31
0.53
NDA
NDA
30
0.93
NDA = No Detectable Amount
Before and after the August 6 accident, handheld gas detectors were used to monitor gas
concentrations in the Panel 13 sealed area to the south and the Main West sealed area to the
north. Samples were drawn from pipes installed through seals. Measurements were also made
by handheld gas detectors inby the breached seal in Main West during the rescue operation.
These concentrations are shown in Table 13.
143
Table 13 - Handheld Gas Detector Concentrations
Location
Crosscut 107 Seal (Panel 13)
Crosscut 107 Seal (Panel 13)
Crosscut 107 Seal (Panel 13)
Crosscut 107 Seal (Panel 13)
Crosscut 107 Seal (Panel 13)
Crosscut 107 Seal (Panel 13)
Crosscut 107 Seal (Panel 13)
Crosscut 107 Seal (Panel 13)
Crosscut 107 Seal (Panel 13)
Crosscut 107 Seal (Panel 13)
Crosscut 107 Seal (Panel 13)
Crosscut 107 Seal (Panel 13)
Crosscut 107 Seal (Panel 13)
Crosscut 118 Center (Main West)
Crosscut 118 Center (Main West)
Crosscut 118 Center (Main West)
Crosscut 118 Center (Main West)
Crosscut 118 Center (Main West)
Crosscut 118 Center (Main West)
Crosscut 118 Center (Main West)
Crosscut 118 Center (Main West)
Crosscut 118 Center (Main West)
Crosscut 118 Center (Main West)
Crosscut 118 Center (Main West)
Behind #1 Seal (Main West)
#1 Seal (Main West)
Date
6/18/2007
6/19/2007
6/20/2007
6/21/2007
6/27/2007
7/4/2007
7/11/2007
7/18/2007
7/25/2007
8/1/2007
8/8/2007
8/15/2007
8/29/2007
6/18/2007
6/19/2007
6/20/2007
6/21/2007
6/27/2007
7/4/2007
7/11/2007
7/18/2007
7/25/2007
8/1/2007
8/8/2007
8/6/07 13:30
8/6/07 15:15
O2
1.2
20.9
20.9
1.1
0.7
2.6
0.0
0.8
0.4
0.4
20.9
7.0
20.9
20.9
20.9
20.9
10.1
20.9
20.8
20.9
20.9
20.9
20.9
20.6
6.8
8.0
CH4
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
0.0
-
Gas
CO Direction
out
in
in
out
out
out
out
out
out
out
in
out
in
in
in
in
out
in
in
in
in
in
in
out
57
out
Gas concentrations measured at the seals varied due to the pressure differential. This is typical
of sealed areas. The change in pressure differential direction is related to normal changes in
barometric pressure. All seals leak some amount and during a rise in barometric pressure air will
typically leak into the sealed area and samples will indicate higher oxygen content than
representative of the atmosphere in the sealed area. When the barometric pressure decreases, the
differential will reverse and out-gassing will occur. After enough time, samples will more
accurately reflect the atmosphere behind the seal.
The results of bottle sample analyses and handheld detector gas concentrations indicated that the
South Barrier section was bounded on both sides by sealed areas with oxygen deficient
atmospheres. Leakage of normal air from the active areas into and out of the sealed areas can
only increase the oxygen levels. Based on this fact, the most reliable samples were those with
the lowest oxygen levels taken while the sealed areas were out-gassing. Oxygen concentrations
in the Panel 13 and Main West sealed areas before the accident were near zero percent and four
percent, respectively.
144
The level of oxygen in Borehole No. 1 drilled into the South Barrier section was approximately
7.5%. Earlier samples indicated higher concentrations. This was due to problems with the
sample collection (i.e., plugged bit).
The oxygen concentrations from Boreholes Nos. 3 and 4 were approximately 17% and 12%,
respectively. These holes were drilled into the bleeder entry at the back of the section. The
higher concentration of oxygen indicated that a pocket of less contaminated air existed there.
Borehole No. 3 was drilled in that location anticipating that such a pocket of breathable air might
exist and provide a refuge for the entrapped miners. Although Borehole Nos. 3 and 4 contained
high enough oxygen concentrations to sustain life, video images taken from the boreholes
showed no indications that the miners had traveled to this area.
The most likely cause of the oxygen deficiency was a breach in the barriers separating the South
Barrier section from the sealed Panel 13 area to the south and the Main West sealed area to the
north. This conclusion is based on several factors. First, damage to the southern barrier was
observed as a rib displacement of up to 10 feet into the No. 1 entry during the rescue work.
Second, InSAR data indicates subsidence occurred over the barriers to the north and south.
Third, the rapid convergence that occurred during the August 6 accident that created the air blast
felt outby in the South Barrier section would have likely caused a similar flow of air from the
sealed areas through the damaged barriers into the South Barrier section work area.
GRI and AAI did not give proper design consideration to implications of a barrier breach inby
the working section. AAI’s analysis focused on pillar stability at the pillar line. While it was
apparent that the need for a ventilation barrier was recognized, the remnant barriers were not
designed to be stable inby the pillar line. Interview statements by AAI engineers indicated that
no consideration was given to maintaining the integrity of the remnant barrier as a ventilation
separation between the gob and the sealed area. They acknowledged that the structural
component of the remnant barrier was questionable and that it was not designed to carry the
entire load. The stability of the barriers was critical to ensure that the miners were protected
from lethally oxygen deficient atmospheres that were present in sealed workings to either side of
the section.
Attempt to Locate Miners with Boreholes
A decision to drill boreholes into the mine was made early on August 6. Seven boreholes were
drilled from the surface to the mine workings. The goal for drilling the boreholes was to locate
the entrapped miners and assess conditions in the affected area. If miners were located, the
boreholes could be used to provide communication, fresh air, and sustenance until they were
rescued. GRI and MSHA jointly decided the location for each borehole.
Boreholes Drilled Prior to August 16
Three boreholes were completed and a fourth borehole was started prior to the August 16
accident. The location chosen for Borehole No. 1 was near the kitchen/transformer area
(crosscut 138 in No. 3 entry) in the South Barrier section. This was the designated location that
miners were to gather in the event of an emergency and the location of the pager phone. The
drill rig for this borehole did not have directional controls and, as a result, intersected the mine
opening at crosscut 138 in the No. 2 entry, which was 85 feet south of its intended location.
Although the goal for this borehole was not met, the information obtained from it was useful.
This small drill rig was used to drill Borehole No. 1 because it was immediately available and
could be transported quickly to the drill site by helicopter. The mine void was 5.5 feet high at
this location. The drill rod had a 2.25-inch outside diameter and 1.875-inch inside diameter. The
145
drill rod and bit were left in the hole so that air samples could be taken through the rod’s hollow
drill stem.
Initial air samples collected from Borehole No. 1, at 12:00 a.m. on August 10, 2007, showed
20.73% oxygen. It was later discovered that the holes in the bit were clogged and the sample did
not represent the true air quality in the mine. After the bit was flushed with water, another air
sample was collected at 1:45 a.m. which indicated 8.17% oxygen. This concentration of oxygen
would cause unconsciousness in about two minutes. Two down-hole cameras were on site. One
was a four-inch diameter camera and the other a 2.5-inch diameter. Due to the small borehole
diameter of 2.4 inches, neither camera was used.
The projected mine location for Borehole No. 2 was the No. 2 belt entry at crosscut 137, in the
intersection outby the section feeder. The location for this borehole was chosen because it could
be drilled from the same drill pad as Borehole No. 1 and, therefore, could be started immediately.
This hole was one crosscut outby the location of Borehole No. 1. The mine void was determined
to be 5.7 feet. Air was entering this borehole from the surface and therefore air quality analysis
was not done at that time. Because of its proximity to the Borehole No. 1, the air quality was
likely similar at the two locations. A compressor was used to pump fresh air through the
borehole after video examination was completed.
On August 12, a camera lowered into Borehole No. 2 showed that the intersection was mostly
open. A canvas bag was observed hanging from the mine roof and the intersection was largely
free of rubble. This visual evidence reinforced the assumption that the entrapped crew might
have made their way into an area where they could survive. It was also thought that open entries
might exist inby the blockage at crosscut 126. However, additional observations on August 21
using brighter lighting and computer enhancements on August 22 revealed that while the
intersection was open, severe damage was observed in the entries. Boreholes completed after
August 16 and InSAR subsidence analyses also indicate that the collapse was more extensive
than envisioned when Borehole No. 2 penetrated the mine level. It is now concluded that in
areas of pillar collapse, the intersections may have some voids while the adjoining entries and
crosscuts were rubble filled. There was little chance for a miner to survive at the Borehole No. 2
location because of the low oxygen content observed in Borehole No.1 and because the entries
and crosscuts were partially filled with rubble from the collapse.
Irrespirable air sample results from Borehole No. 1 prompted rescue drilling in an area of the
mine where the entrapped miners could have barricaded to survive these conditions. The
location chosen for Borehole No. 3 was in the No. 4 bleeder entry of the South Barrier section at
crosscut 147 because it was considered a likely location for barricading. Also, the position for
this hole was under the area of lower cover (1,400 feet) where collapsed ground was less likely
to occur. The full entry height of 8 feet was encountered at this location. A camera lowered into
this borehole revealed that the pillars had sloughed but the entries and crosscut were open.
Analysis of an initial air sample showed 16.88% oxygen. The air quality and mine condition
indicated that a miner could survive at this location, which encouraged further rescue efforts
underground and from the surface. Borehole No. 3 also reinforced the concept that open entries
existed inby the blockage at crosscut 126. A later attempt to lower a robot into the mine through
Borehole No. 3 was unsuccessful because the borehole became blocked.
Boreholes Drilled After August 16
After underground rescue efforts were suspended, the focus turned to searching for the entrapped
miners solely by drilling boreholes. If miners were found, a special drill rig, large enough to drill
146
a 30-inch diameter hole, would be acquired to drill a hole of sufficient diameter for the mine
rescue capsule.
Borehole No. 4 was being drilled at the time of the August 16 accident. The location for
Borehole No. 4 was in the No. 4 bleeder entry, crosscut 142, of the South Barrier section, five
crosscuts outby Borehole No. 3. This location was chosen because a pattern of noise was
detected by MSHA’s seismic location system. Although this noise was considered too strong to
be signals from the entrapped miners, to be certain, the borehole was drilled at the location of the
noise. After penetrating the mine on August 18, the miners were signaled by striking the drill
steel and setting off explosive charges. No response was detected. The mine void was 4 feet at
this location. Analysis of the initial air sample showed 11.97% oxygen in the mine. A camera
lowered into the borehole revealed that the entries and crosscut were partially filled with rubble.
The air quality and mine condition indicated that there would be a very low possibility of
survival at this location. Therefore, it was concluded that the noises detected by the MSHA’s
seismic system were not made by entrapped miners.
On August 30, 2007, a robot was lowered into the mine through Borehole No. 4. The prototype
robot lacked vertical clearance and was only able to travel a short distance in the mine. It was
unable to explore the area around the borehole. No information useful to the rescue efforts was
gained from the robot.
The location for Borehole No. 5 was in the No.1 intake escapeway entry of the South Barrier
section at crosscut 133. This location was chosen because it is an area where the entrapped
miners could have tried to escape after the accident. The mine void was 0.5 feet at this location.
An attempt to lower a camera to the mine level was aborted because the borehole was blocked
with mud and water at 511 feet, more than 1,500 feet above the mine level. There would have
been no chance of survival at this location because the entry was filled with rubble.
The location chosen for Borehole No. 6 was near the last known area where mining was taking
place in the South Barrier section. The borehole intersected the mine in the No. 1 entry between
crosscuts 138 and 139. There was no mine void at this location. Based on the material
encountered during drilling, these conditions appeared to rescue workers to be similar to the
packed rubble encountered near crosscut 124 where the barrier had shifted violently into the
No. 1 entry. The material at mine level was so compacted that water flowing down the borehole
could not flow into the mine and backed up approximately 100 feet into the borehole.
Consequently, when a camera was lowered into the borehole, it encountered mud and water
approximately 100 feet from the mine level and could not be lowered any further. There would
have been no chance of survival at this location.
The location chosen for Borehole No. 7 was in the kitchen/transformer area of the South Barrier
section, No. 3 entry between crosscuts 138 and 139. This was near the area in which Borehole
No. 1 was intended to intercept the mine. A 7-foot rubble depth and a 2.7-foot void height were
encountered. An attempt to lower a camera into this borehole was stopped because water and
mud had blocked the hole approximately 9 feet from the mine level. The material at mine level
was so compacted that water flowing down the borehole could not flow into the mine and backed
up into the borehole. There would have been no chance of survival at this location because the
entry was nearly filled with rubble. After drilling the seventh borehole, a decision was made to
discontinue all drilling.
147
It was feasible to acquire a special drill rig and drill a 30-inch diameter rescue hole. However,
the rubble seen through Borehole Nos. 5, 6, and 7 showed that pillar failure was extensive in the
South Barrier section from crosscut 139 to where rescue operations began at crosscut 120.
Rescue workers lowered into the region with the rescue capsule would be forced to clear material
by hand wearing a breathing apparatus and that process could trigger another burst. The strata
above the mine were considered to be unstable with a high probability that the hole could
collapse. Evidence of the strata instability was demonstrated by the fact that some of the 8-inch
boreholes collapsed. Consequently, the rescue capsule option was considered to be too
dangerous and constituted an unacceptable risk to rescue personnel.
Decision makers at the accident site relied on limited information available from boreholes to
determine conditions in the affected area. Only one rig was used to drill boreholes after
Borehole No. 1 intersected the mine. If two directional drill rigs had been used after completion
of Borehole No. 1, five boreholes would have been completed before the August 16 accident. If
three directional drill rigs had been used, all seven boreholes would have been completed before
the August 16 accident. Greater drilling resources would have provided information sooner for
evaluating the potential success of continuing rescue efforts. Similarly, if better lighting and
camera resolution (e.g., zoom capability) had been available, decision makers would have had
more accurate and timely information.
MSHA’s Seismic Location Systems
MSHA’s seismic location system was deployed and arrived at the mine site 32 hours after the
accident. The system was operational within another twelve hours. At the Crandall Canyon
Mine, the system was near its operational limit. The depth of the mine near the accident site was
1,760 feet. The greatest depth the system has ever detected a signal was approximately
2,000 feet. This was during a test over an idle mine with ideal conditions.
The activity associated with rescue drilling interfered with the seismic location system. The
steep terrain required extensive development of roads and drill pads to support the drilling. The
earthwork and the drilling itself generated too much seismic noise to effectively monitor for any
signals from the miners. At the sensitivity required to detect miners at that depth, even vehicular
and pedestrian traffic interfered with the system. However, due to the fact that the system
response to signals is primarily vertical, the underground rescue operations, 2,400 to 1,600 feet
away horizontally, were not believed to be interfering with the system.
Because of the priority given to completion of the rescue boreholes, monitoring was essentially
limited to the quiet times established after the completion of each borehole. Drilling and surface
operations were not stopped to establish additional quiet times. A noise, which was interpreted
as not characteristic of miners, was a factor in determining the location of Borehole No. 4. No
other signals were detected. Other than the previously mentioned event, the system did not play
a role in the rescue.
A portable seismic system was used underground. The range of the system is approximately
200 feet. The trapped miners were over 2,400 feet away. The system was deployed on a water
pipe that extended towards the section in an attempt to expand the operational range. No signals
were detected.
The extent of the collapse and the atmospheric analyses from boreholes indicated that the miners
were likely incapable of signaling. If they survived the collapse, the atmosphere would have
rendered the miners unconscious unless they immediately donned their SCSR units and retreated
148
to the breathable air in the bleeder entry near Borehole Nos. 3 and 4. These boreholes did not
indicate any evidence of the miners.
Emergency Response Plan
Section 2 of the Mine Improvement and New Emergency Response Act of 2006 (MINER Act)
requires underground coal mine operators to have an Emergency Response Plan (ERP), which is
to be approved by MSHA. The ERP in effect at the time of the accident was approved on
June 13, 2007.
MSHA emphasizes that, in the event of a mine emergency, every effort must be made by miners
to evacuate the mine. Barricading should be considered an absolute last resort and should be
considered only when evacuation routes have been physically blocked. Lifelines, tethers,
SCSRs, and proper training provide essential tools for miners to evacuate through smoke and
irrespirable atmospheres.
The operator must periodically update the ERP to reflect: changes in operations in the mine, such
as a change in systems of mining or mine layout, and relocation of escapeways; advances in
technology; or other relevant considerations. When changes to the ERP are required, MSHA
approval must be obtained before the changes are implemented.
Section 2(b)(2)(B)(i) of the MINER Act requires that the ERP shall provide for the evacuation
"of all individuals endangered" by an emergency. The individuals covered by this provision do
not include properly trained and equipped persons essential to respond to a mine emergency, as
permitted in 30 C.F.R. § 75.1501(b).
The ERP established provisions for storage of Self-Rescuers, Lifelines, Post-Accident
Communications, Post-Accident Tracking, Training, Post-Accident Logistics, Post-Accident
Breathable Air, Local Coordination, and Additional Provisions. The Post-Accident Breathable
Air provision of the plan had not been implemented at the time of the accident. It was required
to be implemented within 60 days after the June 13, 2007, approval letter.
Notification
The ERP included a list of emergency responders that will be notified following an emergency:
MSHA One Call 24/7, Ambulance 911, Police 911, Castleview Hospital, Emery Medical, Poison
Control, and MSHA’s Price Field Office. The list also included names and phone numbers of
company officials, mine rescue teams, and several mine emergency equipment suppliers.
Five miners underground responded to the emergency. Soon after the accident occurred at
2:48 a.m., these men evaluated the mine conditions. They observed that numerous ventilation
controls had been blown out and the entries leading into the section were blocked. They called
Leland Lobato (AMS operator) at approximately 3:13 a.m., to relay this information and
instructed him to notify Gary Peacock (superintendent), of the mine emergency. By this time,
the underground miners making the call to the surface were aware that a mine emergency
existed. Lobato briefed Peacock with the information that he had received from the men
underground. He also told him that 18 minutes had passed since he lost communication with the
section. At 3:25 a.m., Hardee was outside in the safety office gathering self contained breathing
apparatus units that the men underground had requested. Before traveling underground he had a
brief telephone discussion with Peacock, who was at his home, to apprise him of the situation.
Peacock then called Bodee Allred (safety director) at 3:30 a.m. and apprised him of the accident.
Peacock instructed Allred to mobilize the mine rescue team and to contact MSHA, in that order.
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The call lasted five minutes. Allred called the mine rescue teams at 3:36 a.m. and MSHA’s tollfree number for immediately reportable accidents at 3:43 a.m. More than 15 minutes had
elapsed from the time that persons underground became aware of the emergency and the time
that MSHA was notified.
Bodee Allred reported to MSHA’s toll-free number operator that there was a bounce, that pillar
recovery had been occurring in the mine, that they had an unintentional cave, and that they lost
ventilation. He also reported that they did not know if it knocked out stoppings, that visibility
was poor, and that miners could not see past crosscut 92. MSHA’s toll-free number report form
indicated no injuries, no death, no fire, and no one trapped.
Self-Rescuers
The operator provided CSE SR-100, Self-Contained Self-Rescuers (SCSR) for use as required by
30 CFR Part 75 requirements. The ERP defined storage and reliability requirements for the
units. At the time of the accident, all SCSR units were located in the areas stipulated in the ERP.
Following the accident, five miners initiated a rescue attempt into the South Barrier section.
Two miners used Dräger, 30-minute, self-contained breathing apparatus units (SBAs), two used
the CSE SR-100, and one did not don any type of unit. Tim Curtis and Brian Pritt were trained
to use the SBAs as members of the mine fire brigade. Tim Harper and Jameson Ward donned
the SR-100s to cope with dust in the atmosphere. Harper and Ward stated that the SCSR units
activated properly, and performed as expected without incident. Brent Hardee did not don any
type of unit. During their attempt to advance into the section, the miners retreated after
encountering low levels of oxygen and adverse ground conditions. The lowest oxygen level
detected was 16.0%.
Post-Accident Logistics
The command center was located on the second floor of the warehouse building (AMS
dispatcher and safety office) as required by the ERP. On August 6, the command center was
established and manned by MSHA and GRI personnel to formulate the plans for the rescue
operation and to coordinate initial exploration by mine rescue teams. Later, MSHA personnel
were principally located in the MSHA mobile command center vehicle immediately adjacent to
the warehouse, while the command center in the warehouse building was primarily manned by
GRI. Both locations were linked to the underground communication system and to each other.
Joint meetings between GRI and MSHA were held twice daily and more often when necessary.
New or revised plans were formulated and approved by both groups, which would meet at either
location. Separate locations for mine operator and MSHA personnel were not typical for past
mine emergency command center operations.
The ERP detailed that the family accommodations will be located in the main shop on mine
property. However, this location was not used. On August 6, 2007, the families were
accommodated for a short time at the Senior Citizens Center in Huntington, Utah, and relocated
later that day to the Canyon View Jr. High School in the same town. On August 18, 2007,
family accommodations were established at the Desert Edge Christian Center Chapel, also in
Huntington, and remained there until August 31, 2007, when all rescue operations were
suspended.
Exceptional security and traffic control was provided by Emery County Sheriff Lamar Guymon
and his department at the mine and at family accommodation sites. The Emery County Sheriff’s
Office also provided and manned a command vehicle that was stationed on State Route 31 at the
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entrance to the mine access road. Press conferences and accommodations were provided at this
location.
The State of Utah also provided support during the rescue efforts. The Governor and his staff
met with the family members and assisted with both the media and family briefings. The
Department of Public Safety, through the Utah Highway Patrol, assisted the Emery County
Sherriff with traffic control. The Division of Homeland Security provided transportation of
supplies and equipment. The Department of Natural Resources assisted with media relations
with the Director of the Division of Oil, Gas and Mining, John R. Baza, the senior state official
on location for most of the rescue effort. The American Red Cross and the Salvation Army also
provided assistance at the mine site and to the families during rescue efforts.
Lifelines
Directional lifelines were installed in the primary and secondary escapeways from the working
section to the surface. The directional lifelines were marked with reflective material every
25 feet and had directional indicators showing the escape route at intervals no greater than
100 feet. The small end of the directional cone was facing inby. Before the accident, both
lifelines had been installed. Lifelines outby the area affected by the accident were intact. At the
edge of the collapse area, they extended inby above the rubble or were embedded into the top of
the rubble.
Post-Accident Communication
The mine utilized two independent hardwired communication systems that were located in
separate entries to provide redundant means of communication between the surface and persons
underground. Each independent system consisted of a number of pager phones installed
throughout the underground mine and linked to various locations on the surface. On the South
Barrier section, one pager phone system was located in the primary escapeway, No. 1 entry, and
the other was in the alternate escapeway, No. 4 entry. These two systems were in place before
the accident.
Although not an MSHA requirement, a Personal Emergency Device (PED) system was used as
an additional means of in-mine communication. The PED is a one-way communication system
integrated with the miner’s cap lamp battery. The AMS operator is capable of sending text
messages from the surface location to any miner that is carrying a PED unit. The receiving unit
was not capable of verifying back to the sender that a message was received nor was it capable of
transmitting messages.
The PED system was comprised of a surface computer and an underground computer/transmitter
located at crosscut 44. A loop antenna was located in the Nos. 1 and 2 entries of Main West
from the transmitter to Main West crosscut 107, to Main North crosscut 25, and back to the
transmitter, a distance of approximately 4.8 miles. While the accident on August 6, 2007,
damaged ventilation controls as far outby as crosscut 90, it did not appear that the loop antenna
was damaged. Text messages were successfully received by rescuers during the initial rescue
attempt. Because the PED system was still operational after the accident, it was likely that if the
receiving unit Don Erickson was carrying was still operational, messages would have been
received by the unit.
During the rescue operation, a two-way voice activated microphone was lowered into accessible
boreholes that were open to the mine level. The microphone was turned on each time it was
lowered into the mine void. No record was kept of exactly how long a microphone remained in
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each hole. The microphone was not removed until it was certain that no sounds of life were
heard. If a mine pager phone was located anywhere near a borehole and the phone system had
survived the accident, the microphone would have picked up any messages broadcast from the
pager phones. During the listening time, no pager phone communication was heard. The
accident involved all four entries leading into the South Barrier section. Because of the violent
nature and magnitude of the burst, it is highly unlikely that this part of the pager phone system
remained intact.
Post-Accident Tracking
The mine utilized a dispatcher system (AMS operator) to track miners underground by using a
magnetic tracking board and later an electronic spreadsheet. There were five tracking zones
from the portal to the South Barrier section. Pager phones were located at all zone intersections,
the belt head of each section, belt flight transfer points, and in the bleeder travelway. All zone
intersections were marked with placards. The magnetic tracking board was located at the AMS
operator’s station and when a person called out with their location, the AMS operator moved the
magnetic strip with their name to that location on the board. Another magnetic board was
located in a room in the underground mine office/bathhouse near the mine portal. This was used
as the check-in, check-out board required by 30 CFR 75.1715. Before entering or leaving the
mine, each person moved his/her nametag to correspond with their location. Based on company
records and interviews obtained during the investigation, the system was effective on August 6.
However, problems with the dispatcher system did occur during the August 16 accident, as
discussed later in this report.
Local Coordination
A complete list of emergency responders and their phone numbers was included in the ERP.
This list included MSHA’s 1-800 number, mine management contact information, and mine
rescue teams. The list also included contact information for mine emergency suppliers,
including: mine drilling services, mining cranes, heavy equipment, nitrogen foam and
generators, gas detection/ mine rescue equipment, and ventilation sealing services. Local
emergency responders, including airlift providers, were familiar with the mine location,
operation, and personnel.
On August 6, 2007, following the accident, Mark Toomer, AMS operator, called the Emery
County Emergency Dispatcher at 3:52 a.m., and requested that an ambulance be sent to the mine
for a possible mine emergency. The ambulance arrived on mine property at 4:22 a.m. escorted
by an officer from the Emery County Sheriff’s Office. The ambulance remained at the mine that
day but was not needed.
Training
Training was provided in accordance with the ERP. The miners and mine managers who were
interviewed were familiar with the ERP requirements and the operator’s records documented that
the required training was completed.
Post-Accident Breathable Air
The plan described the locations in the mine where post-accident breathable air is to be provided.
It also discusses oxygen consumption rates, air supply, purging of the safe haven barricade,
chemicals used for scrubbing carbon dioxide, and a map identifying locations of the supplies.
The post-accident breathable air provisions were not required until 60 days following approval of
the ERP, which was approved on June 13, 2007. At the time of the accident, the post-accident
breathable air provisions of the ERP had not been implemented.
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On August 9, 2007, the operator ordered two Strata Emergency Air/Barricade Skids, one 32-man
unit and one 11-man unit from Strata Safety Products, LLC, of Jasper, Alabama, as documented
by a purchase order. Delivery was expected in April 2008.
Additional Provisions
The plan identified additional materials that must be stored on an Emergency Materials Skid
and/or trailer and its location. Some of these materials included: a first aid kit, roof jacks or
timbers, wedges, tools, brattice material, and foam packs. A complete list was detailed in the
approved ERP. The operator provided information showing that the skid was located near
crosscut 122 and later moved to crosscut 113.
Family Liaisons
Under Section 7 of the Mine Improvement and New Emergency Response Act of 2006 (MINER
Act), the Secretary of Labor established a policy that required the temporary assignment of a
Department of Labor official to be a liaison between the Department and the families of victims
of mine tragedies involving multiple deaths. It also requires MSHA to be as responsive as
possible to requests from the families of mine accident victims for information relating to mine
accidents. In addition, it requires that in such accidents, MSHA serve as the primary
communicator with the operator, miners’ families, the press, and the public.
MSHA personnel were assigned as family liaisons to establish communication with the victims’
families. They were: William Denning, District 9 Staff Assistant; Carla Marcum, District 7,
Specialist; Robert Gray, District 10, Health Supervisor; and Richard Laufenberg, Metal/NonMetal Rocky Mountain District, Assistant District Manager. These individuals were specially
trained by the National Transportation Safety Board to serve as family liaisons between MSHA
and families during mine accidents involving fatal injuries or where miners are unaccounted for.
They maintained constant contact with family members and met with them for regular briefings
to provide updates and answer questions. These designated family liaisons were assisted by
other MSHA personnel in support of the victims’ families’ needs. Also, the Assistant Secretary
of Labor, the Administrator for Coal Mine Safety and Health, and the District 9 District Manager
played key roles communicating with the operator, miners’ families, the press, and the public.
MSHA’s Lead Accident Investigator regularly conducted family briefings in person and by
telephone during the weeks and months following the accident. These briefings provided the
families an opportunity to follow the progress of the investigation, to ask questions and to
contribute any information to the investigation.
Mine Emergency Evacuation and Firefighting Program of Instruction
Section 30 CFR 75.1502 requires each operator of an underground coal mine to adopt and follow
a mine emergency evacuation and firefighting program that instructs all miners in the proper
procedures they must follow if a mine emergency occurs. MSHA approved the Mine Emergency
Evacuation and Firefighting Program of Instruction (Program) on March 16, 2007. This
Program must be reviewed with all miners annually and with newly employed miners prior to
assignments of work duties in accordance with 30 CFR Part 48.
The Program includes provisions for: fire, explosion, water and gas inundation emergency
procedures; location and use of fire-fighting equipment; location of escapeways; exits and routes
of travel; evacuation procedures; fire drills; SCSR location, use and storage; AMS fire detection;
operation of fire suppression equipment; mine emergency evacuation drills; two-entry response
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parameters, and mine emergency scenarios. Portions of the approved Program relevant to the
August 2007 accidents are discussed in the following sections of this report.
Procedures for Evacuation
The Program stated in part, “The proper evacuation procedures shall be initiated by the
Responsible Person who has current knowledge of assigned locations and expected movement of
miners. This Responsible Person shall also be knowledgeable in escapeways, mine
communications, mine monitoring systems, mine emergency evacuation, firefighting program of
instruction, and all personnel qualified to respond to emergencies.” The Program did not
specifically identify the Responsible Person by name or title, but clearly defined their duties and
responsibilities. In practice, the shift foreman was typically identified as the Responsible Person
for each shift. A nameplate located above the mine check-in/check-out board identified this
specific person each shift. If the Responsible Person changed during the shift, all miners were
notified before the start of the shift when this change was to occur. The Program did not define
the physical location of the Responsible Person during the shift.
The Responsible Person on the night shift, August 5/6, (6:00 p.m. to 6:00 a.m.) was Gale
Anderson. Anderson, Benny Allred, and Powell were scheduled to attend training on August 6,
and would not have been working their entire scheduled shift. Therefore, Anderson designated
Don Erickson to act as the Responsible Person during his absence. Anderson, Benny Allred, and
Powell exited the mine around 9:00 p.m. and left the mine property sometime after 10:00 p.m.
The program stated, “the procedure for rapid assembly and transportation of persons necessary
to respond to the specific mine emergency, emergency equipment, and rescue apparatus to the
scene of the emergency shall be initiated, by the responsible person in charge, who will notify the
mine rescue team so that equipment can be assembled”. Erickson, working in the South Barrier
section, was one of the six miners entrapped in the section and, therefore, was not able to
respond as the designated Responsible Person.
Leland Lobato (AMS operator) was stationed on the second floor of the shop/office building
which was located several hundred yards from the mine opening. His assigned duties included
monitoring the AMS and underground mine communication systems, along with documenting
the location and movement of miners. On August 6, Lobato was training Mark Toomer as a new
AMS operator.
There were five miners underground at the time of the accident in addition to the six miners in
the working section. Peacock talked with them from his home through the AMS operator. An
evacuation of the mine was not ordered because all miners underground were needed to assess
post accident conditions and restore ventilation.
Atmospheric Monitoring System (AMS) Fire Detection
The primary function of the AMS system was fire detection with sensors capable of detecting
levels of carbon monoxide. The system also continuously monitored mine electrical power,
mine conveyor belts and tonnage, and fan operation. The accident did not involve fire or
explosion. Therefore, none of the sensors detected alert or alarm levels of carbon monoxide. A
requirement of the system is that it shall automatically provide visual and audible signals at the
designated surface location for any interruption of circuit continuity and any electrical
malfunction of the system.
The system functioned properly at the time of the August 6 accident. After the accident, the
system alarmed and recorded a communication failure for all sensors located from the No. 6 belt
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drive inby including the working section. The main fan continued operating during the entire
event without interruption but the AMS system did record a change in pressure.
Training Plan
The approved Part 48 Training Plan was reviewed to verify that the plan met the requirements of
30 CFR 48.3. The plan included all required subject matter. An addendum to the plan included
Mine Emergency Evacuation instructions for the donning and transfer of self-rescue devices.
The training records required by 30 CFR 48.9 were reviewed for all miners employed at the
Crandall Canyon Mine at the time of the accident. Based on this review and interviews
conducted during the investigation it was determined that training met the requirements of
30 CFR Part 48.
August 16 Accident Discussion
The August 6, 2007, accident rendered all entries to the working section inaccessible and there
was no further communication with the crew of six miners working there. Burst coal filled or
partially obstructed mine openings, blocking all approaches to the section. The force of the burst
damaged roof supports in some locations and the associated air blast damaged stoppings over a
broader area.
There is no record 17 of a disaster of this type in the last 50 years of U.S. mining history. The
miners were located beneath 1,760 feet of overburden in rugged terrain with difficult access.
MSHA’s mine rescue capsule, which had proved effective at the Quecreek #1 Mine in 2002, had
never been deployed at such depth. The miners also were separated from coworkers
underground by approximately 2,400 feet of rubble-filled entries. An underground rescue
through this type and extent of failed ground was unprecedented.
While surface drilling efforts were being initiated to locate the entrapped miners, plans were
formulated for an underground rescue effort. The underground rescue work involved
reestablishing ventilation, clearing a travelway through the failed pillars, and re-supporting the
roof as necessary. The degree of ground failure was so extensive that the clean-up effort began
at crosscut 120 of the South Barrier section. The repair of ventilation controls began more than
one mile from the entrapped miners.
Initial efforts to reach the miners via the No. 4 entry progressed only 300 feet before a burst
occurred that refilled much of the path that had been cleared. No one was injured, but the
occurrence emphasized the need to provide rescue workers some form of protection against
further bursts. The subsequent rescue plan relocated the effort to the No. 1 entry and
incorporated several elements to mitigate the burst hazard.
Standing supports were installed on either side of the No. 1 entry. They were placed outby for a
distance of several hundred feet before recovery work began and then they were installed behind
the clean-up face as it advanced. Initially, wood timbers were used in conjunction with a
hydraulic pre-loading device to wedge them between the roof and floor. However, they were
only used for a distance of about 200 feet, when another form of hydraulically wedged standing
support, RocProps, was employed. As clean-up advanced in the No. 1 entry, a number of
changes were implemented to enhance the support system and/or to reduce worker exposure.
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Advance rate in the No. 1 entry between August 8 and 12 was somewhat erratic but afterward
became relatively consistent at about 65 feet per day. The haul distance between the clean-up
face and the belt feeder increased as the clean-up advanced. Also, the amount of debris
encountered in the No. 1 entry increased substantially. In some areas between crosscuts, the
barrier side rib was observed to have moved up to 10 feet into the entry. The entry was
completely filled and had the appearance of a previously unmined face. In some areas, roof bolts
had been sheared and/or damaged and hazardous roof conditions were encountered. Despite all
these issues, rescue workers managed to find efficient means to overcome the problems they
encountered and maintain a steady rate of progress. Although some bounces were noted, the
support system was effective in containing coal dislodged from the ribs.
The first surface borehole penetrated the mine workings inby the collapse at 9:58 p.m. on
August 9. Information that the mine atmosphere contained only about 8% oxygen was not
encouraging. However, the rescue effort continued with the prospect that the miners could have
escaped to another area of the mine with a favorable atmosphere or that they may have
barricaded safely. Air quality could not be evaluated at Borehole No. 2 when it penetrated the
workings at 12:57 a.m. on August 11. However, the presence of a 5½-foot void at mine level
(similar to the void at No. 1) provided encouragement that perhaps the burst had not affected the
mine openings in the area where the miners had been working.
Between August 10 and 13, the reported location of bounces and bursts was somewhat mixed
(i.e., at the clean-up face, outby crosscut 120, away from the No. 1 entry and unknown).
However, from August 13 to 16, the reports indicated that the activity was most often associated
with areas outby the fresh air base (FAB) at Crosscut 119. Changes in roof conditions also were
noted outby the FAB and, in response, additional standing supports were installed and an array
of convergence stations was established to monitor ground behavior. Bursts occurred in the
clean-up face periodically but were either at the continuous mining machine inby the RocProps
or they were contained by the RocProps.
Subsequent analyses of satellite images and information gained from later surface boreholes
revealed that the degree of damage encountered in the No. 1 entry would have worsened
substantially before the rescuers reached the last known location of the miners. However, this
information was not available on August 16. At that time, rescuers were operating under the
premise that the worst conditions were likely associated with the overlying ridgeline (i.e., the
greatest overburden depth). Calculations at the time were consistent with that premise. It was
anticipated that the conditions observed on the outby side of the collapse would correlate to
conditions under similar overburden on the inby side. Thus, there was hope that the miners had
not been subjected to the effects of bursting coal and could have retreated to a safe area. This
hope was bolstered when, at 10:11 a.m. on August 15, Borehole No. 3 penetrated 8 feet high
workings that contained 17% oxygen.
At 10:04 a.m. on August 16, a burst occurred in the clean-up area that filled the entry between
the continuous mining machine and the pillar rib to a depth of approximately 2½ feet. No one
was injured and the event did not displace the support system. The debris was cleared and the
clean-up cycle continued. A gradual opening encountered in the recovery face on August 16 was
perceived as an indication that a travelable opening might be encountered soon. Efforts were
initiated to prepare a mine rescue team to enter the area if that opportunity arose. Neither the
burst that occurred at 6:38 p.m. on August 16 nor the associated failure of the support system
was anticipated.
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Ground Control during Rescue Efforts
Pillar bursting in the South Barrier filled or partially obstructed entries up to 20 crosscuts outby
the pillar line. The force of the burst damaged roof supports in some locations and the associated
air blast damaged stoppings over a broader area. Thus, the underground rescue work involved
reestablishing ventilation, clearing a travelway through the failed pillars, and re-supporting the
roof as necessary.
Selection of Entry for Rescue Work
Initial efforts to reach the entrapped miners were focused on clean-up in the Nos. 3 and 4 entries.
The August 7 burst forced the rescue effort to be temporarily halted until another plan could be
developed. A revised plan was proposed by the mine operator and approved by MSHA the
evening of August 7, 2007. This plan relocated the rescue operation from the No. 4 entry to the
No. 1 entry (see Figure 3). After the August 7 burst, the Nos. 3 and 4 entries were refilled to a
depth of at least 6 ½ feet inby crosscut 120 (see Figure 4) and the roof continued to work (make
noise indicative of continued failure) to the north and outby this location. In contrast, coal depth
and rock noise were less in the No. 1 entry. Also, recovery in the No. 1 entry allowed rescue
work to be conducted in intake air with air returning in the Nos. 2, 3, and 4 entries.
The initial rescue effort in No. 4 entry provided little protection against hazards related to coal
bursts. However, the August 7 event heightened the rescuers’ awareness of the potential for
further ground failure. In response, the operator proposed and MSHA approved a plan to
mitigate the hazard. One element of the plan was the support system installed concurrent with
advance. This system was intended to protect workers should a burst occur. Additional
elements were intended to reduce the likelihood of bursts. For example, precautions were taken
to minimize the disturbance of failed pillars. Clean-up was limited to the minimum width
necessary to allow the support system to be installed. Clean-up was limited to one entry and
crosscuts were occasionally cleared to provide space for personnel or equipment.
Intuitively, the No. 1 entry could have been perceived as a poor choice for the rescue effort. As
discussed earlier, abutment stress levels typically are highest near gob areas. Since the No. 1
entry is nearest the mined-out longwall panel 13 south of Main West, it could be assumed that
the pillar between Nos. 1 and 2 entries would be the most highly stressed and most burst-prone.
However, observed ground conditions were inconsistent with this expectation. Pillar damage on
the outby edge of the collapsed area appeared to be more severe near the Main West entries and
better near the barrier. In choosing the No. 1 entry, it was noted that the 121-foot wide barrier
beside the No. 1 entry had a width-to-height (W/H) ratio of 15. In contrast, the minimum 55-foot
wide barrier (measured to the Main West notches) adjacent to No. 4 entry had a W/H ratio of
approximately 9. Historically, pillars with W/H ratios in the range of 5 to 10 have been
associated with bursts.
As the mine operator prepared to advance in the No. 1 entry, MSHA performed ARMPS
and LaModel analyses. These analyses were done to gain insight to the mechanics of the
failure and to estimate the extent and severity of poor ground conditions likely to be
encountered during the rescue. Both LaModel and ARMPS models showed that pillars
throughout the Main West area (including the North and South Barrier sections) may
have been involved with the failure that had occurred on August 6. The results were
supported by descriptions of bursting in the North Barrier section, pillar damage observed
during the August 7 exploration inby the Main West seals at crosscut 118, and reports of
substantial floor heave outby the South Barrier section pillar line in the vicinity of
crosscuts 138 to 140.
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GRI furnished a map to MSHA during the rescue effort on which topography was slightly
shifted out of position over the mine workings. This map was used to note the general
positions of valleys and ridges during rescue operations. However, this map was not used
as a basis for any detailed analysis.
On the basis of engineering analyses and underground observations, MSHA considered
on August 9 that the South Barrier failure most likely could be attributed to instability
within the large expanse of nearly equal size pillars created by mining in Main West and
the adjacent north and south barriers. Progressive pillar failure was thought to have
occurred within the Main West pillars inby the seals at crosscut 118 under the deepest
overburden along the East Mountain ridge. MSHA surmised that the failure of Main
West would have shifted load onto the South Barrier section pillars and that this load
could have generated the extensive failure in the South Barrier section. Analyses
available at that time indicated that it was possible that the burst originated under the
deepest cover of the East Mountain ridge and that the miners, who were located under
shallower overburden, may not have been subjected to the extensive pillar burst.
However, the potential effects of the air blast on the entrapped miners’ location could
have been worse than the air blast that propagated outby (eastward).
Information gained from the first three surface boreholes drilled into the mine supported the
belief that the inby extent of the burst was limited. These holes penetrated the mine workings
between the evening of August 9 and August 15. Each one provided an initial indication that a
substantial height of entry was open at mine level. Estimated opening heights ranged between
5.5 and 8 feet. At that time, clean-up in the No. 1 entry progressed under the assumption that
total blockage of entries would be limited to the highest overburden between crosscuts 126 to
132 and the effects of the burst inby crosscut 137 may not have been as severe. Holes completed
after August 16 indicate that this assumption was overly optimistic. Subsequent analyses of
satellite images and information gained from later surface boreholes revealed that the degree of
damage encountered in the No. 1 entry would have worsened substantially between Crosscut 132
and the last known location of the miners.
Work Procedures under Operator’s Recovery Plan
The rescue effort was a dynamic process. The work procedures and corresponding plan
approvals underwent numerous changes to minimize exposure to miners, improve efficiency, and
improve the effectiveness of the support system. The number of miners working in the clean-up
area was reduced. Work processes were adjusted and refined to efficiently excavate material and
install the required ground support. Supports for burst control were reinforced through the
installation of additional of steel cables and roof control was maintained by installing additional
roof bolts, roof mesh, and steel channel where required.
Timely access to the entrapped miners in the South Barrier section work area required the
rehabilitation of debris filled, previously mined entries of the South Barrier section or Main
West. There were no alternative routes. To reach the entrapped miners required removing coal
debris from entries within damaged pillars. This unavoidable process required removal of
compacted coal that reduced the confinement around damaged pillars. Consequently, this led to
working in the vicinity of ground with high burst potential.
The most rapid method of advance in the No.1 entry required the implementation of typical coal
mining methods using the most available coal mining equipment. No other means of excavation
was available to quickly reach the miners. Remote means of excavating the debris filled entry
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was available through the use of the remote control continuous mining machine. However,
during the rescue work in the No. 1 entry, the RocProps and associated chain-link fence and steel
cables, which were advanced behind the continuous mining machine, had to be installed
manually. This process required working and traveling in close proximity to ground with high
burst potential. No methods were available to remotely install the ground control system.
Pillar Burst Support System
After the August 7, 2007, burst in the No. 4 entry, support systems were used to protect rescue
workers from additional pillar bursts. Standing supports installed on either side of the No. 1
entry were an integral part of these systems. They were placed outby for a distance of several
hundred feet before recovery work began in the No. 1 entry and then installed behind the cleanup face as it advanced.
All forms of standing support used in the U.S. coal mining industry primarily are designed to
support the mine roof. The stated capacity of these supports refers to their ability to sustain
vertical roof loads rather than lateral loads. The lateral load-carrying capability of the installed
supports was unknown as was the force that the supports would be required to resist. It was
known, however, that the RocProps could be installed with a substantial preload, the mine
workers were familiar with their installation, and they had been used successfully for protection
from burst hazards at another mine. Other support systems including arches and steel sets were
considered. However, at the time RocProps were chosen to be used in the rescue, planners were
unaware of any preferable alternative to RocProps in terms of versatility, availability, worker
familiarity, and installation exposure. No other support system capable of withstanding
significantly greater lateral loading was available. A NIOSH ground support specialist familiar
with the testing and evaluation of underground mining support systems was consulted regarding
support systems that could be used in this application. RocProps were also suggested
independently by the NIOSH specialist.
The mine operator submitted and MSHA approved a plan to install a support system that
included standing supports. Initially, posts (6 x 8-inch hardwood) were used in conjunction with
Jackpots, hydraulic preloading devices, to wedge them between the roof and floor. Once inflated
with high-pressure water through a non-return valve, the Jackpots provided a preload that
improved the wood posts ability to close cracks in the roof and secure any loose rock, reduce the
likelihood of ground falls, and provide resistance to lateral loading. Wood posts were only used
for a distance of about 200 feet, when another form of hydraulically wedged standing support,
RocProps, was employed.
A RocProp is a hydraulic cylinder that also provides an active preload when it is inflated using
high pressure water. During the rescue effort, a hose was connected from a high pressure pump
to the injection nozzle at the base of the RocProp. A control valve was opened allowing water
into the cylinder. The water pressure telescoped the inner tube until the RocProp was against the
mine roof and self-supporting. From a safe position, the RocProp was further pressurized until a
setting pressure of between 1,100 and 1,200 psi was achieved. The control valve was closed to
maintain the required setting pressure and a cone shaped locking ring was hammered into place
with a cone-setting tool. The setting tool was positioned around the RocProp and the cone was
driven into the flare of the outer tube to complete installation. The pump was powered by
tapping into the hydraulic system of the continuous mining machine, shuttle car, roof-bolting
machine, or Ramcar by using quick connect/disconnect couplings.
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During most of the rescue work in the No. 1 entry, RocProps were a primary component of the
support system. They were installed on 2.5-foot centers, typically one at a time, one side of the
entry and then the other, until all of the required roof-to-floor supports were set. The spacing
between supports on opposite sides of the entry was established at 14 feet. This dimension was
considered the minimum that would allow equipment to tram to and from the clean-up face.
This limited entry width was maintained in an effort to minimize the disturbance to the burst
pillars on either side. Opening height varied in the recovered entry. However, RocProps were
available to accommodate various mining heights.
After a series of RocProps was installed, chain-link fencing was installed on the rib side of the
RocProps to contain sloughed or burst coal. Periodically, 5/8-inch diameter steel cables were
installed on the travelway side of the RocProps to contain the RocProps and fencing in the event
of a larger burst event. Three cables were installed on the travelway side of the RocProps at the
top, middle, and bottom. Each cable connection or loop was secured with three cable clamps.
The cable was wrapped around one RocProp every 40 feet and connected to itself. Each cable
was anchored to a separate RocProp (Figure 88). The RocProps and associated chain-link fence
and steel cables were advanced behind the continuous mining machine.
Figure 88 – Steel Cables Connected to RocProps
When damaged roof bolts were encountered or the roof showed signs of fractured conditions,
additional roof bolts, wire roof mesh, and/or steel channels were installed. Occasionally,
channels spanned the entry and were supported on either end using RocProps or wood posts.
They also were installed using fully grouted roof bolts. A twin-boom walk-thru roof-bolting
machine was utilized to install the roof bolts, mesh, or channels if it was necessary (Figure 89).
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Figure 89 - New Roof Bolts and New Wire Mesh Installed in the No. 1 Entry
As clean-up advanced in the No. 1 entry, a number of changes were implemented to enhance the
support system and/or to reduce worker exposure. For example, a 4 x 8-foot sheet of ½-inch
thick Lexan 18 was provided near the face to offer protection to rescue workers in the clean-up
area. The sheet was secured to the mine roof by chains attached along one edge. The chain was
connected to roof bolt plates (Figure 90). The Lexan sheet served as a shield between personnel
and the coal pillar rib.
Figure 90 - Sheet of Lexan Suspended from Mine Roof
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Seismic Activity Recorded by UUSS during Rescue Efforts
After the August 6 accident, seismic activity continued regularly for approximately 37 hours (see
Figure 32). During this period, miners reported a substantial amount of rock noise emanating
from the area north and west of the accessible portion of the South Barrier workings. One of
these events recorded by UUSS was related to the August 7 coal burst that ended the rescue
operation in the No. 4 entry. No further seismic events were recorded until August 13, 2007,
when seismic activity was recorded at the inby edge of the collapse area (over 2,000 feet west of
the clean-up area). In a presentation before the Utah Mine Safety Commission on November 11,
2007, Dr. Walter Arabasz noted a “5.8 day gap between August 7 and 13 for events above the
threshold for complete detection of magnitude (MC) 1.6.” A general reduction in activity was
observed underground during this time period as well.
On August 15, 2007, at 2:26 a.m., a seismic event occurred that was related to a burst in the
clean-up area, inby crosscut 125 in the No. 1 entry. Another seismic event was recorded at
10:04 a.m. on August 16, which was related to a burst in the clean-up area, inby crosscut 126 in
the No. 1 entry. The next recorded seismic event was related to the August 16 accident at
6:38 p.m.
Bounces and bursts were observed underground throughout the rescue effort. Most of these
occurrences were not in the seismologic record due to the reporting threshold of the network.
The UUSS seismic network was set to record only events larger than approximately magnitude
1.6. After additional seismic stations were installed between August 9 and 11, 2007, the
threshold was reduced to approximately magnitude 1.2. Some smaller events were recorded
concurrently with a larger event that had triggered the system.
Initial locations of seismic events lacked sufficient accuracy to be used for decisions affecting
rescue efforts. Figure 91 shows the initial locations generated by the UUSS automated system.
The red circle depicts the August 6 accident. The blue circle depicts the August 16 accident.
The remaining magenta circles depict those events recorded between these accidents. All events
plot in regions away from the underground rescue work. The more accurate locations of events
shown in Figure 92 were not available until well after the rescue efforts had been suspended.
Underground observations were much more representative of actual ground activity.
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Figure 91 - Initial Location of Seismic Events August 6-16, 2007
Figure 92 - Double Difference Locations of Seismic Events, August 6-16, 2007
(unavailable until November 2007)
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Pillar Bounce and Burst Activity during Rescue in No. 1 Entry
The command center log book noted bounces and bursts from August 6 through August 16.
Protocol to qualify an event’s significance for reporting purposes, which could range from a
noise generated by a mild bounce to a coal burst, was not clearly established. Rescue workers
called and reported such events to the command center based on varying individual perceptions
of the event’s significance. Reporting was also dependent on whether or not the individual was
in the vicinity of the event. With these constraints, the recorded bounce and burst activity can
only be discussed in general terms.
Forty-one events were reported by underground personnel during rescue work in the No. 1 entry
prior to the August 16 accident. All bounce activity, which included bursts, originated from the
section pillars to the north of the No. 1 entry. None was associated with the barrier to the south.
The majority of these bounces or bursts were outby crosscut 120 (see Figure 93). This area was
outby the crosscut leading to the feeder, away from the clean-up operation in the No. 1 entry (see
Figure 3). The rescue work area was protected with RocProps or wood posts with Jackpots. Rib
deterioration and bursts that occurred outby the clean-up area were contained by the support
system.
Figure 93 – Bounce or Burst Activity Recorded in Command Center Log Book
August 8 to August 16, Prior to August 16 Accident
Prior to the August 16 accident, eleven burst/bounce events were reported to have originated
from the north side (right side) section pillars inby crosscut 120 (see Figure 93). These events
occurred at the remote-controlled continuous mining machine where the material was being
loaded, inby the area of the advancing RocProp system. The approved clean-up plan included
procedures that minimized exposure of rescue workers in this area. It was thought that if a
significant pillar burst were to occur, it most likely would be in the area where material was
being removed. The command center log book noted that events in the clean-up area varied in
size with two large pillar bursts in this area recorded prior to the August 16 accident. Prior to
August 16, no significant bounces or bursts were recorded within the RocProp support system
inby crosscut 120. One burst event was noted outby crosscut 120. Material piled behind the
chain-link fencing inby crosscut 120 resulted from unreported bounces or bursts, or from rib
sloughage.
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The rescue advance in the No. 1 entry achieved a somewhat steady rate of approximately ½
crosscut (65 feet) per day after August 12 as illustrated in Figure 94. No correlation to rescue
advance rate in the No. 1 entry and the burst or bounce frequency could be identified.
Figure 94 - No. 1 Entry Rescue Clean-up Progress Plotted by Day
On the evening of August 16, a large burst originated from the north side of the No. 1 entry. The
burst dislodged the installed RocProps, steel cables, and chain-link fencing, violently throwing
the debris and the support system from one side of the entry to the other. It happened at a time in
the rescue work cycle where the maximum number of personnel was in the area. This accident
resulted in six injuries and three fatalities.
The August 16 accident confirmed that potential energy remained in the damaged pillars. The
level of ground activity in the No. 1 entry from August 8 to 15 did not provide a clear indicator
of pillar stability. The lack of ground activity could have indicated either that the pillars were
stable or that hazardous unreleased energy remained in the pillar. Likewise, substantial activity
could have indicated that the pillars are remaining stable as they release energy, or that a
hazardous event is pending. Therefore, analysis of underground observations and frequency of
bounce or burst activity (Figure 93) offered little useful guidance on potential for bounces and
bursts. Because of the magnitude of the pillar burst and the failure of the roof-to-floor support
system, all underground rescue activity was suspended. The 103(k) order was modified
requiring all personnel to remain outby crosscut 107 in Main West.
Ground Condition Monitoring
During the rescue operation, underground observations and convergence measurements were
used to assess the stability of the areas that rescuers worked in or traveled through in the South
Barrier section. These monitoring activities identified areas requiring supplemental support but
failed to anticipate the burst that occurred on August 16. Measurements and visual observations
did not indicate that failure was imminent and the rescue activity should be suspended.
The burst that occurred on August 7 during the initial clean-up effort in No. 4 entry had
demonstrated that additional local bursting could occur as a travelway was reestablished. The
event illustrated that, despite their fragmented appearance, pillars within the burst area still were
capable of violent failure sufficient to cause injury. Although specific conditions that might be
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indicative of an impending burst were not known, MSHA and GRI personnel remained alert to
any changes in the work environment as the clean-up progressed. MSHA positioned an
inspector at the clean-up face at all times to visually monitor conditions and observe work
practices. Usually these MSHA personnel were from the Price, Utah, Field Office since these
inspectors had knowledge of the mine, regional mining conditions and practices, and burst
hazards in general. An MSHA inspector also was stationed each shift at the FAB phone at
crosscut 119 and another took air measurements at various locations throughout each shift.
As the clean-up effort advanced between August 8 and 11, the amount of debris encountered in
the No. 1 entry increased substantially. In some areas, roof bolts had been sheared and/or
damaged and hazardous roof conditions were encountered. The bolt damage in some instances
was associated directly with movement of the barrier-side rib. This rib line was observed to have
moved horizontally up to 10 feet into the entry. The displaced coal was much different in
appearance than ribs encountered to that point. Whereas most burst ribs had a loose, fragmented
appearance, the barrier-side rib appeared to be more intact and remained nearly vertical as cleanup progressed. Initially, the competent appearance of the coal raised concerns that it might be
more capable of storing strain energy that could be released as a burst event. However, as cleanup continued, bursts were observed to originate from the pillar-side rather than the barrier-side.
On August 11, GRI and MSHA mapped pillar damage east of the Main West seals (see Figure
26). The damaged pillar ribs were sloughed due to abutment stress from failed pillars to the
west. Earlier, a substantial amount of rock noise had been noted in this area, but on August 11, it
was relatively quiet. Thus, it was determined that the ground stress had stabilized and that pillar
failure was no longer progressing eastward. Roof deterioration and slight widening of roof joints
was observed in the No. 1 entry outby crosscut 117. Roof-to-floor supports were installed
through this area and steel channels were installed where adverse roof conditions were present.
On August 12, observations of RocProps tilted from vertical had prompted the MSHA inspector
positioned at the clean-up face to install a measurement point to monitor RocProp horizontal
movement. The measurement was taken routinely between RocProps installed on opposite sides
of the No. 1 entry between crosscuts 123 and 124. Between August 12 and 13, the horizontal
distance between the RocProps decreased by ½ inch across the ~13 ½-foot opening. From
August 13 to the last measurement on August 15, no further movement was noted,
Between August 12 and 15, clean-up progressed steadily but there was an increasing number of
reports of rock noise emanating from locations outby crosscut 119 and roof cracks were observed
between crosscuts 115 and 119. These observations raised concerns that a roof fall could occur
outby the rescue workers and that additional pillar failure could be responsible for the changing
conditions. MSHA installed 10 roof-to-floor convergence stations (at crosscuts 111, 113, 115,
117, and 119 in the No. 2 and No. 4 entries) to assess ground behavior.
Each convergence station was established between two points on the mine roof and floor. Roof
bolt heads were identified at specific locations to serve as measurement points on the roof.
Directly beneath each roof bolt, a ⅜-inch diameter hole was drilled to accept a plastic anchor and
a ¼-inch diameter screw that served as the measurement point on the floor. Spray paint and
survey ribbon were used to identify the monitored locations. Convergence measurements were
taken using a telescoping rod, shown in the photograph on the left side of Figure 95. This
instrument, manufactured by Sokkia, can extend up to 26 feet and is capable of determining the
distance between roof and floor points to within one millimeter.
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Figure 95 - Convergence Measurements
Left: Roof-to-floor convergence station. Right: RocProp convergence station.
The convergence stations were monitored to determine the magnitude, rate, and distribution of
roof-to-floor closure. Historically, measurements of this type have been useful in monitoring
changing and potentially hazardous ground conditions. Initial (baseline) measurements were
taken on August 15 and the stations were measured twice on August 16 prior to the accident.
Measurements in this time frame indicated that ground conditions were stable; three of ten
stations showed closures of 0.04 inches but this amount of displacement is within the precision
of the measuring instrument.
Sixteen monitoring locations were established using RocProps in the No. 1 entry. As shown in
the photograph on the right side of Figure 95, these monitoring locations were established by
painting a line on installed RocProps, 12 inches above the locking ring. Entry convergence
could be monitored at these locations simply by measuring the distance between the lock ring
and paint line using a tape measure. Although not as exact as a convergence rod, these
measurements were intended to provide a convenient method for determining convergence
between the mine roof and floor that anyone with a tape measure could perform.
The RocProps designated for measurement stations extended from crosscut 116 to 126 in the
travelway to the clean-up area. No convergence stations had been established inby crosscut 126,
near the August 16 accident site, because the area had just recently been cleaned and supported
before the accident. The RocProp stations were measured twice on August 16, prior to the
accident, and indicated stable conditions. No closure was noted at 14 of the 16 measurement
points. One RocProp near crosscut 126 showed 1/16-inch of closure and another near crosscut
121 showed 3/16-inch. Subsequent measurements by the accident investigation team on
September 10 indicated that additional vertical closure had occurred in eight RocProps. Seven of
the eight moved 1/8 inch or less while closure on the RocProp at crosscut 123 measured ½ inch.
Two RocProps located farther inby at crosscuts 124 and 125 showed no additional closure.
Ventilation on August 16
During the rescue operation on August 16 the clean-up area was ventilated with line curtain.
Oxygen deficiency, as low as 14%, was detected inby the continuous mining machine earlier that
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day. When the accident occurred, the line curtain was damaged and buried in coal. Multi-gas
detectors carried by victims and the rescuers began to alarm. The lowest oxygen concentration
was generally observed on the north side of the entry, away from the victims. Repairs to the line
curtain began as rescuers continued removing debris to free the injured miners. Ventilation was
reestablished in a short time.
An oxygen deficient atmosphere was present in the rubble in advance of the continuous mining
machine. The ventilation system had diluted and carried away gasses that had migrated into the
workplace. The accident damaged the ventilation system and may have pushed additional
oxygen deficient air onto the accident site. During the exploration on the morning of August 6,
16% oxygen was detected in the area explored near crosscut 126. The lowest oxygen
concentration reported after the accident on August 16 was 14.7%. The presence of oxygen
deficient air and the need to reestablish ventilation diverted resources from the rescue effort for a
short time, however, no ill effects were reported from the oxygen deficient air.
Post-Accident Tracking
The mine tracking system was changed on August 11, 2007. The new system eliminated the use
of the magnetic tracking board and was replaced with a computer spreadsheet. This system
functioned identically to the magnetic board with the exception that it provided a printed copy of
each person’s underground location every hour. In addition, the check-in, check-out procedure
was supplemented by having each person write their name, date, and time they entered and
exited the mine in a log located at the portal.
On August 16, 2007, the post-accident tracking system was not maintained so that it could be
used to determine the pre-accident location of all underground personnel and was not reliable
during the post-accident setting. On the morning of August 16, audio recordings of the pager
phone system verified that Dale Black’s location was reported to the AMS operator as he
traveled between zones toward the clean-up area. However, Black was not entered into the
tracking system during this shift. All other miners in the clean-up area were properly tracked.
Immediately following the August 16 accident, the mine pager phone system was needed to
coordinate rescue efforts from the command center. Miners attempting to call out as they
changed zones interfered with communications between the command center and rescue workers
at the accident site. This prompted mine management to temporarily limit use of the phone
system. Vehicles transporting injured miners, including cases where CPR were being performed,
did not stop to call out zone locations as this would have delayed potentially life-saving
treatment. Additionally, some rescue workers rapidly responded to the accident scene without
reporting their movements. This caused an increase in time and confusion when accounting for
all persons after the mine had been evacuated. However, the tracking system failures did not
cause any delays in medical treatment to the injured miners.
Local Coordination
Following the August 16 accident, the response was rapid. Immediately after the accident
occurred, a call went out to 911 emergency medical services. Several ambulance services in the
area responded, including medical evacuation helicopters. Medical personnel were stationed at
the mine portal and began medical treatment as the injured exited the mine. At least one
Emergency Medical Technician traveled underground to provide onsite first aid. There were no
delays in treatment or transportation of the injured rescue workers.
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ROOT CAUSE ANALYSIS
An analysis was conducted to identify the most basic causes of the accidents that were
correctable through management controls. Listed below are root causes identified for each
accident and their corresponding corrective actions to prevent a recurrence of the accident.
Root Causes of August 6, 2007, Accident
1. Root Cause: GRI and AAI’s mine design was not compatible with effective control of
coal bursts. The dimensions of pillars within the active workings, as well as dimensions of
the adjoining barrier pillars, did not provide sufficient strength to withstand stresses. AAI’s
ARMPS analysis of the pillar dimensions was inappropriately applied and their LaModel
analysis was faulty. These analyses were not adequately reviewed for correctness and
results were not accurately reported.
Corrective Action: Engineering procedures should ensure analyses are conducted in
accordance with established guidelines. Correspondence, input files, and output files should
be adequately reviewed for accuracy at each stage of model analysis. Systematic
verification of numerical model construction, parameter selection, and model calibration
should be conducted to ensure that output represents known conditions. Reports should
accurately convey analyses results, provide clear recommendations, and include
justifications for any departure from established guidelines. Pillars and mining methods
should be designed to maintain ventilation systems, including separation from adjacent
sealed areas.
2. Root Cause: GRI did not take adequate steps to prevent recurrences of coal outburst
accidents. Revisions of the roof control plan were not proposed by the operator when
conditions at the mine indicated that the plan was not adequate or suitable for controlling
the roof, face, ribs or coal bursts. These conditions included roof and rib burst damage,
miners being struck by coal, and several coal outburst accidents that were not reported to
MSHA as required by 30 CFR 50.10.
Corrective Action: All coal outburst accidents must be properly reported to MSHA and
mapped to accurately portray accident history for determining adequacy of the approved
roof control plan. Adequate steps to prevent the recurrence of all coal outburst accidents
should be taken before mining is resumed. Revisions to the roof control plan must be
proposed when the plan is not suitable for controlling coal bursts.
3. Root Cause: GRI did not follow their approved roof control plan and pillar design
parameters. The barrier south of the No. 1 entry was mined between crosscut 142 and
crosscut 139 where pillar recovery was not permitted by the approved roof control plan.
Pillars were mined to a greater height by mining of bottom coal and entries were centered
differently than modeled.
Corrective Action: Mine operators must follow their approved roof control plan. Persons
analyzing mine designs should be provided with all pertinent aspects of intended mining,
and any revisions to such information. Mine operators should consult with analysts before
implementing any changes to modeled mining plans.
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4. Root Cause: GRI included incorrect information in the roof control plan submitted to
MSHA for approval. GRI submitted roof control plans based on AAI’s inaccurate
evaluations, which determined that projected mining would be safe and pillar and barrier
dimensions were appropriate when in fact they were not.
Corrective Action: Mine operators should ensure that proposed roof control plans are
suitable for prevailing geological conditions and the mining system to be used at the mine.
Corrective actions regarding MSHA’s roof control plan approval process will be addressed
in the findings of an independent review team.
Root Causes of August 16, 2007, Accident
All root causes for the August 6 accident can also be attributed to the August 16 accident; the
following are additional root causes unique to the latter. Unlike the August 6 accident, viable
alternatives were not available for most causes of the August 16 accident, which imposed
greater risks on rescue workers than would be accepted for normal mining. The prospect of
saving the entrapped miners’ lives warranted the heroic efforts of the rescue workers. The
greater risks imposed on the rescue workers underscore the high degree of care that must be
taken by mine operators to prevent catastrophic pillar failures as occurred on August 6.
1. Root Cause: Information was not sufficient to determine underground conditions
prior to August 16.
Corrective Action: Due to the high level of risk inherent to rescue efforts, all resources,
including drilling resources, should be deployed to obtain information necessary to
determine underground conditions in the shortest possible timeframe. Information is
critical to evaluate the potential success of rescue efforts.
2. Root Cause: The method used for reaching the entrapped miners required removal
of compacted coal debris, which reduced confinement pressure on the failed pillars.
Corrective Action: None. No viable excavation method exists to rescue the entrapped
miners.
3. Root Cause: Ground support systems were not capable of controlling maximum
potential coal burst intensity.
Corrective Action: None. Viable support systems capable of sustaining significantly
greater lateral loads are not available. Methods do not exist to determine the maximum
coal burst intensity that the ground support system would be subjected to.
4. Root Cause: Installation of ground control systems required rescue workers to
travel near areas with high burst potential.
Corrective Action: None. No means exists to remotely install the ground control
systems.
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CONCLUSION
The catastrophic coal outburst accident on August 6, 2007, initiated near the pillar line in the
South Barrier section and propagated outby, resulting in a magnitude 3.9 mining related
seismic event. Within seconds, pillars failed over a distance of approximately ½-mile,
expelling coal into the mine openings. The six miners working on the section likely received
fatal injuries from the ejected coal as it violently filled the entries. The barrier pillars to the
north and south of the South Barrier section entries also failed, inundating the section with
lethally oxygen-deficient air from the adjacent sealed area(s) and may have contributed to the
death of the miners. The extensive pillar failure and subsequent inundation of the section by
oxygen-deficient air occurred because of inadequacies in the mine design, faulty pillar
recovery methods, and failure to adequately revise mining plans following coal burst
accidents. The mine design was inadequate because it incorporated recommendations from
AAI’s flawed LaModel and ARMPS analyses. These design issues and faulty pillar recovery
methods resulted in pillar dimensions that were not compatible with effective ground control
to prevent coal bursts under the deep overburden and high abutment loading that existed in the
South Barrier section.
AAI’s ARMPS analysis was inappropriately applied. They used an area for back-analysis
that experienced poor ground conditions and did not consider the barrier pillar stability factors
in any of their analyses. The mine-specific ARMPS design threshold proved to be invalid, as
evidenced by the March 7 and 10, 2007, coal outburst accidents and other pillar failures. GRI
did not propose revisions to their roof control plan before resuming mining following the
March 7 coal outburst. Despite these accidents, AAI recommended a pillar design for the
South Barrier section that had a lower calculated pillar stability factor than the failed pillars in
the North Barrier section, lower than recommended by NIOSH criteria, and lower than
established by their mine specific criteria. AAI performed the ARMPS analysis for the South
Barrier section, but did not include these results in their reports that were presented to MSHA
in support of GRI’s plan submittal.
AAI’s LaModel analysis was flawed. They used an area for back-analysis that was
inaccessible and could not be verified for known ground conditions, which resulted in an
unreliable calibration and the selection of inappropriate model parameters. These model
parameters overestimated pillar strength and underestimated load. AAI modeled pillars with
cores that would never fail regardless of the applied load, which was not consistent with
realistic mining conditions. They did not consider the indestructible nature of the modeled
pillars in their interpretation of the results. Modeled abutment stresses from the adjacent
longwall panels were underestimated and inconsistent with observed ground behavior and
previous studies at this and nearby mines. AAI managers did not review input and output
files for accuracy and completeness. They also did not review vertical stress and total
displacement output at full scale, which would have shown unrealistic results and indicated
that corrections were needed to the model. Following the March 10 coal outburst accident,
AAI modified the model, but failed to correct the significant model flaws. They did not make
further corrections to the model when this analysis result still did not accurately depict known
failures that AAI and GRI observed in the North Barrier section.
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The mine designs recommended by AAI and implemented in part by GRI did not provide
adequate ground stability to maintain the ventilation system. The designs did not consider the
effects of barrier pillar and remnant barrier pillar instability on separation of the working
section from the adjacent sealed areas. Failure of the barrier pillars or remnant barrier pillars
resulted in inundation of the section by lethally oxygen-deficient air. AAI and GRI also did
not consider the effects of ground stability on ventilation controls in the bleeder system. GRI
allowed frequent destruction of ventilation controls by ground movement and by air blasts
from caving. GRI mined cuts from the barrier pillar in the South Barrier section between
crosscuts 139 and 142 intended to be left unmined to protect the bleeder system.
GRI employed a mine design that exposed miners to hazards related to coal bursts. The large
area of similarly sized and marginally stable pillars developed in the Main West and North
and South Barrier sections created a system primed for collapse. Pillar recovery in the South
Barrier section most likely triggered the pillar collapse. GRI’s unapproved mining practices,
including bottom mining and additional barrier slabbing between crosscuts 139 and 142,
reduced the strength of the barrier and increased stress levels in the vicinity of the miners.
GRI failed to have AAI evaluate the design that was actually employed in the South Barrier
section. Proper evaluation of either design, as mined or as proposed, would have indicated
failure.
GRI continued pillar recovery without adequately revising their mining methods when
conditions and accident history indicated that their roof control plan was not suitable for
controlling coal bursts. GRI investigations of non-injury coal burst accidents did not result in
adequate changes of pillar recovery methods to prevent similar occurrences before continued
mining. GRI did not consult with AAI or propose revisions to their roof control plan
following the August 3, 2007, coal outburst accident in the South Barrier section, even though
pillar conditions were similar to the failed area in the North Barrier section.
GRI did not immediately notify MSHA of previous coal outburst accidents. GRI’s failure
denied MSHA the opportunity to investigate these accidents and ensure corrective actions
were taken before mining resumed in the affected area. GRI did not submit written reports of
these accidents to MSHA or plot coal bursts on a mine map available for inspection by
MSHA and miners. The lack of proper documentation and reporting of ground conditions and
related accidents denied MSHA required information for reviews to determine the suitability
of the roof control plan to prevailing geological conditions and mining systems used at the
mine.
The fatal August 16, 2007, coal pillar burst accident occurred when the pillar between the
No. 1 and No. 2 entries failed adjacent to rescue workers as they completed installing ground
support behind the continuous mining machine. Coal ejected from the pillar dislodged
RocProps, steel cables, chain-link fence, and a steel roof support channel, which struck the
rescue workers and filled the entry with approximately four feet of debris. This accident
resulted in the death of two mine employees and one MSHA inspector. Six additional rescue
workers, including an MSHA inspector, received nonfatal injuries.
The August 16 accident occurred because access to the entrapped miners required removal of
compacted coal debris from an entry affected by the August 6 accident. Entry clean-up
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reduced confining pressure on the failed pillars and increased the potential for additional
bursts. Methods for installing ground control systems required rescue workers to travel near
areas with high burst potential. Methods were not available to determine the maximum coal
burst intensity that the ground support system would be subjected to. On August 16, the coal
burst intensity exceeded the capacity of the support system. No alternatives to these methods
were available to rescue the entrapped miners, which imposed greater risks on rescue workers
than would be accepted for normal mining. As a result, only suspension of underground
rescue efforts could have prevented this accident. Prior to the August 16 accident, this was
only likely to occur once definitive information was available to indicate that the entrapped
miners could not have survived the accident. However, information provided by the drilling
operations was not obtained in time to fully evaluate conditions on the section prior to this
accident. The prospect of saving the entrapped miners’ lives warranted the heroic efforts of
the rescue workers. The greater risks imposed on the rescue workers underscore the high
degree of care that must be taken by mine operators to prevent catastrophic pillar failures.
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ENFORCEMENT ACTIONS
An order was issued to Genwal Resources Inc on the morning of the accident, pursuant to section
103 (k) of the Mine Act. The order required the mine operator to obtain MSHA approval of any
plan to rescue the entrapped miners, to recover the affected area of the mine to normal, and to
assure the safety of all persons at this operation. The order was modified numerous times to
allow the rescue and recovery operations to proceed. Additionally, nine enforcement actions
were issued to the mine operator, Genwal Resources Inc, and one to the engineering contractor,
Agapito Associates, Inc., for violations identified as contributing to the causes and effects or
severity of the accident as follows:
Genwal Resources Inc
Type of Issuance: 104 (d) (2) Order
Standard Violated: 30 CFR 75.203 (a)
Gravity: S&S, Fatal, Occurred
Negligence: High
Condition or Practice: During pillar development and recovery in the Main West Barrier
sections, pillar dimensions were not compatible with effective control of coal or rock bursts.
Pillar stability analysis confirms that the length and width of pillars within the active workings,
as well as dimensions of the adjoining barrier pillars, did not provide sufficient strength to
withstand stresses during pillar recovery. This also constitutes a violation of 75.202(a).
On August 6, 2007, a sudden and violent failure of the overstressed coal pillars and barrier
occurred in the Main West South Barrier working section. This instantaneous release of energy
caused the coal ribs to burst, fatally injuring the six man production crew. A second failure of a
coal pillar occurred on August 16, 2007, fatally injuring three rescuers and injuring six other
rescuers. This constituted an unwarrantable failure to comply with a mandatory standard.
Type of Issuance: 104 (d) (2) Order
Standard Violated: 30 CFR 75.203 (a)
Gravity: S&S, Fatal, Occurred
Negligence: High
Condition or Practice: During pillar recovery of the Main West South Barrier section from July
15, 2007, until August 6, 2007, the mining of bottom coal exposed persons to hazards caused by
faulty pillar recovery methods. GRI mined up to five feet of additional bottom coal from the
barrier and the pillars. This resulted in pillars with heights up to 13 feet, as opposed to the
original 8-foot high pillars. This compromised the stability of the pillars. These pillar
dimensions were not compatible with effective control of coal or rock bursts.
On August 6, 2007, a sudden and violent failure of the overstressed coal pillars occurred,
instantaneously releasing large amounts of accumulated energy that exposed miners on the Main
West South Barrier section to hazards related to the coal burst. This constitutes an unwarrantable
failure to comply with a mandatory standard.
Type of Issuance: 104 (d) (2) Order
Standard Violated: 30 CFR 75.223 (a)
Gravity: S&S, Fatal, Occurred
Negligence: High
Condition or Practice: Revisions of the roof control plan were not proposed by the operator
when conditions at the mine indicated that the plan was not adequate or suitable for controlling
the roof, face, ribs or coal bursts. These conditions included bounces, which occurred in the
Main West North Barrier section that resulted in roof and rib damage, and caused miners to fall
onto the mine floor and a reportable coal outburst that occurred on March 7, 2007. The
operator’s failure to make appropriate changes to its roof control plan contributed to the August
174
6, 2007 fatal accident. This constitutes an unwarrantable failure to comply with a mandatory
standard.
Type of Issuance: 104 (d) (2) Order
Standard Violated: 30 CFR 75.223 (a)
Gravity: S&S, Fatal, Occurred
Negligence: High
Condition or Practice: The operator did not propose adequate revisions to the roof control plan
when conditions at the mine indicated that the plan was not adequate or suitable for controlling
the roof, face, ribs or coal bursts. These conditions included bounces that occurred in the Main
West North Barrier section and resulted in roof and rib damage and equipment damage, and a
coal outburst, which occurred on March 10, 2007 and caused substantial damage to the section.
The revisions to the roof control plan proposed following the March 10, 2007 coal outburst did
not make the plan adequate or suitable for controlling the roof, face, ribs or coal or rock bursts.
The operator’s failure to make appropriate changes to its roof control plan contributed to the
August 6, 2007 fatal accident. This was an unwarrantable failure to comply with a mandatory
standard.
Type of Issuance: 104 (d) (2) Order
Standard Violated: 30 CFR 75.223 (a)
Gravity: S&S, Fatal, Occurred
Negligence: Reckless Disregard
Condition or Practice: Revisions of the roof control plan were not proposed by the operator
when conditions at the mine indicated that the plan was not adequate or suitable for controlling
the roof, face, ribs or coal bursts. These conditions included bounces that occurred in the Main
West South Barrier section that resulted in roof and rib damage, and caused miners to fall onto
the mine floor and a reportable coal outburst that occurred on August 3, 2007. The operator’s
failure to make appropriate changes to its roof control plan contributed to the August 6, 2007
fatal accident. This constitutes an unwarrantable failure to comply with a mandatory standard.
Type of Issuance: 104 (d) (2) Order
Standard Violated: 30 CFR 75.220 (a) (1)
Gravity: S&S, Fatal, Occurred
Negligence: Reckless Disregard
Condition or Practice: 30 CFR 75.220(a) (1) requires that a mine operator develop and follow a
roof control plan approved by the District Manager. The mine operator did not follow the
approved roof control plan amendment dated June 15, 2007 addressing pillar recovery mining in
the Main West South Barrier. The site specific approved plan does not permit mining in any of
the barrier to the south of the No. 1 entry between crosscut 142 and crosscut 139. The barrier
south of the No. 1 entry was mined in this restricted mining area. This mining worsened the
stability of the barrier and pillars in this area and contributed to the fatal accident on August 6.
This violation constitutes an unwarrantable failure to comply with a mandatory standard.
Type of Issuance: 104 (d) (2) Order
Standard Violated: 30 CFR 50.10
Gravity: S&S, Fatal, Occurred
Negligence: Reckless Disregard
Condition or Practice: The operator did not immediately contact MSHA at once without delay
and within 15 minutes at the toll-free number, 1-800-746-1553, once the operator knew that an
accident in the Main West North Barrier section occurred on March 7, 2007. A coal outburst
threw coal into the mine openings, disrupting regular mining activity for more than one hour.
The accident was not reported to MSHA pursuant to this standard. Without proper notification,
MSHA had no opportunity to investigate this accident. The failure to report this accident denied
MSHA an opportunity to investigate it and learn that the mining methods provided inadequate
protections. This failure contributed to the August 6 fatal accident. This violation is an
unwarrantable failure to comply with a mandatory standard.
175
Type of Issuance: 104 (d) (2) Order
Standard Violated: 30 CFR 50.10
Gravity: S&S, Fatal, Occurred
Negligence: Reckless Disregard
Condition or Practice: The operator did not immediately contact MSHA at once without delay
and within 15 minutes at the toll-free number, 1-800-746-1553, once the operator knew that an
accident in the Main West North Barrier section occurred on March 10, 2007. A coal outburst
threw coal into the mine openings, disrupting regular mining activity for more than one hour.
The accident was not reported to MSHA pursuant to this standard. The failure to report this
accident denied MSHA an opportunity to investigate it and learn that the mining methods
provided inadequate protections. This failure contributed to the August 6 fatal accident. This
violation is an unwarrantable failure to comply with a mandatory standard.
Type of Issuance: 104 (d) (2) Order
Standard Violated: 30 CFR 50.10
Gravity: S&S, Fatal, Occurred
Negligence: Reckless Disregard
Condition or Practice: The operator did not immediately contact MSHA at once without delay
and within 15 minutes at the toll-free number, 1-800-746-1553, once the operator knew that an
accident in the Main West South Barrier section occurred on August 3, 2007. A coal outburst
threw coal into the mine openings, disrupting regular mining activity for more than one hour.
The accident was not reported to MSHA pursuant to this standard. The failure to report this
accident denied MSHA an opportunity to investigate it and learn that the mining methods
provided inadequate protections. This failure contributed to the August 6 fatal accident. This
violation is an unwarrantable failure to comply with a mandatory standard.
Agapito Associates Inc.
Type of Issuance: 104 (d) (1) Citation
Standard Violated: 30 CFR 75.203 (a)
Gravity: S&S, Fatal, Occurred
Negligence: Reckless Disregard
Condition or Practice: During pillar development and recovery in the Main West Barrier
sections, pillar dimensions were not compatible with effective control of coal or rock bursts.
Pillar stability analysis confirms that the length and width of pillars within the active workings,
as well as dimensions of the adjoining barrier pillars, did not provide sufficient strength to
withstand stresses during pillar recovery. This also constitutes a violation of 75.202(a).
On August 6, 2007, a sudden and violent failure of the overstressed coal pillars and barrier
occurred in the Main West South Barrier section. This instantaneous release of energy caused
the coal ribs to burst, fatally injuring the six man production crew. A second failure of a coal
pillar occurred on August 16, 2007, fatally injuring three rescuers and injuring six other rescuers.
Contractor, Agapito Associates Inc., (AAI) inaccurately evaluated the conditions and events at
the mine when determining if areas were safe for mining. Based on its results, AAI
recommended to the operator that mining methods were safe and pillar and barrier dimensions
were appropriate when in fact they were not. The negligence of the contractor directly
contributed to the death of nine people. This violation is an unwarrantable failure to comply
with a mandatory standard.
176
Appendix A - Persons Participating in the Investigation
Murray Energy Corporation
Jerry M. Taylor ........................................................................................ Corporate Safety Director
UtahAmerican Energy Inc.
P. Bruce Hill...............................................................................................................President/CEO
Laine Adair ............................................................................................................General Manager
James A. Poulson ..................................................................................................... Safety Manager
Genwal Resources Inc
Gary D. Peacock .............................................................................................Mine Superintendent
Bodee R. Allred ........................................................................................................ Safety Director
Blaine K. Fillmore .............................................................................. Representative of the Miners
Agapito Associates, Inc.
Michael P. Hardy, Ph.D. ..............................................................President, Chairman of the Board
Ware Surveying & Engineering
Cody Ware. .....................................................................................Professional Licensed Surveyor
Neva Ridge Technologies
David Cohen, Ph.D. .......................................................................... Vice President of Engineering
State of Utah
Sherrie Hayashi................................................................................................Labor Commissioner
University of Utah
Walter J. Arabasz, Ph.D............................Director of the University of Utah Seismograph Station
James C. Pechmann, Ph.D. .................................. Associate Professor of Geology and Geophysics
Kristine Pankow, Ph.D................... Asst. Director of the University of Utah Seismograph Stations
Michael K. McCarter, Ph.D. ........................................ Professor and Chair of Mining Engineering
William G. Pariseau, Ph.D............................................................Professor of Mining Engineering
West Virginia University
Keith A. Heasley, Ph.D.................................................................Professor of Mining Engineering
U. S. Geological Survey, Earth Resources Observation and Science Center
Zhong Lu, Ph.D............................................................... Scientist, Radar Project of Land Sciences
Bureau of Land Management
James F. Kohler ............................................................................. Chief, Branch of Solid Minerals
Stephen W. Falk..................................................................................................... Mining Engineer
A-1
Mine Safety and Health Administration
Richard A. Gates.................................................................................................... District Manager
Michael Gauna ....................................................................................................... Mining Engineer
Thomas A. Morley ................................................................................................. Mining Engineer
Joseph R. O’Donnell Jr. ............................................................... Supervisory Coal Mine Inspector
Gary E. Smith............................................................................... Supervisory Coal Mine Inspector
Timothy R. Watkins................................................................................Assistant District Manager
Chris A. Weaver........................................................................... Supervisory Coal Mine Inspector
Joseph C. Zelanko.............................................................................. Supervisory Mining Engineer
Steve Powroznik ........................................................................................Education Field Services
James I. Pruitt........................................................... Coal Mine Safety & Health Inspector Trainee
Michael E. Turner ............................................................................... Health and Safety Specialist
A-2
Appendix B - Victim Data Sheets
B-1
B-2
B-3
B-4
B-5
Appendix C - Safety Zone Map
Appendix D - Mine Development History Map
Appendix E - AAI May 5, 2000, Report
Barrier Pillar to Protect Bleeders for Panel 15, South of West Mains
E-1
E-2
E-3
E-4
E-5
E-6
Appendix F - AAI July 20, 2006, Draft Report
DRAFT-GENWAL Crandall Canyon Mine Main West Barrier Mining Evaluation
F-1
F-2
F-3
F-4
F-5
F-6
F-7
F-8
F-9
F-10
F-11
F-12
F-13
F-14
F-15
F-16
F-17
F-18
F-19
F-20
F-21
F-22
F-23
F-24
F-25
F-26
F-27
F-28
F-29
F-30
F-31
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